ML19350B260

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Forwards IE Info Notice 81-04, Cracking in Main Steam Lines. No Response Required
ML19350B260
Person / Time
Site: Oyster Creek
Issue date: 02/27/1981
From: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Finfrock I
JERSEY CENTRAL POWER & LIGHT CO.
References
NUDOCS 8103200185
Download: ML19350B260 (1)


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UNITED STATES

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631 PARK AVENUE

,o' KING OF PRUSSIA, PENNSYLVANIA 19406 Docket No. 50-219 FEB 2 71991 Jersey Central Power and Light Company ATTN: Mr. Ivan R. Finfrock, Jr.

Vice President P. O. Box 388 Forked River, New Jersey 08731 Gentlemen:

The enclosed IE Information Notice No. 81-04, " Cracking in Main Steam Lines" is forwarded to you information.

No written response is required.

If you desire additional information regarding this matter, please contact this office.

Sincerely, frm/e-)?f s

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e H. Grier J1 rector

Enclosures:

1.

IE Information Notice No. 81-04, with 2 attachments CCNTACT:

L. E. Tripp-(215-337-5232)

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J. T. Carroll, Director, Oyster Creek-Operations l

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SSINS No.: 6835 Accession No.:

8011040265 IN 81-04 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D.C. 20555 February 27,1981 IE Information Notice No. 81-04:

CRACKING IN MAIN STEAM LINES Description of Circumstances:

The Virginia Electric Power Company promptly notified the NRC on February 23, 1981 that a radiography examination, during the ongoing steam generator replacement outage at Surry Unit 1, had revealed a lengthy crack indication in the I.D. counterbore area of a weldment on the in-line "T" fitting whi'ch connects the vertical run of 30-inch piping to the safety relief valve header and 30-inch main steam line of Steam Generator "A".

This piping connection is located outside the containment penetration immediately upstream of the main steam isolation valve as shown in the attached sketch.

A visual and dye penetrant examination on the pipe I.D. surface of the weldment nearest the containment penetration established that the cracking extended about 120 F around the fitting counterbore between the 4 o' clock to 8 o'cleck 0

position. Cracking was also observed in the weld counterbore at the opposite end of the T-fitting during visual examination of the piping interior.

Radio-graphic examination of "B" and "C" main steam line T-fitting welds cisclosed i

crack indications at similar locations.

l Metallurgical specimens of the cracking were trepanned from the T-fitting I

of the "A" main steam line for analysis.

Controlled excavation and depth measurements of the crack at its mid-length indicated a crack depth of about 0.090" in tnis location. The cause of cracking has not yet been established.

VEPCO.has planned an ultrasonic examination.of similar weldments in Surry Unit 2 main steam lines utilizing " Hot Piping" ultrasonic techniques.

Preparations are also being made to ultrasonic examine similar weldments at North Anna Unit 1, currently in cold shutdown for refueling.

Recommendation to Licensees:

This information is provided as an early notification of a significant safety matter that is still under review by the NRC staff.

It is expected that recipients will review the information for possible applicability to their plants.

For those plants having

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are currently in a refueling or - /

that a ultrasonic and/or radiogr DUPLICATE DOCUMENT counterbore areas of the T-fitti operations, unless some current Entire document previously is available, entered into systera under:

^m _10I104021,5 No. of pages:

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