05000321/LER-1980-085-03, /03L-0:on 800720,w/unit at 300 Mwt & O Mwe,Reactor Water Not Sampled & Analyzed for Chlorides & Ph.Caused by Personnel Oversight.Retraining Session for Responsible Employees Conducted

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/03L-0:on 800720,w/unit at 300 Mwt & O Mwe,Reactor Water Not Sampled & Analyzed for Chlorides & Ph.Caused by Personnel Oversight.Retraining Session for Responsible Employees Conducted
ML19331B596
Person / Time
Site: Hatch 
Issue date: 08/07/1980
From: Rogers W
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19331B583 List:
References
LER-80-085-03L-01, LER-80-85-3L-1, NUDOCS 8008120479
Download: ML19331B596 (2)


LER-1980-085, /03L-0:on 800720,w/unit at 300 Mwt & O Mwe,Reactor Water Not Sampled & Analyzed for Chlorides & Ph.Caused by Personnel Oversight.Retraining Session for Responsible Employees Conducted
Event date:
Report date:
3211980085R03 - NRC Website

text

U.S. NUCLEAR REGULATCRY COMMISSION NRC FORM 364

. (7 77)

,t LICENSEE EVENT REPORT O.

CONTROL BLOCK: l l

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l l lh (PLEASE PRINT CR TYPE ALL REQUIRED INFORMATION) 1 6

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LICENSEE CODE 14 LICENSE NUMBER 25 26 LICENSE TYPE Jo 57 CAT 58 7

8 CON'T l L l@l 015 l 0 l 0 l0 l 3 l 2 l1 l@l0 l7 l2 l018 l0 l@l0 l8 l0 l71810 l@

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8 60 68 DOCKET t. UMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h

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IT]T1 1On 7-20-80, with the unit at 300 MWT and 0 MWE reactor water was not i

l sampled and analyzed for chlorides and pH at 1530 and 2330 hours0.027 days <br />0.647 hours <br />0.00385 weeks <br />8.86565e-4 months <br /> as i

O 3 frequired by Tech Spec Sections 4.6.F.2.c.2 and 4.6.F.2.c.3.

This is l

O 4 la non-repetitive occurrence.

There were no effects on public health '

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l Tis ] land safety due to this event.

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I ITITI I 80 DE CODE S BC E COMPONENT CODE SUS dE SU E

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3J 34 3h 36 31 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 27 7

8 iThe cause of these events can be attributed to an oversight by the l

l personnel responsible for taking samples.

A re-training session for l

i i lall personnel who collect and analyse reactor water has been conducted l

1 2 l stressing the Tech Spec requirements for reactor water sampling.

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8 9 10 11 44 45 PERSONNEL FxPOSURES NUYHER TYPE

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NAurmamumn W. H. Ibgers Health Physics PHONE:

c LERG:.'50-321/1980-085:

Licensce: Georgia Ptraer Company Facility Nane:

llidin I Ilatch Ibcket #:

50-321 NMIRATIVE REPORP

. futIRt 50-321/1980-085 On 7-20-80, with the unit at 300 M1r and 0 MP, the reactor water conductivity exceeded 2.0 umho/cm due to a condenser tube leak and only oin reactor water c1can up punp in service. ' Tech Spec Sections 4.6.F.2.c.2 and.4.6.F.2.c.3 require a pII and chloride r.rasurcrent to be taken every cight hours.should the reactor water conductivity exceed-2.0 unho/cm. '1ko consecutive eight nour samples were missed after this occurrence. Subsequent sample analyses indicate, hoaever, that pil and chloride values were well within Tcdi S n:

1 i

requirennnts for reactor water. fnis is a non-repetitive occurrence. 'Ihere

.were In effects on the public health and safety due to this event.-

The cause of these events can be $ttributed to an oversight by the personnel responsible for taking sanples. A re-training session for all personnel who

- collect and analyze reactor water has been conducted, stressing the Tech Spec requirements for reactor water samples on both Units 1 and 2.

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