05000333/LER-1980-071-03, /03L-0:on 800810,during Plant Startup at Less than 150 Psig,Reactor Core Isolation Cooling Turbine Speed Would Not Control in Manual During Surveillance Test.Sys Flow Also Did Not Control in Automatic.Cause Not Determined

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/03L-0:on 800810,during Plant Startup at Less than 150 Psig,Reactor Core Isolation Cooling Turbine Speed Would Not Control in Manual During Surveillance Test.Sys Flow Also Did Not Control in Automatic.Cause Not Determined
ML19344F068
Person / Time
Site: FitzPatrick 
Issue date: 09/09/1980
From: W. Verne Childs
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19344F063 List:
References
LER-80-071-03L, LER-80-71-3L, NUDOCS 8009120365
Download: ML19344F068 (1)


LER-1980-071, /03L-0:on 800810,during Plant Startup at Less than 150 Psig,Reactor Core Isolation Cooling Turbine Speed Would Not Control in Manual During Surveillance Test.Sys Flow Also Did Not Control in Automatic.Cause Not Determined
Event date:
Report date:
3331980071R03 - NRC Website

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8 60 61 CoCKET NUMS ER 68 69 EVENT OATE 74 75 REPORT C ATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l o 121 l During plant startup at less than 150 psig, the RCIC turbine speed would not control l Io la1 I in manual during surveillance required by TS 3.5.E.

About nine (9) hours later, l

l0t4l l fellowing resolt31on of the speed control problem, testing was resumed and system i

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