LER-1981-003, /01T-0:on 810526,steam Generator 2A Blowdown Sample Isolation Valve Failed to Close Upon Actuation.Caused by Excessive Stem to Packing Friction Due to Dried Out Packing.Packing Gland Adjusted & Valve Stem Lubricated |
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n U. S. NUCLEA'1 CEiULATCY COMMISSION CRC F OEM 364 (7 77)
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8 60 61 oOCKET NUM8ER 68 69 EVENT oATE 74 75 REPORT oATE 80 EVENT DESCRIPTION AND PROGA8LE CONSEOUENCES h lDuring normal operations at 1250 hours0.0145 days <br />0.347 hours <br />0.00207 weeks <br />4.75625e-4 months <br />, on May 26, 1981, attempts to I
o 2 l cycle 2A steam generator blowdown sample isolation valve, 2CV-20 8 3, we re l g o,3 l io g4; lunsuccess ful.
Failure of 2CV-2083 to close when actuated is a technicall l o I s l lviolation of containment integrity as defined in T. S. 15.1.d.
This l
loccurrence is reportable in accordance with T. S.
15.6.9.2.A.2 as l
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3b 36 31 30 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 27 Fi l o t IFailure of 2CV-2083 to close upon actuation was due to excessive stem tol packing friction resulting from dried out packina.
Followina disecve w I i i g jof the probi.em the packing gland was adjusted and the valve stem was I
g l1ubricated.
The valve was tested satisfactorily and returned to I
ii i,i l operation at 1330 hours0.0154 days <br />0.369 hours <br />0.0022 weeks <br />5.06065e-4 months <br /> on May 26, 1981.
At no time was the public l
safety endangered.
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NAME OF PREPARER 8,an,nn5Dr
,e ATTACHMENT TO LICENSEE SVENT REPORT NO. 81-O'13/O lT-0 Wisconsin Electric Power Company Point Beach Nuclear Plant Unit 2 Docket No. 50-301 i
At 1250 hours0.0145 days <br />0.347 hours <br />0.00207 weeks <br />4.75625e-4 months <br /> on May 26, 1981, during normal power operation, Unit 2, "A" steam generator blowdown sample valve, 2CV-20 8 3, failed to close upon a manual remote signal from the control operator.
The attempt to close 2CV-2083 was at the request of Chemistry Group personnel to stroke the valve.
Valve 2CV-2083 is an air-operated containment isolation valve which is required to close automatically upon actuation of containment isolation.
Inoperability of 2CV-2083 is a technical violation of containment integrity as defined in Technical Specification 15.1.d.
This occurrence is reportable in accordance with Technical Specification 15.6.9.2. A.2 as operating in a less conservative manner than the limiting condition of operation specified in Technical Specification 15.3.6.A.a.
After an immediate investigation it was found that 2CV-2083 failed to close due to excessive stem to packing friction resulting from dried out packing.
The packing was adjusted and the valve stem lubricated.
Following a satis-factory operational' test on 2CV-2083, it was returned to an operable status at 1330 hours0.0154 days <br />0.369 hours <br />0.0022 weeks <br />5.06065e-4 months <br /> on May 26, 1981.
The automatic containment isolation function of 2CV-20 83 was installed, in accordance with NUREG-0578, -
during the Unit 2 refueling outage ending on May 22, 1981.
The last operability test of 2CV-2083 was conducted on May 13, 1981, with satisfactory results.
If containment isolation was initiated while 2CV-2083 was inoperable, isolation could be provided via accessible manual valves downstream of 2CV-208 3.
At no time was the public safety endangered.
The nameplate data for 2CV-2083 is as follows:
Manufacturer:
Copes Vulcan Body Size:
3/4" Pressure Rating:
600 psig Type:
D-100-60
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