05000321/LER-1980-101-03, /03L-0:on 800819,Standing Order 80-45, Scram Discharge Vol Residual Water or Vacuum Determination, Was Not Performed.Caused by Personnel Error

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/03L-0:on 800819,Standing Order 80-45, Scram Discharge Vol Residual Water or Vacuum Determination, Was Not Performed.Caused by Personnel Error
ML19344F450
Person / Time
Site: Hatch 
Issue date: 09/09/1980
From: Baxley S
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19344F448 List:
References
LER-80-101-03L-01, LER-80-101-3L-1, NUDOCS 8009150283
Download: ML19344F450 (2)


LER-1980-101, /03L-0:on 800819,Standing Order 80-45, Scram Discharge Vol Residual Water or Vacuum Determination, Was Not Performed.Caused by Personnel Error
Event date:
Report date:
3211980101R03 - NRC Website

text

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8 60 61 DOCKET NUMBER 08 69 EVENT DATE 74 75 HEPORT DATE 80 EVENT DESCRIPTION AND PROD ADLE CONSEQUENCES h 10121 lDuring normal operation plant personnel discovered that Standing ordnr I

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NARRATIVE

REPORT Georgia Fower Company Plant E. I. Hatch Baxley, Gerogia License Event Report No. 50-321-1980-101 During normal plant operation plant personnel discovered that Standing Order 80-45,' " Scram discharge volume residual water or vacuum determination" had not been performed on 8-19-80. The event was discovered at 0055 on 8-20-80 and,the standing order was immediately performed.

The causes of this event are personnel error and inadequate procedures.

The standing order was required once per day and was being routinely performed on the day shift.. The fay shift missed performing the standing order. The evening shift a,s'sumed the day shift performed the standing order. At the time of this event there was no adequate method of ensuring that a standing order was performed. HNP-1-1050 and HNP-2-1050 surveillance check procedures have been revised to include a data sheet to log all active standing orders'at the beginning of each day. These procedures will be in effect by 10-9-80.

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