05000348/LER-1980-071-03, /03L-0:on 801027 & 28,containment Atmosphere Particuulate & Gaseous Radioactivity Monitoring Sys (R11 & R12) Declared Inoperable Due to Low Flow Pump Trips.Caused by Failing Bearings & Partially Opened Isolation Valve

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/03L-0:on 801027 & 28,containment Atmosphere Particuulate & Gaseous Radioactivity Monitoring Sys (R11 & R12) Declared Inoperable Due to Low Flow Pump Trips.Caused by Failing Bearings & Partially Opened Isolation Valve
ML19345B833
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 11/26/1980
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19345B806 List:
References
LER-80-071-03L, LER-80-71-3L, NUDOCS 8012020595
Download: ML19345B833 (2)


LER-1980-071, /03L-0:on 801027 & 28,containment Atmosphere Particuulate & Gaseous Radioactivity Monitoring Sys (R11 & R12) Declared Inoperable Due to Low Flow Pump Trips.Caused by Failing Bearings & Partially Opened Isolation Valve
Event date:
Report date:
3481980071R03 - NRC Website

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Io i3i l' zaseous radioactivity monitoring systems (R11 and' R12, respectively) were declared f*5TT] I inoperable due to low flow pump trips.. Tech. Soec.' 3.4.6.1, in part, re

'res R11 Jais! l and R12 to be operable. Tech. Spec. 3.4.6.1 action statement requirements were met.

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Lo 18.1 I the health and safety.of the pablic ' ere not affected.

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3J 34 35 36 37 40 44 42 43 CAUSE DESCAl??!CN ANDCCaaECTIVE ACTIONS h 124oII The low flow trip in the first occurrence was due to failing bearings on the inboard i 6il l pump which caused oscillations in pump performance. The inboard pump was tagged out I for maintenance, the outboard pump was valved in and approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> later gl the second incident occurred.

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l LER 80-071/03L-0 Cause Description and Corrective Actions (Cont'd) subsequent pump trip. The valve was fully opened and the system was returned to service at 2343 on 10/28/80.

Personnel responsible for the error have been instructed as to the necessity of insuring proper position of the isolation veilves. Other personnel with these responsibilities will be instructed on this matter.

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