05000321/LER-1980-086-01, /01T-0:on 800724,w/Unit 1 in Cold Shutdown,Support P52-F512-H704 Determined Missing on Instrument Air Sys. Caused by Inadequate Small Bore Piping Design.New Hanger Design Supplied & Support Installed

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/01T-0:on 800724,w/Unit 1 in Cold Shutdown,Support P52-F512-H704 Determined Missing on Instrument Air Sys. Caused by Inadequate Small Bore Piping Design.New Hanger Design Supplied & Support Installed
ML19330C387
Person / Time
Site: Hatch 
Issue date: 08/04/1980
From: Coggin C
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19330C383 List:
References
LER-80-086-01T, LER-80-86-1T, NUDOCS 8008080310
Download: ML19330C387 (2)


LER-1980-086, /01T-0:on 800724,w/Unit 1 in Cold Shutdown,Support P52-F512-H704 Determined Missing on Instrument Air Sys. Caused by Inadequate Small Bore Piping Design.New Hanger Design Supplied & Support Installed
Event date:
Report date:
3211980086R01 - NRC Website

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EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h coolers, a review of I lWith Unit 1 in cold shutdown for repair of drywell 0 2 g taj Idata. for IEB 79-14 by the AE revealed that a support (P52-F512-H704) wasl integrity could!

Imissing on the instrument air system and that the piping O 4 IOlsi Inot be assured in a seismic DBE.

Piping failure would have rendered 8 l

10181 Ivalves for post-LOCA hydrogen ventina of the containment inoperative.

1 This is a repetitivel IThere were no effects on public health and safety.

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Facility Name:

Edwin-I. Hatch Docket #:

50-321

Narrative

Report for LER 50-321/1980-086 On 7-24-80, the site was notified by the AE (Bechtel) that a

- support was-missing on the instrument air system.

This missing support (P52-F52-F512-H704) was discovered during a review of field data for IEB 79-14.

At the time of discovery Unit I was in. cold shutdown for repair of drywell cooling fans.

Computer analysis indicated - that while the piping and support arrangement was safe for normal plant operating conditions, the ' code allowable stresses would be exceeded for an OBE - seismic event, field stresses would be exceeded for a DBE seismic _ event, and piping integrity could not be assured in this case.

Failure of the piping would

cause

loss of operability of. valves T48-F332A&B, F333A&B, F334A&B, and F335A&B used for post-LOCA hydrogen venting of containment.

These valves could be operated manually if required.

Prior to startup the missing support was per an AE supplied design.

There were no effects upon public health and safety.

This is a repetitive event; see LER 50-321/1979-065.

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