05000311/LER-1981-023-01, /01T-0:on 810522,main Steam Isolation Valves Failed to Close within Required 5-s During Startup Test. Caused by Design Error.Design Change Developed to Allow for Proper Interaction of Hydraulic & Steam Closing Subsys

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/01T-0:on 810522,main Steam Isolation Valves Failed to Close within Required 5-s During Startup Test. Caused by Design Error.Design Change Developed to Allow for Proper Interaction of Hydraulic & Steam Closing Subsys
ML20004E739
Person / Time
Site: Salem PSEG icon.png
Issue date: 06/02/1981
From: Espey J
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20004E737 List:
References
LER-81-023-01T, LER-81-23-1T, NUDOCS 8106150144
Download: ML20004E739 (1)


LER-1981-023, /01T-0:on 810522,main Steam Isolation Valves Failed to Close within Required 5-s During Startup Test. Caused by Design Error.Design Change Developed to Allow for Proper Interaction of Hydraulic & Steam Closing Subsys
Event date:
Report date:
3111981023R01 - NRC Website

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CRC FORM 366 U. S. NUCLE AR GEGULAToRY COMMISSION (7 77)

LICENSEE EVENT REPORT CONTROL BLOCK. l l

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60 61 DOCKET NUMBER 68 9

EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROB ABL'E CONSEQUENCES b10 g

ring the performance of Start-up TeTt (Sup-53) the Main Steam Isolation Valves y l failed to close within the required 5 seconds. The closing time was verified as l

lo ;4 l l8.63 seconds.

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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l i j o l lThe change over from normal hydraulic closing to emergency steam closing had not l

li ;i j [ allowed for this in eraction. A time delay relay was installed for Unit 2 by DCR-lEC-12 30

,, j7g lDCR-2EC-1229 and the valves were retested satisfactorily at 3.9 seconds.

g gi;3l lwill be incorporated in Unit 1 prior to the next plant start-up.

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% POWER OTHE R STATUS DISCO RY DISCOVERY DESCRIPTION Wh l0 l 0 lC l@l Not Applicable l

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8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUM8ER TYPE DE SCRIPTION LTE] I 01 of Ol@l zl@l NA I

P3RSONNa'IN;U 'IES otSCRe noNh NuMeER lalolol@l 1 8 NA 7

8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY TYPE DE SCRIPTION h!

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68 69 80 NAV OF PREPARER PHONE-

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