| | | Reporting criterion |
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| 05000298/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | |
| 05000298/LER-1980-001-01, /01T-0:on 800102,during HPCI Turbine Stop Valve Monitor Test,Procedural Steps Were Improperly Completed. Caused by Personnel Error.Occurrence Discussed W/Operations & Instrument Personnel | /01T-0:on 800102,during HPCI Turbine Stop Valve Monitor Test,Procedural Steps Were Improperly Completed. Caused by Personnel Error.Occurrence Discussed W/Operations & Instrument Personnel | |
| 05000298/LER-1980-002-03, /03L-0:on 800103,operator Found Valve Stem on HPCI Stop Valve Broken Separating Valve from Operator.Caused by Valve Stem Being Overstressed During Process of Freeing Stop Valve Piston on 790912.Valve Reassembled | /03L-0:on 800103,operator Found Valve Stem on HPCI Stop Valve Broken Separating Valve from Operator.Caused by Valve Stem Being Overstressed During Process of Freeing Stop Valve Piston on 790912.Valve Reassembled | |
| 05000298/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | |
| 05000298/LER-1980-003-03, /03L-0:on 800111,during Valve Realignment Per Special Procedure 80-1,PC-230MV Was Not Closing Completely. Caused by Improper Assembly of Gear Limit Switch in Limitorque Model SMB00 Operator | /03L-0:on 800111,during Valve Realignment Per Special Procedure 80-1,PC-230MV Was Not Closing Completely. Caused by Improper Assembly of Gear Limit Switch in Limitorque Model SMB00 Operator | |
| 05000298/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | |
| 05000298/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | |
| 05000298/LER-1980-004-03, /03L-0:on 800115,during Normal Operation, Discovered That RHR Valve M018 Was Inoperable.Caused by Failure of GE Relay Coil,Blowing Valve Control Circuit Fuse. Relay Coil Was Replaced & Correct Operation Verified | /03L-0:on 800115,during Normal Operation, Discovered That RHR Valve M018 Was Inoperable.Caused by Failure of GE Relay Coil,Blowing Valve Control Circuit Fuse. Relay Coil Was Replaced & Correct Operation Verified | |
| 05000298/LER-1980-005-03, 1-0:on 800116,during Normal Operation,Two through-wall Cracks in Welds in Radiant Energy Conversion North Critical Loop Discovered.Caused by Intergranular Stress Corrosion.Welds Will Be Replaced | 1-0:on 800116,during Normal Operation,Two through-wall Cracks in Welds in Radiant Energy Conversion North Critical Loop Discovered.Caused by Intergranular Stress Corrosion.Welds Will Be Replaced | |
| 05000298/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | |
| 05000298/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | |
| 05000298/LER-1980-006-03, /03L-0:on 800222,during Normal Operation,While Hydrotesting Reactor Bldg Fire Sprinkler Sys,Gasket in Flow Switch in Water Line Failed & Water Sprayed Into 125 Volt Dc Starter Racks for Reactor Core Isolation Cooling & RHR | /03L-0:on 800222,during Normal Operation,While Hydrotesting Reactor Bldg Fire Sprinkler Sys,Gasket in Flow Switch in Water Line Failed & Water Sprayed Into 125 Volt Dc Starter Racks for Reactor Core Isolation Cooling & RHR | |
| 05000298/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | |
| 05000298/LER-1980-007-03, /03L-0:on 800310,during Surveillance Testing of Standby Liquid Control Pumps,Standby Liquid Control Pump 1B Would Pump Only 36.5 Gpm at 1,215 Psig.Caused by Wear & Pitting to Seating Surface | /03L-0:on 800310,during Surveillance Testing of Standby Liquid Control Pumps,Standby Liquid Control Pump 1B Would Pump Only 36.5 Gpm at 1,215 Psig.Caused by Wear & Pitting to Seating Surface | |
| 05000298/LER-1980-008-03, /03L-0:on 800312,during Insp of Reactor Core Isolation Cooling Turbine,Two Buckets on Turbine Wheel Were Discovered Damaged.Caused by Foreign Object Striking Wheel During Operation.Investigation Is Continuing | /03L-0:on 800312,during Insp of Reactor Core Isolation Cooling Turbine,Two Buckets on Turbine Wheel Were Discovered Damaged.Caused by Foreign Object Striking Wheel During Operation.Investigation Is Continuing | |
| 05000298/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | |
| 05000298/LER-1980-009-03, /03L-0:on 800329,during Refueling outage,through- Wall Crack Discovered on Upstream Side of Isolation Valve to REC Noncritical Header.Cracked Weld Characteristic of Intergranular Stress Corrosion.Weld Will Be Repaired | /03L-0:on 800329,during Refueling outage,through- Wall Crack Discovered on Upstream Side of Isolation Valve to REC Noncritical Header.Cracked Weld Characteristic of Intergranular Stress Corrosion.Weld Will Be Repaired | |
| 05000298/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | |
| 05000298/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | |
| 05000298/LER-1980-010-03, /03L-0:on 800408,subsurface Planar Flax in Weld CSB-BF-12 Core Spray B Loop Found During Augmented Inservice Insp.Caused by Const Defect.Defect Removed,Repaired & Successfully Volumetrically Examined Per ASME Code | /03L-0:on 800408,subsurface Planar Flax in Weld CSB-BF-12 Core Spray B Loop Found During Augmented Inservice Insp.Caused by Const Defect.Defect Removed,Repaired & Successfully Volumetrically Examined Per ASME Code | |
| 05000298/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | |
| 05000298/LER-1980-011-03, /03L-0:on 800418,check Valves Upstream of Accumulators Had Excessive Back Leakage.Caused by BUNA-N Seat Embrittlement Due to Age.Check Valve Seats Replaced W/Ethylene Propylene Matl.Valves Bench Tested | /03L-0:on 800418,check Valves Upstream of Accumulators Had Excessive Back Leakage.Caused by BUNA-N Seat Embrittlement Due to Age.Check Valve Seats Replaced W/Ethylene Propylene Matl.Valves Bench Tested | |
| 05000298/LER-1980-012-03, /03L-0:on 800521,during Local Leak Rate Test,Nine Penetrations Found Leaking Excessively.Caused by Normal Wear.Seal Ring Replaced,Seats Polished,Packing Tightened & Ring Seal Cleaned | /03L-0:on 800521,during Local Leak Rate Test,Nine Penetrations Found Leaking Excessively.Caused by Normal Wear.Seal Ring Replaced,Seats Polished,Packing Tightened & Ring Seal Cleaned | |
| 05000298/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | |
| 05000298/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | |
| 05000298/LER-1980-013-03, /03L-0:on 800516,during Surveillance Procedure on Primary Containment Isolation Valve Timing,Rhr Discharge to Radwaste Inboard Isolation Failed to Close in Time.Caused by Failure to Check Stroke Time After Maint | /03L-0:on 800516,during Surveillance Procedure on Primary Containment Isolation Valve Timing,Rhr Discharge to Radwaste Inboard Isolation Failed to Close in Time.Caused by Failure to Check Stroke Time After Maint | |
| 05000298/LER-1980-014-03, /03L-0:on 800518,while Performing Sp 6.3.13.1, Relay 14A-K2B Was Found de-energized,preventing Start of Core Spray Pump on Normal Power.Superflous Contacts Were Inadvertently Left Connected in Core Spray Pump Circuits | /03L-0:on 800518,while Performing Sp 6.3.13.1, Relay 14A-K2B Was Found de-energized,preventing Start of Core Spray Pump on Normal Power.Superflous Contacts Were Inadvertently Left Connected in Core Spray Pump Circuits | |
| 05000298/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | |
| 05000298/LER-1980-015-03, /03L-0:on 800606,during Control Rod Scramtime testing,full-in Control Rods Incorrectly Scrammed & Fully Withdrawn.Caused by Personnel Error.Rod Returned to Correct Position.Procedure Modified | /03L-0:on 800606,during Control Rod Scramtime testing,full-in Control Rods Incorrectly Scrammed & Fully Withdrawn.Caused by Personnel Error.Rod Returned to Correct Position.Procedure Modified | |
| 05000298/LER-1980-015, Forwards LER 80-015/03L-0 | Forwards LER 80-015/03L-0 | |
| 05000298/LER-1980-016, Forwards LER 80-016/01T-0 | Forwards LER 80-016/01T-0 | |
| 05000298/LER-1980-016-01, /01T-0:on 800707,during Normal Operation,D RHR Svc Water Booster Pump Taken Out of Svc for Longer than 24-h for Preventive Maint.Pump Overhauled After Tests Per ASME Section XI | /01T-0:on 800707,during Normal Operation,D RHR Svc Water Booster Pump Taken Out of Svc for Longer than 24-h for Preventive Maint.Pump Overhauled After Tests Per ASME Section XI | |
| 05000298/LER-1980-017, Forwards LER 80-017/03L-0 | Forwards LER 80-017/03L-0 | |
| 05000298/LER-1980-017-03, /03L-0:on 800618,during Surveillance Testing of HPCI Steam Line Low Pressure Instruments,Hpci Steam Supply Was Isolated Leaving Sys Inoperable.Probably Caused by Failure of Pressure Switch HPCI-PS-68B | /03L-0:on 800618,during Surveillance Testing of HPCI Steam Line Low Pressure Instruments,Hpci Steam Supply Was Isolated Leaving Sys Inoperable.Probably Caused by Failure of Pressure Switch HPCI-PS-68B | |
| 05000298/LER-1980-018, Forwards LER 80-018/03L-0 | Forwards LER 80-018/03L-0 | |
| 05000298/LER-1980-018-03, /03L-0:on 800623,during Performance of Surveillance Procedure 6.2.2.3.1,HPCI Steam Line High Flow Test,Procedural Step Overlooked,Resulting in HPCI Line Isolation.Caused by Personnel Error | /03L-0:on 800623,during Performance of Surveillance Procedure 6.2.2.3.1,HPCI Steam Line High Flow Test,Procedural Step Overlooked,Resulting in HPCI Line Isolation.Caused by Personnel Error | |
| 05000298/LER-1980-019-01, /01T-0:on 800709,condenser Cooling Water Outlet Temp Limit of 102 F Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades.Event Terminated Upon Power Reduction | /01T-0:on 800709,condenser Cooling Water Outlet Temp Limit of 102 F Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades.Event Terminated Upon Power Reduction | |
| 05000298/LER-1980-019, Forwards LER 80-019/04T-0 | Forwards LER 80-019/04T-0 | |
| 05000298/LER-1980-020, Forwards LER 80-020/04T-0 | Forwards LER 80-020/04T-0 | |
| 05000298/LER-1980-020-04, /04T-0:on 800710,during Normal Operation,Condenser Cooling Water Outlet Temp Limit Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades.River Temp Decreased Naturally | /04T-0:on 800710,during Normal Operation,Condenser Cooling Water Outlet Temp Limit Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades.River Temp Decreased Naturally | |
| 05000298/LER-1980-021, Forwards LER 80-021/03L-0 | Forwards LER 80-021/03L-0 | |
| 05000298/LER-1980-021-03, /03L-0:on 800622,while Performing Routine Surveillance Test procedure,6.3.9.4,MSIV-86A Was Found to Have Closing Time Faster than Tech Spec Allowance.Caused by Setting MSIV-86A Too Close to Fast Limit During Shutdown | /03L-0:on 800622,while Performing Routine Surveillance Test procedure,6.3.9.4,MSIV-86A Was Found to Have Closing Time Faster than Tech Spec Allowance.Caused by Setting MSIV-86A Too Close to Fast Limit During Shutdown | |
| 05000298/LER-1980-022-03, /03L-0:on 800629,during Normal Operation,While Discharging RHR to Radwaste,Inboard Throttle Isolation Valve RHR-MO-57 Could Not Be Manually or Remotely Operated.Caused by Seat Jamming Disc.Seat Replaced & Valve Ordered | /03L-0:on 800629,during Normal Operation,While Discharging RHR to Radwaste,Inboard Throttle Isolation Valve RHR-MO-57 Could Not Be Manually or Remotely Operated.Caused by Seat Jamming Disc.Seat Replaced & Valve Ordered | |
| 05000298/LER-1980-022, Forwards Updated LER 80-022/03L-1 | Forwards Updated LER 80-022/03L-1 | |
| 05000298/LER-1980-023-04, /04T-0:on 800714,during Normal Operation,Condenser Cooling Water Outlet Temp Limit of 103 F Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades | /04T-0:on 800714,during Normal Operation,Condenser Cooling Water Outlet Temp Limit of 103 F Was Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades | |
| 05000298/LER-1980-023, Forwards LER 80-023/04T-0 | Forwards LER 80-023/04T-0 | |
| 05000298/LER-1980-024-04, /04T-0:on 800715,during Normal Operation,Condenser Cooling Water Outlet Temp Limit Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades | /04T-0:on 800715,during Normal Operation,Condenser Cooling Water Outlet Temp Limit Exceeded.Caused by Abnormally High River Temp & Removal of Several Rows of Low Pressure Turbine Blades | |
| 05000298/LER-1980-024, Forwards LER 80-024/04T-0 | Forwards LER 80-024/04T-0 | |
| 05000298/LER-1980-025, Forwards LER 80-025/04T-0 | Forwards LER 80-025/04T-0 | |
| 05000298/LER-1980-025-04, /04T-0:on 800716,during Normal Operation,Condenser Cooling Water Outlet Temp Limit Exceeded Tech Specs.Caused by High River Temp & Removal of Rows of Low Presssure Turbine Blades.Event Terminated When Temp Decreased | /04T-0:on 800716,during Normal Operation,Condenser Cooling Water Outlet Temp Limit Exceeded Tech Specs.Caused by High River Temp & Removal of Rows of Low Presssure Turbine Blades.Event Terminated When Temp Decreased | |