LER-1980-047, Forwards LER 80-047/03L-0.Detailed Event Analysis Also Submitted |
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d g,,*u COOPER NUCLEAR STATION
- - K ; Nebraska Public Power District
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.CNSS800732 December 16, 1980
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r DEC 2 21980 Mr. K. V. Seyfrit, Director
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. i U.S. Nuclear Regulatory Commission 1
Office of Inspection and Enforcement Region IV JJ' l.[q ' }\\
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611 Ryan Plaza Drive
,D Suite 1000
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9 A,Y 0 81981 -
Arlington, Texas 76011 u.
Dear Sir:
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This report is submitted in accordance with Section 6.7.2.B.2 of t
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Technical Specifications for Cooper Nuclear Station and discusses a
- . ; ic-reportable occurrence that was discovered on November 17, 1980.
In i
eccordance with the requirements of IE Bu'lletin 80-17, Mr. Spangler was notified while he was on site November 18, 1980.,A licensee event report for1n is also enclosed.
Report No.:
50-298-80-47 Report Date:
December 16, 1980 Occurrence Date: November 17, 1980 Facility:
Cooper Nuclear Station Brownville, Nebraska 68321 Identification of Occurrence:
Conditions which may have led to operation in a degraded mode permitted by a limiting condition for operation as delineared in Section 3.5.B of the Technical Specifications.
Conditions Prior to Occurrence:
Reactor was in cold shutdown.
Description of Occ,urrence:
During normal operation of RHR motor operated valves for torus cooling while in cold shutdown, RHR-MO-34A, the "A" Loop suppres-sion pool cooling throttle valve would not operate.
Designation of Apparent Cause of Occurrence:
The operator is'a Limitorque SMB-4 The motor was removed and the key between the motor pinion gear and the motor shaft was found sheared.
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Mr. K. V. Seyfrit December 16, 1980 Page 2.
I Analysis of Occurrence:
RHR-MO-34A is the RHR "A" Loop suppression pool containment valve which isolates the torus from the RHR system.
It is a normally closed valve.
If open during LPCI initiation, it receives a close signal. The subject valve failed iri che closed position.
Had the subject valve faihd in the open position, RHR-MO-39A, the outboard isolation valve, would have closed allowing LPCI injection with the "A" Loop. The torus cooling mode of the "A" Loop of RER was in-operable, however torus cooling could have been supplied by the "B" RER Loop. During this event, both diesel generators and the re-dundant loop of RHR were operable.
This occurrence presented no adverse consequences from the standpoint of public health and safety.
Carrective Action:
The motor, motor shaf t pinion gear, and motor shaft pinion gear key l
were replaced.
The motor shaft and pinion gear were worn due to the motor shaft rotating inside the pinion gear.
This is a re-petitive occurrence, reference LER's 7,6-14, 77-11, and 80-30.
The key was sent to' the manufacturer. Limitorque Corporation, j
for analysis. The results of that analysis indicates that Limitorque installed a key of improper hardness. Machinery history records I
indicated that this operator had never had any maintenance per-t formed on it that would have necessitated removal of the motor.
As was reported on LER 80-30-1, all sizes of Limitorque operators use standard key stock except for sizes SMB-3, 4, and 5.
RHR-MO-34A is a SMB-4.
The proper key stock is 4140 s* eel with a hardness of between 280/320 Brinell.
The failed key had a hardness of 250 The' proper key material was used for the repair.
Brinell.
This failure points out a potential area for concern for other SMB-3's, 4's, and 5's.
Lismisorquewill review-all~cperators-installed,rt g n,,,.3.
'eceedn-
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Limitorque uses the hardened key in all SMB-3, 4, and 5's to reduce parts inventory as all operators do not need the hardened key.
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| 05000298/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000298/LER-1980-001-01, /01T-0:on 800102,during HPCI Turbine Stop Valve Monitor Test,Procedural Steps Were Improperly Completed. Caused by Personnel Error.Occurrence Discussed W/Operations & Instrument Personnel | /01T-0:on 800102,during HPCI Turbine Stop Valve Monitor Test,Procedural Steps Were Improperly Completed. Caused by Personnel Error.Occurrence Discussed W/Operations & Instrument Personnel | | | 05000298/LER-1980-002-03, /03L-0:on 800103,operator Found Valve Stem on HPCI Stop Valve Broken Separating Valve from Operator.Caused by Valve Stem Being Overstressed During Process of Freeing Stop Valve Piston on 790912.Valve Reassembled | /03L-0:on 800103,operator Found Valve Stem on HPCI Stop Valve Broken Separating Valve from Operator.Caused by Valve Stem Being Overstressed During Process of Freeing Stop Valve Piston on 790912.Valve Reassembled | | | 05000298/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000298/LER-1980-003-03, /03L-0:on 800111,during Valve Realignment Per Special Procedure 80-1,PC-230MV Was Not Closing Completely. Caused by Improper Assembly of Gear Limit Switch in Limitorque Model SMB00 Operator | /03L-0:on 800111,during Valve Realignment Per Special Procedure 80-1,PC-230MV Was Not Closing Completely. Caused by Improper Assembly of Gear Limit Switch in Limitorque Model SMB00 Operator | | | 05000298/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000298/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000298/LER-1980-004-03, /03L-0:on 800115,during Normal Operation, Discovered That RHR Valve M018 Was Inoperable.Caused by Failure of GE Relay Coil,Blowing Valve Control Circuit Fuse. Relay Coil Was Replaced & Correct Operation Verified | /03L-0:on 800115,during Normal Operation, Discovered That RHR Valve M018 Was Inoperable.Caused by Failure of GE Relay Coil,Blowing Valve Control Circuit Fuse. Relay Coil Was Replaced & Correct Operation Verified | | | 05000298/LER-1980-005-03, 1-0:on 800116,during Normal Operation,Two through-wall Cracks in Welds in Radiant Energy Conversion North Critical Loop Discovered.Caused by Intergranular Stress Corrosion.Welds Will Be Replaced | 1-0:on 800116,during Normal Operation,Two through-wall Cracks in Welds in Radiant Energy Conversion North Critical Loop Discovered.Caused by Intergranular Stress Corrosion.Welds Will Be Replaced | | | 05000298/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000298/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000298/LER-1980-006-03, /03L-0:on 800222,during Normal Operation,While Hydrotesting Reactor Bldg Fire Sprinkler Sys,Gasket in Flow Switch in Water Line Failed & Water Sprayed Into 125 Volt Dc Starter Racks for Reactor Core Isolation Cooling & RHR | /03L-0:on 800222,during Normal Operation,While Hydrotesting Reactor Bldg Fire Sprinkler Sys,Gasket in Flow Switch in Water Line Failed & Water Sprayed Into 125 Volt Dc Starter Racks for Reactor Core Isolation Cooling & RHR | | | 05000298/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000298/LER-1980-007-03, /03L-0:on 800310,during Surveillance Testing of Standby Liquid Control Pumps,Standby Liquid Control Pump 1B Would Pump Only 36.5 Gpm at 1,215 Psig.Caused by Wear & Pitting to Seating Surface | /03L-0:on 800310,during Surveillance Testing of Standby Liquid Control Pumps,Standby Liquid Control Pump 1B Would Pump Only 36.5 Gpm at 1,215 Psig.Caused by Wear & Pitting to Seating Surface | | | 05000298/LER-1980-008-03, /03L-0:on 800312,during Insp of Reactor Core Isolation Cooling Turbine,Two Buckets on Turbine Wheel Were Discovered Damaged.Caused by Foreign Object Striking Wheel During Operation.Investigation Is Continuing | /03L-0:on 800312,during Insp of Reactor Core Isolation Cooling Turbine,Two Buckets on Turbine Wheel Were Discovered Damaged.Caused by Foreign Object Striking Wheel During Operation.Investigation Is Continuing | | | 05000298/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000298/LER-1980-009-03, /03L-0:on 800329,during Refueling outage,through- Wall Crack Discovered on Upstream Side of Isolation Valve to REC Noncritical Header.Cracked Weld Characteristic of Intergranular Stress Corrosion.Weld Will Be Repaired | /03L-0:on 800329,during Refueling outage,through- Wall Crack Discovered on Upstream Side of Isolation Valve to REC Noncritical Header.Cracked Weld Characteristic of Intergranular Stress Corrosion.Weld Will Be Repaired | | | 05000298/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000298/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000298/LER-1980-010-03, /03L-0:on 800408,subsurface Planar Flax in Weld CSB-BF-12 Core Spray B Loop Found During Augmented Inservice Insp.Caused by Const Defect.Defect Removed,Repaired & Successfully Volumetrically Examined Per ASME Code | /03L-0:on 800408,subsurface Planar Flax in Weld CSB-BF-12 Core Spray B Loop Found During Augmented Inservice Insp.Caused by Const Defect.Defect Removed,Repaired & Successfully Volumetrically Examined Per ASME Code | | | 05000298/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000298/LER-1980-011-03, /03L-0:on 800418,check Valves Upstream of Accumulators Had Excessive Back Leakage.Caused by BUNA-N Seat Embrittlement Due to Age.Check Valve Seats Replaced W/Ethylene Propylene Matl.Valves Bench Tested | /03L-0:on 800418,check Valves Upstream of Accumulators Had Excessive Back Leakage.Caused by BUNA-N Seat Embrittlement Due to Age.Check Valve Seats Replaced W/Ethylene Propylene Matl.Valves Bench Tested | | | 05000298/LER-1980-012-03, /03L-0:on 800521,during Local Leak Rate Test,Nine Penetrations Found Leaking Excessively.Caused by Normal Wear.Seal Ring Replaced,Seats Polished,Packing Tightened & Ring Seal Cleaned | /03L-0:on 800521,during Local Leak Rate Test,Nine Penetrations Found Leaking Excessively.Caused by Normal Wear.Seal Ring Replaced,Seats Polished,Packing Tightened & Ring Seal Cleaned | | | 05000298/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000298/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000298/LER-1980-013-03, /03L-0:on 800516,during Surveillance Procedure on Primary Containment Isolation Valve Timing,Rhr Discharge to Radwaste Inboard Isolation Failed to Close in Time.Caused by Failure to Check Stroke Time After Maint | /03L-0:on 800516,during Surveillance Procedure on Primary Containment Isolation Valve Timing,Rhr Discharge to Radwaste Inboard Isolation Failed to Close in Time.Caused by Failure to Check Stroke Time After Maint | | | 05000298/LER-1980-014-03, /03L-0:on 800518,while Performing Sp 6.3.13.1, Relay 14A-K2B Was Found de-energized,preventing Start of Core Spray Pump on Normal Power.Superflous Contacts Were Inadvertently Left Connected in Core Spray Pump Circuits | /03L-0:on 800518,while Performing Sp 6.3.13.1, Relay 14A-K2B Was Found de-energized,preventing Start of Core Spray Pump on Normal Power.Superflous Contacts Were Inadvertently Left Connected in Core Spray Pump Circuits | | | 05000298/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000298/LER-1980-015-03, /03L-0:on 800606,during Control Rod Scramtime testing,full-in Control Rods Incorrectly Scrammed & Fully Withdrawn.Caused by Personnel Error.Rod Returned to Correct Position.Procedure Modified | /03L-0:on 800606,during Control Rod Scramtime testing,full-in Control Rods Incorrectly Scrammed & Fully Withdrawn.Caused by Personnel Error.Rod Returned to Correct Position.Procedure Modified | | | 05000298/LER-1980-015, Forwards LER 80-015/03L-0 | Forwards LER 80-015/03L-0 | | | 05000298/LER-1980-016, Forwards LER 80-016/01T-0 | Forwards LER 80-016/01T-0 | | | 05000298/LER-1980-016-01, /01T-0:on 800707,during Normal Operation,D RHR Svc Water Booster Pump Taken Out of Svc for Longer than 24-h for Preventive Maint.Pump Overhauled After Tests Per ASME Section XI | /01T-0:on 800707,during Normal Operation,D RHR Svc Water Booster Pump Taken Out of Svc for Longer than 24-h for Preventive Maint.Pump Overhauled After Tests Per ASME Section XI | | | 05000298/LER-1980-017, Forwards LER 80-017/03L-0 | Forwards LER 80-017/03L-0 | | | 05000298/LER-1980-017-03, /03L-0:on 800618,during Surveillance Testing of HPCI Steam Line Low Pressure Instruments,Hpci Steam Supply Was Isolated Leaving Sys Inoperable.Probably Caused by Failure of Pressure Switch HPCI-PS-68B | /03L-0:on 800618,during Surveillance Testing of HPCI Steam Line Low Pressure Instruments,Hpci Steam Supply Was Isolated Leaving Sys Inoperable.Probably Caused by Failure of Pressure Switch HPCI-PS-68B | | | 05000298/LER-1980-018, Forwards LER 80-018/03L-0 | Forwards LER 80-018/03L-0 | | | 05000298/LER-1980-018-03, /03L-0:on 800623,during Performance of Surveillance Procedure 6.2.2.3.1,HPCI Steam Line High Flow Test,Procedural Step Overlooked,Resulting in HPCI Line Isolation.Caused by Personnel Error | /03L-0:on 800623,during Performance of Surveillance Procedure 6.2.2.3.1,HPCI Steam Line High Flow Test,Procedural Step Overlooked,Resulting in HPCI Line Isolation.Caused by Personnel Error | | | 05000298/LER-1980-019-01, /01T-0:on 800709,condenser Cooling Water Outlet Temp Limit of 102 F Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades.Event Terminated Upon Power Reduction | /01T-0:on 800709,condenser Cooling Water Outlet Temp Limit of 102 F Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades.Event Terminated Upon Power Reduction | | | 05000298/LER-1980-019, Forwards LER 80-019/04T-0 | Forwards LER 80-019/04T-0 | | | 05000298/LER-1980-020, Forwards LER 80-020/04T-0 | Forwards LER 80-020/04T-0 | | | 05000298/LER-1980-020-04, /04T-0:on 800710,during Normal Operation,Condenser Cooling Water Outlet Temp Limit Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades.River Temp Decreased Naturally | /04T-0:on 800710,during Normal Operation,Condenser Cooling Water Outlet Temp Limit Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades.River Temp Decreased Naturally | | | 05000298/LER-1980-021, Forwards LER 80-021/03L-0 | Forwards LER 80-021/03L-0 | | | 05000298/LER-1980-021-03, /03L-0:on 800622,while Performing Routine Surveillance Test procedure,6.3.9.4,MSIV-86A Was Found to Have Closing Time Faster than Tech Spec Allowance.Caused by Setting MSIV-86A Too Close to Fast Limit During Shutdown | /03L-0:on 800622,while Performing Routine Surveillance Test procedure,6.3.9.4,MSIV-86A Was Found to Have Closing Time Faster than Tech Spec Allowance.Caused by Setting MSIV-86A Too Close to Fast Limit During Shutdown | | | 05000298/LER-1980-022-03, /03L-0:on 800629,during Normal Operation,While Discharging RHR to Radwaste,Inboard Throttle Isolation Valve RHR-MO-57 Could Not Be Manually or Remotely Operated.Caused by Seat Jamming Disc.Seat Replaced & Valve Ordered | /03L-0:on 800629,during Normal Operation,While Discharging RHR to Radwaste,Inboard Throttle Isolation Valve RHR-MO-57 Could Not Be Manually or Remotely Operated.Caused by Seat Jamming Disc.Seat Replaced & Valve Ordered | | | 05000298/LER-1980-022, Forwards Updated LER 80-022/03L-1 | Forwards Updated LER 80-022/03L-1 | | | 05000298/LER-1980-023-04, /04T-0:on 800714,during Normal Operation,Condenser Cooling Water Outlet Temp Limit of 103 F Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades | /04T-0:on 800714,during Normal Operation,Condenser Cooling Water Outlet Temp Limit of 103 F Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades | | | 05000298/LER-1980-023, Forwards LER 80-023/04T-0 | Forwards LER 80-023/04T-0 | | | 05000298/LER-1980-024-04, /04T-0:on 800715,during Normal Operation,Condenser Cooling Water Outlet Temp Limit Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades | /04T-0:on 800715,during Normal Operation,Condenser Cooling Water Outlet Temp Limit Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades | | | 05000298/LER-1980-024, Forwards LER 80-024/04T-0 | Forwards LER 80-024/04T-0 | | | 05000298/LER-1980-025, Forwards LER 80-025/04T-0 | Forwards LER 80-025/04T-0 | | | 05000298/LER-1980-025-04, /04T-0:on 800716,during Normal Operation,Condenser Cooling Water Outlet Temp Limit Exceeded Tech Specs.Caused by High River Temp & Removal of Rows of Low Presssure Turbine Blades.Event Terminated When Temp Decreased | /04T-0:on 800716,during Normal Operation,Condenser Cooling Water Outlet Temp Limit Exceeded Tech Specs.Caused by High River Temp & Removal of Rows of Low Presssure Turbine Blades.Event Terminated When Temp Decreased | |
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