05000333/LER-1980-065-03, /03T-0:on 800814,during Normal Operations,While Inerting Primary Containment,Standby Gas Treatment Sys A&B Found Inoperable.Caused by Blocked Drain Line Allowing Water to Accumulate in Line Until Fans Could Not Discharge

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/03T-0:on 800814,during Normal Operations,While Inerting Primary Containment,Standby Gas Treatment Sys A&B Found Inoperable.Caused by Blocked Drain Line Allowing Water to Accumulate in Line Until Fans Could Not Discharge
ML19331D640
Person / Time
Site: FitzPatrick Constellation icon.png
Issue date: 08/27/1980
From: W. Verne Childs
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19331D634 List:
References
LER-80-065-03T, LER-80-65-3T, NUDOCS 8009030414
Download: ML19331D640 (2)


LER-1980-065, /03T-0:on 800814,during Normal Operations,While Inerting Primary Containment,Standby Gas Treatment Sys A&B Found Inoperable.Caused by Blocked Drain Line Allowing Water to Accumulate in Line Until Fans Could Not Discharge
Event date:
Report date:
3331980065R03 - NRC Website

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60 61 COCK ET NUMBER 68 69 EVENT CATE 74 75 RE80RT O ATE 80 EVENT DESCRIPTION AND PROBABLE CONSECUENCES h IoI:l lDuring normal operations and while inerting primary containment, Standby Gas Treatment

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