05000333/LER-1980-095-03, /03L-0:on 801217,reactor Core Isolation Cooling Sys High Steam Flow Switch 13-DPIS-84 Found Set Outside Tech Specs.Caused by Instrument Drift.Switch Recalibr

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/03L-0:on 801217,reactor Core Isolation Cooling Sys High Steam Flow Switch 13-DPIS-84 Found Set Outside Tech Specs.Caused by Instrument Drift.Switch Recalibr
ML19341A046
Person / Time
Site: FitzPatrick 
Issue date: 01/15/1981
From:
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19341A042 List:
References
LER-80-095-03L, LER-80-95-3L, NUDOCS 8101210506
Download: ML19341A046 (1)


LER-1980-095, /03L-0:on 801217,reactor Core Isolation Cooling Sys High Steam Flow Switch 13-DPIS-84 Found Set Outside Tech Specs.Caused by Instrument Drift.Switch Recalibr
Event date:
Report date:
3331980095R03 - NRC Website

text

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60 68 CoCKET NUMB ER 68 69 EVENT CATE 74 75 REPCRT CATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h Io Ial l "During normal operation while conducting surveillance reCuired by Ts Table 4.2-2, l

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