05000348/LER-1980-053-03, /03L-0:on 800909,during Surveillance Testing, Containment Spray Automatic Actuation Logic Declared Inoperable.Caused by Integrated Circuit Failure.Circuit Card Replaced & Logic Returned to Svc

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/03L-0:on 800909,during Surveillance Testing, Containment Spray Automatic Actuation Logic Declared Inoperable.Caused by Integrated Circuit Failure.Circuit Card Replaced & Logic Returned to Svc
ML19338F196
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 09/29/1980
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19338F190 List:
References
LER-80-053-03L, LER-80-53-3L, NUDOCS 8010070621
Download: ML19338F196 (1)


LER-1980-053, /03L-0:on 800909,during Surveillance Testing, Containment Spray Automatic Actuation Logic Declared Inoperable.Caused by Integrated Circuit Failure.Circuit Card Replaced & Logic Returned to Svc
Event date:
Report date:
3481980053R03 - NRC Website

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l Operability Test). T/S 3.3.2.1 requires, in part, that the Containment Spray Atitomatic ;

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