05000348/LER-1981-035-03, /03L-0:on 810511,containment Isolation Valve CCW-MOV-3052,was Declared Inoperable When Valve Position Indication Was Lost.Caused by Blown Control Power Fuse.Fuse Replaced

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/03L-0:on 810511,containment Isolation Valve CCW-MOV-3052,was Declared Inoperable When Valve Position Indication Was Lost.Caused by Blown Control Power Fuse.Fuse Replaced
ML20004E199
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 06/05/1981
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20004E191 List:
References
LER-81-035-03L, LER-81-35-3L, NUDOCS 8106110336
Download: ML20004E199 (1)


LER-1981-035, /03L-0:on 810511,containment Isolation Valve CCW-MOV-3052,was Declared Inoperable When Valve Position Indication Was Lost.Caused by Blown Control Power Fuse.Fuse Replaced
Event date:
Report date:
3481981035R03 - NRC Website

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