ML19344F090

From kanterella
Jump to navigation Jump to search
LER 80-019/03L-0:on 800817,while Operating at 400 Mw,After Performance of Reactor Core Isolation Cooling Monthly Pump Operability Surveillance Test,Flow Controller Was Left in Manual.Caused by Operator Failure to Readjust to Automatic
ML19344F090
Person / Time
Site: Quad Cities Constellation icon.png
Issue date: 08/25/1980
From: Kopacz J
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19344F085 List:
References
LER-80-019-03L-04, LER-80-19-3L-4, NUDOCS 8009120399
Download: ML19344F090 (2)


Text

U. O. rwut L2nn niuus.n e un e ww . w.3 NRC FEM 366 -

ir m '

- LICENSEE EVENT REPORT p CONTROt. S LOCK: l l l l l l lh 6

(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) t o li4 l9I I l LICENSEE t 10 ICODE A lD l 1l@l 0 l 0 l 0LIGENSE l - l NUMSER 0 l 0 l 0 l - l 02$l 0 l 0 LICENSE 26 l@l 4l TYPE1l1JO l1 l

SFlcar l@

1 58l@l

? le 15 CON'T loltl ,"gC]

, l L l@l0 l5 lo lo l0 l2 l5 14 68l@l 69o l 8EVENT l 1 OATE l 818 l o l@l0181215 74 75 REPORT OATE l8 1080l@ ,

7 4 60 61 OOCK ET NUMS E R '

EVENT DESCRIPTION AND PROeABLE CONSEQUENCES h

["6TTl l On August 17, 1980, with Unit 1 operating at 400 MWe, the RCIC Monthly Pump l Io Ia l 1 Operability Surveillance was performed. At the conclusion of the test the flow I .;

in t ai l controller was inadvertently lef t in manual at a reduced flow. No other RCIC l l o # 31 l components were affected. Had an RCIC Auto Initiation taken place, the system i j io is i i valves would have lined up properly and partial flow would have been provided. [

l lo l'I i 1

l06-1l 80 E CODE SUSC E COMPONENT CODE SUS DE & E

[0iil 7 i lC lE l@ W@ l A l@ l1 lN lS lT lR lU ]@ W@ lZ l@

9 10 1 12 13 18 19 20 Riyt$lON SEQUENTI AL OCCURRENCE REPORT REPORT NO. CODE TYPE NO. .

LER RO EVENT YE A R

@ ,AEQR l8l0l l-l l0 l1 l9 l l 0l 3 l lL l l-l l0l 24 26 27 28 29 30 31 32 21 22 23 HOURS $8 I 80 1 8. SUPPLt MANUPAC RER T N A O O P NT ME

(,X,,,,j@l X l@ l35Z l@ W@ l Ol0l0l0 l W@

36 37 40 el l42N l@ lZl@ lZ(9l9l9l@

43 44 47 33 J4 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l

1i ll The Unit licensed ooerator failed en nince the fino controller in automatic.

,.,.,i The flow controller was placed in automatic upon detection. The Shift Technical I Advisors are presently accompanying the operators during their panel checks. I

,., ,g This event is being discussed with the operators and procedures were reviewed. I I

1; 6 : I L 80 7 i 9

% POWER OTHER STATUS Das Y DISCOVERY DESCRIPTION

$A S Routine inspection l'I!I b @ l0l6l1l@l 7

a ' "

NA l lB l@l

  • l 6 ,cTiviT - CO0 TENT AMOUNT OF ACTIVITY LOCATION OF RELEASE l 2ELEASED CP RELEASE NA l l l l' le l l Z l @ W@l 9 10 tt 44 45 80 PERSONNEL EXPOSURf 5 NUM8tR TYPE DESCRIPTION

[

l i - j l 0 l 0 l 0 l@l Z l@]

  • PERSONsEtiNau' lits Nuv8ER DESCRIPTION @ l NA l ! . lt l90 l 0 l0 l@l it 12 80 LOSS 08 C88 OAuaGE TO PActLITY

. TveE CESCRiPTION NA l l l - l . l l Z [@l0 80 s 9

'* N AC USE ONLY

,S$[*$iScR,PTiON @

I: t :l lN l NA I l l l I I l I l l I I 8,,j l 64 69 80 r.

g 3 v3 Jeffrey Kopacz ,,.,0NE.

309-654-2241, ext . 178 {

PARER l .A v E op ,O' 0 0 9 2 % ;p p

e

l. LER NUMBER: LER/R0 80-19/03L
11. LICENSEE NAME: Commonwealth Edison Company quad-Cities Nuclear Power Station lil. FACILITY NAME: Unit One IV. DOCKET NUMBER: 050-254 -

V. EVENT DESCRIPTION:

On August 17, 1980, with Unit One operating at 400 MWe, the RCIC Monthly Punip Operab!Ilty Surveillance was performed. At the conclusion of the test the flow controller was inadvertently lef t in MANUAL at a reduced flow.

VI. PROBABLE CONSEQUENCES OF THE OCCURRENCE:

The Reactor Core Isolation Cooling System is designed to supply makeup cooling water to the reactor vessel should the main condenser become isolated from the reactor, with normal feedwater unavailable. The HPCI System was operable at all times the RCIC flow controller was in the MANUAL mode. No other RCIC components were affected by this event.

Had ar RCIC automatic initiation event taken place, the system valves would have lined up properly, and partial flow would have been provided.

Vll. CAUSE:

At the conclusion of the pump operability surveillance the Unit Licensed Operator failed to place the flow controller into AUTO.

Vill. CORR,ECTIVE ACPION:

The immediate action upon detection of the occurrence was to place the flow controller into AUTO. The Shift Technical Advisors are presently accompanying the operators during their panel checks to provide additional assurance of correct Control Room panel line-ups. This event is being discussed with those operators involved. Procedures were reviewed, and i

no additions or changes are deemed necessary.

l l

l l

t I

- _ ,_ . . , _ __ . _ _