ML19338G147

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LER 80-057/03L-0:on 800922,during Startup,Rhr Sys Was Removed from Svc & Isolated from RCS at 250 F.Caused by Operator Error.Tech Specs Changed to Clarify Svc Procedure
ML19338G147
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 10/22/1980
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19338G118 List:
References
LER-80-057-03L, LER-80-57-3L, NUDOCS 8010280502
Download: ML19338G147 (1)


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7 64 60 occa gT P.uust R Gd G'J EVE 4T oATE 34 75 EVENT DESCRIPTION AND PROS A8LE CCNSECUENCES h ,

f5Ti-l l At 0250 on 9-22-80, while performing FNP-1-UOP-1.1 (Startup of Unit from Cold Shutdown . I

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(5 73-l [ to Hot Standby), the Residual Heat Removal (RHR) system was removed from service and  ;

.- g l isolated from the RCS due to operator misinterpretation of the UOP. RCS temperaturg was; pg-l-j ;250 F. Tech. Spec. 3.4.9.3 requires, in part, that two RHR relief valves be.opdrable 9

,a g ; g when the temperature of one or more of the RCS cold legs is f,310 F. Tech. Spec. 3.4.9.3 g g [ action statement requirements were met. Health / safety of the public were not affected. y lo ta l l I 2 as 80 systru cAust CAUsE CooE CoMr. watvg Coot SUSCoot COMPONENT Coot SURCooE foTO l C I 10F l@ [oj@ l z12 l@ Iz lz lz Iz Iz Iz l@ SUSCooEIz i@ g@

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36 l010l0l 31 40 l l Nlg l N lg el l z l9 l9 l9 l 42 42 44 47 CAUSE DESCRIPTION AND CCMECTIVE ACTICNS E IThe FNP-1-UOP-1.1 Precautions and Limitation's stated that RHR must be removed from  ;.

y [ service pr'ior to pressurizer temperature reaching 47f F but did not caution against g l removing RHR if the RCS temperature is <310 F. A chanste to _

l l FNP-1-UOP-1.1 was generated to preclude ftiture occurren'ces. RHR was. returned to an g

g, ,4 ; ; operable status at 0255 on 9-22-80. .

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NAME CF PnCPARER W. G. airston, III -

.(205) 899-5156 [