ML19331D817

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LER 80-033/03L-0:on 800803,following Routine Sampling of Core Flood Tank A,Sample Isolation Valve CFV-11 Failed to Close.Caused by Failed Contact Rotor in Limitorque Operator. Contact Rotor 2 Replaced & Declared Operable
ML19331D817
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 08/28/1980
From: Neuschaefer E
FLORIDA POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19331D808 List:
References
LER-80-033-03L, LER-80-33-3L, NUDOCS 8009030609
Download: ML19331D817 (2)


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SUPPLEMENTARY INFORMATION Report No.: 50-302/80-033/03L-0 Facility: Crystal River Unit #3 -

Report Date: 28 August 1980 Occurrence Date: 3 August 1980 Identification of Occurrence: Containment isolation valve CFV-ll failed to close contrary to Technical Specification 3.6.3.1, Table 3.6-1.

Conditions Prior to Occurrence: Mode 4, Hot Shutdown Description of Occurrence: At 1119 following routine sampling of "A" Core Flood Tank, it was discovered that "A" CFI sample isolation valve, CFV-11, would not close upon remote actuation.

Core Flood Valve, CFV-ll was then manually closed along with Core Flood Valve, CFV-71 to isolate the penetration and maintain containment integrity.

Designation of Apparent Cause: The cause of this event is attributed to a failed contact rotor in the limitorque operator of core flood valve, CFV-ll.

Analysis of Occurrence: No effect upon the plant or general public as a result of this event.

Corrective Action: Contact rotor #2 was replaced and the valve declared operable at 0940 on August 5, 1980 after successful completion of SP-370. An inspection of Core Flood Valve, CFV-ll, limitorque operator has been scheduled for the next planned outage to check for contact rotor wear.

Failure Data: This is the second occurrence of this type reported for CFV-ll, (reference LER #77-114) and the 26th event reported under specification 3.6.3.1.

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