LER-1980-027, /01T-0:on 801015,during IE Bulletin 79-14 Reanalysis of safety-related Piping,Ten Pipes Failed to Meet Operability Criteria.Caused by Improper Const.Pipes Will Be Modified to Meet Requirements Prior to Startup |
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| 2541980027R01 - NRC Website |
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6 60 61 DOCK ET NUMBER 64 69 EVENT DATE 74 75 REPOR T DATE 80 EVENT DESCRIPTION AND PROSABLE CCNSEQUENCES O'o 10 l 21 l While performing a re-analysis of sarety related p'iping as required by lE Bulletin l
m j 79-14 the following pipes were found not to meet the operability criteria g
g ; estahlished by Commonwealth Edison Company:
1-4858A & B 4", 1-3747-8", 1-3769-8" 1-0201A & B 22", 1-1033A & B 3", 1-1067-3", and 1-4309-3".
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LER NUMBER: LER/R0 80-27/0lT-0 11.
LICENSEE NAME: Commonwealth Edison Comoany quad-Cities Nuclear Power Station Ill.
FACILITY NAME: Unit One IV.
DOCKET NUMBER: 050-254 V.
EVENT DESCRIPTION
As required by NRC IE Bulletin 79-14, re-analysis of all safety related piping began after extensive piping walkdowns to verify as-built condi-tions.
In June, the work scope changed to focus the analysis on the inaccessible areas of Unit One.
In October, the results disclosed that the scope of wcrk was approximately two times greater tnan initially estimated. When scheduling problems arose further study was done to determine critical supports in order to establish a priority list.
On October 15, it was determined that operability problems existed on the following pipes:
1 1,858A & B-4" - RHRS Service Water Relief Valve lines on the RHR heat exchangers 1-3747-8"
- - Discharge of Reactor Building Closed Cooling Water from the Drywell at the penetration 1-3769-8"
- - Supply of Reactor Building Closed Cooling Water to the Drywell at the-penetration 1-0201A & B-
- - Recirculation System Discharge ring header 22" l-1033A & B-3" - A & B RHR discharge pipe drains 1-1067-3"
- - RHR crosstie fill line from Condensate Storage 1-4309-3"
- - Clean Demineralized water at the Drywell penetration VI.
PROBABLE CONSEQUENCES OF THE OCCURRENCE:
i Each line will be addressed separately as to probable consequences upon failure. Those systems addressed in the FSAR will not be further analyzed in this report.
Line (1-4858A & B-4"):
Failure of this line would result in a partial loss of service cooling water to the RHR heat exchanger. The RHR primary coolant boundary would have remained unaffected. Redundant RHR service water pumps in each loop would mitigate the partial loss of flow.
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Lines (1-3747-8", 1-3769-8", 1-4309-3"): The RBCCW system 'in the dry-I well is a closed internal loop. Loss of. RBCCW in the drywell would cause loss of the recirculation pumps. However, these pumps trip during a postulated LOCA, and such tripping is analyzed in the FSAR.
i Recirc pump trips under other circur. stances are Ilkewise analyzed.
The RBCCW lines can be isolated external and internal to the drywell.
i Loss of clean demin water to the drywell poses no safety concern.
The line is valved out during normal plant operation both inside and outside the drywell.
Line (1-0201 A & B-22"): This line has been evaluated in the FSAR as to probable consequences upon failure.
In' addition, the calculated OBE stresses, although above the operability limit, were only 60 per-cent of material ultimate strength and failure during an OBE would not be expected.
Line (1-1033A & B-3"):
A failure of either of these lines would result in the partial loss of RHR cooling flow from the A and B RHRS pumps.
The C and D RHRS pumps discharge flow is not affected.
Based on the large volume of flow produced by the LPCI Mode of RHRS and the 33 percent excess system capacity, loss of these lines would not render.
LPCI completely incapable of performing its function.
Line (1-1067-3"): A failure of this line would reduce the capacity of the LPCI Mode of RHR. The relatively small size of this line as compared to the large LPCI flow volume and the 33 percent excess system capacity would not result in serious LPCI flow deterioration.
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Vil. CAUSE:
The preliminary design of the systems involved was sufficient to meet the. analysis as provided in the FSAR. Orioinal construction was not to the requirements as given by Bulletin 79-14.
Vill. CORRECTIVE ACTION:
Prior to the Unit startup, all lines listed will be supported 4.
sufficiently to meet the operability requirements of. !E Bulletin 79-14.
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| 05000265/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000254/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000254/LER-1980-001-03, /03L-0:on 800111,while Performing Suppression Chamber to Drywell Pressure Separation Test,Differential Pressure Transmitter 1-8741-51 Was Not Indicating Properly. Caused by Personnel Error Due to Drawing Error | /03L-0:on 800111,while Performing Suppression Chamber to Drywell Pressure Separation Test,Differential Pressure Transmitter 1-8741-51 Was Not Indicating Properly. Caused by Personnel Error Due to Drawing Error | | | 05000254/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000254/LER-1980-002-03, /03L-0:on 800111,while Performing in-place Charcoal Absorber Leak Rate Test on Standby Gas Treatment sys,1.93% Leakage Found.Caused by Damaged Gasket on 4x4 Inch Access Plate.Gasket Replaced | /03L-0:on 800111,while Performing in-place Charcoal Absorber Leak Rate Test on Standby Gas Treatment sys,1.93% Leakage Found.Caused by Damaged Gasket on 4x4 Inch Access Plate.Gasket Replaced | | | 05000265/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000265/LER-1980-002-03, /03L-0:on 800108,while Leak Testing RHR Svc Water Vault Penetrations,Observed Leakage from Electrical Penetration P-12.Caused by Loose hold-down bolts.Hold-down Bolts Tightened & Penetration Retested Satisfactorily | /03L-0:on 800108,while Leak Testing RHR Svc Water Vault Penetrations,Observed Leakage from Electrical Penetration P-12.Caused by Loose hold-down bolts.Hold-down Bolts Tightened & Penetration Retested Satisfactorily | | | 05000265/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000265/LER-1980-003-03, /03L-0:on 800213,while Performing Procedure Qis 35-2,reactor Bldg Ventilation Sys Would Not Reset After Test Isolation.Caused by Burnt CR 120 Relay.Relay 1705-105 Replaced & Functional Test Sucessfully Completed | /03L-0:on 800213,while Performing Procedure Qis 35-2,reactor Bldg Ventilation Sys Would Not Reset After Test Isolation.Caused by Burnt CR 120 Relay.Relay 1705-105 Replaced & Functional Test Sucessfully Completed | | | 05000254/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000254/LER-1980-003-03, /03L-0:on 800206,while Performing Procedure Qos 1000-3,RHR to Suppression Chamber Dump Valve,Mo 1-1001- 36A,circuit Breaker Tripped Out.Caused by Burned Out 480/120-volt Transformer in Circuit Breaker Cabinet | /03L-0:on 800206,while Performing Procedure Qos 1000-3,RHR to Suppression Chamber Dump Valve,Mo 1-1001- 36A,circuit Breaker Tripped Out.Caused by Burned Out 480/120-volt Transformer in Circuit Breaker Cabinet | | | 05000254/LER-1980-004-03, /03L-0:on 800215,while Performing Reactor low-low Water Level Calibr Test,Procedure QIS-11,level Switch LIS-1-263-72A Failed.Caused by Slight Misalignment of Mercury Wetted Magnetic Switch W/Actuating Magnet | /03L-0:on 800215,while Performing Reactor low-low Water Level Calibr Test,Procedure QIS-11,level Switch LIS-1-263-72A Failed.Caused by Slight Misalignment of Mercury Wetted Magnetic Switch W/Actuating Magnet | | | 05000254/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000265/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000265/LER-1980-004-03, /03L-0:on 800219,while Performing Procedure Qms 700-1,automatic Blowdown Timer 287-105A Took 122-s to Time Out,Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Timer Adjusted & Verified to Be 100-s | /03L-0:on 800219,while Performing Procedure Qms 700-1,automatic Blowdown Timer 287-105A Took 122-s to Time Out,Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Timer Adjusted & Verified to Be 100-s | | | 05000265/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000265/LER-1980-005-03, /03L-0:on 800303,while Performing LPCI & Containment Cooling Modes of Rhrs Logic test,5-s Delay Timer 10A-M2A for 1002B RHR Pump Failed to Actuate Relay K21A.Relay Failed to Energize.Caused by Microswitch Drift | /03L-0:on 800303,while Performing LPCI & Containment Cooling Modes of Rhrs Logic test,5-s Delay Timer 10A-M2A for 1002B RHR Pump Failed to Actuate Relay K21A.Relay Failed to Energize.Caused by Microswitch Drift | | | 05000254/LER-1980-005-03, /03L-0:on 800224,while Performing Misv Closure Timing,Valve AD 1-203-1B Failed to Close When Control Switch Was Operated.Caused by Blockage of Exhaust Restrictor on on Pilot Valve.Exhaust Restrictor Cleaned | /03L-0:on 800224,while Performing Misv Closure Timing,Valve AD 1-203-1B Failed to Close When Control Switch Was Operated.Caused by Blockage of Exhaust Restrictor on on Pilot Valve.Exhaust Restrictor Cleaned | | | 05000254/LER-1980-006-03, /03L-0:on 800222,while Doing Routine Panel Checks, Reactor Core Isolation Cooling Supply Valves Mo 1-1301-16 & 17 Were Found in Closed Position.Caused by Procedural Inadequacy & Personnel Performance.Procedures Revised | /03L-0:on 800222,while Doing Routine Panel Checks, Reactor Core Isolation Cooling Supply Valves Mo 1-1301-16 & 17 Were Found in Closed Position.Caused by Procedural Inadequacy & Personnel Performance.Procedures Revised | | | 05000254/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000265/LER-1980-006-01, /01T-0:on 800308,while Performing Reactor Vessel Pressure Test,Several Crack Indications Were Discovered in Pipe to Elbow Welds.Cause Not Determined.Affected Pipe Sections Will Be Replaced W/Carbon Steel Piping | /01T-0:on 800308,while Performing Reactor Vessel Pressure Test,Several Crack Indications Were Discovered in Pipe to Elbow Welds.Cause Not Determined.Affected Pipe Sections Will Be Replaced W/Carbon Steel Piping | | | 05000265/LER-1980-006, Forwards LER 80-006/01T-0 | Forwards LER 80-006/01T-0 | | | 05000254/LER-1980-007-03, /03L-0:on 800308,while Performing Control Room Insp & Panel Check,B Main Steam Line Radiation Monitor Found Reading Low.Caused by Logarithmic Radiation Monitor Chassis Electronically Drifting Out of Calibr.Chassis Recalibr | /03L-0:on 800308,while Performing Control Room Insp & Panel Check,B Main Steam Line Radiation Monitor Found Reading Low.Caused by Logarithmic Radiation Monitor Chassis Electronically Drifting Out of Calibr.Chassis Recalibr | | | 05000254/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000265/LER-1980-007-03, /03L-0:on 800316,while Ultrasonically Inspecting Jet Pump Fixture Beam Assemblies One Through 20,width-wise Crack Indication Discovered Along Upper Surface of Pump 16 Near Bolt.Caused by Intergranular Stress Corrosion | /03L-0:on 800316,while Ultrasonically Inspecting Jet Pump Fixture Beam Assemblies One Through 20,width-wise Crack Indication Discovered Along Upper Surface of Pump 16 Near Bolt.Caused by Intergranular Stress Corrosion | | | 05000265/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000254/LER-1980-008-03, /03L-0:on 800308,after Performing Preventive maint,1/2 Diesel Generator Would Not Start from Control Room.Caused by Poor Electrical Contact Between Fuse & Clip. Fuse Clip Adjusted | /03L-0:on 800308,after Performing Preventive maint,1/2 Diesel Generator Would Not Start from Control Room.Caused by Poor Electrical Contact Between Fuse & Clip. Fuse Clip Adjusted | | | 05000265/LER-1980-008-03, /03L-0:on 800305,while Performing LPCI & Containment Cooling Modes,Two 5-S Delay Timers for Starting 1002D RHR Pump Failed to Actuate Timer Contacts.Caused by Microswitch Arm Being Out of Alignment | /03L-0:on 800305,while Performing LPCI & Containment Cooling Modes,Two 5-S Delay Timers for Starting 1002D RHR Pump Failed to Actuate Timer Contacts.Caused by Microswitch Arm Being Out of Alignment | | | 05000265/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000254/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000265/LER-1980-009-03, /03L-0:on 800322,while Performing Pci Simulated Automatic Closure Initiation Test,Procedure Qos 1600-13, Transient in-core Probe 2,failed to Respond to Group 2 Isolation Signal.Caused by Dirty Contacts on Relay K21 | /03L-0:on 800322,while Performing Pci Simulated Automatic Closure Initiation Test,Procedure Qos 1600-13, Transient in-core Probe 2,failed to Respond to Group 2 Isolation Signal.Caused by Dirty Contacts on Relay K21 | | | 05000265/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000254/LER-1980-009-03, /03L-0:on 800410,while Performing Motor Operated Valve Operability Test,Thermal Overload Relay for B-loop Suppression Chamber Cooling Valve Tripped.Caused by High Motor Starting Currents.Torque Switch Adjusted | /03L-0:on 800410,while Performing Motor Operated Valve Operability Test,Thermal Overload Relay for B-loop Suppression Chamber Cooling Valve Tripped.Caused by High Motor Starting Currents.Torque Switch Adjusted | | | 05000254/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000254/LER-1980-010-03, /03L-0:on 800423,while Performing Loss of Electrohydraulic Control Fluid Pressure Scram Surveillance, Pressure Switch 1-5600-PS-3 Tripped Below Tech Spec Limit. Caused by Instrument Setpoint Drift.Switch Adjusted | /03L-0:on 800423,while Performing Loss of Electrohydraulic Control Fluid Pressure Scram Surveillance, Pressure Switch 1-5600-PS-3 Tripped Below Tech Spec Limit. Caused by Instrument Setpoint Drift.Switch Adjusted | | | 05000254/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000265/LER-1980-010-03, /03L-0:on 800517,while Performing Quartlerly MSIV Closure Timing Surveillance Procedure Qos 250-4,MSIV AO 2-203-1C Closed in 2.5-s & MSIV AO 2-203-2D Closed in 9.1-s. Caused by Equipment Failure.Speed Control Valves Adjusted | /03L-0:on 800517,while Performing Quartlerly MSIV Closure Timing Surveillance Procedure Qos 250-4,MSIV AO 2-203-1C Closed in 2.5-s & MSIV AO 2-203-2D Closed in 9.1-s. Caused by Equipment Failure.Speed Control Valves Adjusted | | | 05000265/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000265/LER-1980-011-03, /03L-0:on 800420,while Performing Manual Operation of Relief Valves,Valve 2-203-3C Failed to Open.Caused by Component Failure Due to Excessive Solenoid Plunger to Pilot Valve Stem Clearance | /03L-0:on 800420,while Performing Manual Operation of Relief Valves,Valve 2-203-3C Failed to Open.Caused by Component Failure Due to Excessive Solenoid Plunger to Pilot Valve Stem Clearance | | | 05000265/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000254/LER-1980-011-03, /03L-0:on 800429,main Feed Breaker to MCC 19-1 Tripped.Caused by Excessive Current Trip Time Which Allowed phase-to-phase Short Internal to Be Carried Back to MCC 19-1.Motor & Circuit Breaker Replaced | /03L-0:on 800429,main Feed Breaker to MCC 19-1 Tripped.Caused by Excessive Current Trip Time Which Allowed phase-to-phase Short Internal to Be Carried Back to MCC 19-1.Motor & Circuit Breaker Replaced | | | 05000254/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000254/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000265/LER-1980-012-03, /03L-0:on 800428,reactor Water Conductivity Exceeded 10 Umhos/Cm Tech Spec Limit.Caused by Depleted Demineralizers.Unit Shutdown Initiated.Demineralizers Regenerated & Low Conductivity Coolant Added to Reactor | /03L-0:on 800428,reactor Water Conductivity Exceeded 10 Umhos/Cm Tech Spec Limit.Caused by Depleted Demineralizers.Unit Shutdown Initiated.Demineralizers Regenerated & Low Conductivity Coolant Added to Reactor | | | 05000254/LER-1980-012-03, /03L-0:on 800429,reactor Recirculation Motor Generator Set 1A Tripped Due to Low Oil Pressure from Lube Oil Pump 1A1 Trip.Possibly Caused by Contractor Personnel Dropping Matl on Generator Set Control Cabinet | /03L-0:on 800429,reactor Recirculation Motor Generator Set 1A Tripped Due to Low Oil Pressure from Lube Oil Pump 1A1 Trip.Possibly Caused by Contractor Personnel Dropping Matl on Generator Set Control Cabinet | | | 05000265/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000254/LER-1980-013-03, /03L-0:on 800415,while Performing High,Low & low-low Reactor Water Level Functional Test,Procedure Qis 10-1,reactor Water Level Switch LIS-1-263-57A Was Found to Trip Below Tech Spec Limit.Caused by Instrument Drift | /03L-0:on 800415,while Performing High,Low & low-low Reactor Water Level Functional Test,Procedure Qis 10-1,reactor Water Level Switch LIS-1-263-57A Was Found to Trip Below Tech Spec Limit.Caused by Instrument Drift | | | 05000265/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000254/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000265/LER-1980-013-03, /03L-0:on 800428,while Performing LPCI Motor Operated Valve Operability Test & RHR to Suppression Chamber Test,Cooling Valve Mo 2-1001-36A Failed to Close.Caused by Binding of Plunger Arm on Auxiliary Interlock Contacts | /03L-0:on 800428,while Performing LPCI Motor Operated Valve Operability Test & RHR to Suppression Chamber Test,Cooling Valve Mo 2-1001-36A Failed to Close.Caused by Binding of Plunger Arm on Auxiliary Interlock Contacts | |
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