Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046C0661993-07-30030 July 1993 LER 92-009-01:on 920910,deficiencies Discovered During Dynamic Testing of Motor Operated Valves in Response to Generic Ltr 89-10.MOVs W/Deficiencies Modified or Repaired. W/930730 Ltr ML20046B6011993-07-26026 July 1993 LER 93-004-00:on 930428,plant Entered Mode 2 W/Afw Pump Turbine Main Steam Line Crossover Check Valve MS735 in Open Position.Caused by Inappropriate Use of Engineering Judgement.Valve MS735 closed.W/930726 Ltr ML20045D2451993-06-17017 June 1993 LER 93-003-00:on 930520,plant Experienced Trip from Approx & Continuity Between Fuse & Fuseholder Lost,Resulting in Loss of Selected RCS Average Temp Input to Ics.Faulty Fuse Cap & Fuse replaced.W/930617 Ltr ML20044B1681990-07-10010 July 1990 LER 90-002-01:on 900126,reactor Coolant Pump Current Monitor Inputs to Sfrcs ACH1 & Reactor Pressure Sys Channel 1 Experienced Reactor Trip.Probably Caused by Inadequate Test Switches & Isolation plug.W/900710 Ltr ML20043H3201990-06-18018 June 1990 LER 90-010-00:on 900518,station Experienced Inadvertent Safety Features Actuation Signal Level 1-4 Actuation W/Injection of 1,000 Gallons of Borated Water.Caused by Loss of 120-volt Ac Bus Y3.W/900618 Ltr ML20043B5711990-05-25025 May 1990 LER 90-008-00:on 900425,safety Features Actuation Sys Level 1 Actuation Occurred,Resulting in Trip of Containment Radiation Monitors.Caused by High Radiation Fields While Lifting Core Support Assembly.Mod initiated.W/900525 Ltr ML20043B8051990-05-25025 May 1990 LER 90-009-00:on 900426,source-check of Station Vent Radiation Monitors Not Performed Per Tech Spec 3.3.3.10. Caused by Use of Outmoded Light Emitting Dioide as Check Source.Source Check Procedures revised.W/900525 Ltr ML20042F2811990-05-0303 May 1990 LER 90-007-00:on 900403,inadvertent,inconsequential Safety Features Actuation Signal Occured While Defueled.Caused by Incidental Contact W/Monitor in Containment.Temporary Barriers Built Around monitors.W/900503 Ltr ML20042F2791990-05-0303 May 1990 LER 90-006-00:on 900403,station Experienced Safety Features Actuation Sys Levels 1 Through 5 Actuation.Caused by Contact W/Breaker Switch HAAE2 in High Voltage Switchgear Room 2. Meetings Held W/Craft personnel.W/900503 Ltr ML20042E4891990-04-16016 April 1990 LER 90-005-00:on 900314,determined That Some Class 1E Circuits That Pass Through Containment Electrical Penetrations Do Not Have Adequate Backup Fault Protection. Caused by Inadequate Design control.W/900416 Ltr ML20012D0341990-03-19019 March 1990 LER 90-004-00:on 900217,fuel Assembly Moved in Spent Fuel Pool While Emergency Ventilation Inoperable.Caused by Personnel Error.Personnel Involved Counseled & Subj LER Part of Required reading.W/900319 Ltr ML20012C7151990-03-14014 March 1990 LER 90-003-00:on 900212,station Entered Mode 6,refueling,w/o Operable Audible Source Range Indication.Caused by Personnel Error.Individual counseled.W/900314 Ltr ML20012B4851990-03-0606 March 1990 LER 83-039/03X-2:on 830726,discovered That Handwheel for Inner Door of Personnel Airlock in Shut Position & Partially Opened.Caused by Excessive Use of Door During Outages.Door Repaired & Returned to Operable status.W/900306 Ltr ML20011F3831990-02-26026 February 1990 LER 90-002-00:on 900126,reactor Tripped from 73% Power. Caused by Spurious Reactor Coolant Pump Monitor Signal Indicating Only One Pump Running in Each Loop.Pump Seal to Be Replaced During Sixth Refueling outage.W/900226 Ltr ML20006E6861990-02-20020 February 1990 LER 90-001-00:on 900118,reactor Protection Sys Channel 2 Bypassed Temporarily During Performance of DB-MI-03207. Caused by Inadequate Procedure Re Inoperable Channel Removal.Procedure SP1105.02 revised.W/900220 Ltr ML20011E2251990-01-30030 January 1990 LER 86-032-01:on 860802,inadvertent Start of High Pressure Injection Pump 1-2 Occurred.Caused by Open Relay Coil. Failed Relay Replaced & Procedure Change Initiated. W/900130 Ltr ML20005G1091990-01-0909 January 1990 LER 89-015-01:on 891026,concluded That Transmitter Was Out of Tolerance When Reactor Protection Sys Channel 2 Returned to Operable Status on 890924.Caused by leak-by in Instrument Manifold.Transmitter Recalibr successfully.W/900109 Ltr ML20042D4011990-01-0202 January 1990 LER 89-010-01:on 890612,control Room Ventilation Sys Declared Inoperable Due to Compressor High Pressure Trips. Caused by Tripping of Refrigerant Pressure Switch on High Pressure.Switch Reset & Sys retested.W/900102 Ltr ML19354D7361989-12-22022 December 1989 LER 89-018-00:on 891123,hydrogen Dilution Blower 1-1 Casing Drain Line Broke Off at Casing,Declaring Blower Inoperable. Caused by Drain Line Being Accidentally Stepped On.Drain Removed & Pipe Plug installed.W/891222 Ltr ML19332F8951989-12-13013 December 1989 LER 89-017-00:on 891113,containment Spray Pump 1-1 Inadvertently Started During Monthly Functional Test in Safety Features Actuation Sys (Sfas) Channel 1.Caused by Failed Relay in Sfas Channel 3.Relay replaced.W/891213 Ltr ML19332E7521989-12-0404 December 1989 LER 89-016-00:on 890917,unplanned Release of Radioactive Resin to Onsite Settling Basin Occurred.Caused by Personnel Error.Standing Order 89-051 Generated on 890920 to Direct Use of Working Copy of procedures.W/891204 Ltr ML19332D3111989-11-27027 November 1989 LER 89-015-00:on 890924,RCS Flow Transmitter Out of Tolerance When Reactor Protection Sys Channel 2 Returned to Operable Status.Caused by leak-by in Instrument Manifold Seen as Zero Shift.Transmitter recalibr.W/891127 Ltr ML19324C2081989-11-10010 November 1989 LER 89-014-00:on 891011,plastic Sheeting Blocked Off Fire Detectors in Auxiliary Feedwater Pump 1-1 Room & High Voltage Switchgear Room B,Making Fire Detectors Inoperable. Caused by Personnel Oversight.Event reviewed.W/891110 Ltr ML19325D4671989-10-16016 October 1989 LER 89-004-01:on 890411,determined That Circulating Water Line Break Would Result in Loss of Svc Water as Result of Concerns Raised on 890206.Cause Unknown.Standing Order 89-026 in Place to Plug Floor drains.W/891016 Ltr ML19325C8531989-10-13013 October 1989 LER 89-013-00:on 890913,hourly Fire Watch Patrol Exceeded Allowed Interval,Violating Tech Spec 3.7.10,Action a.2. Caused by Personnel Error.Individual Counseled & Event Info Distributed to Fire Watch personnel.W/891013 Ltr ML20024E2591983-08-0101 August 1983 LER 83-033/03L-0:on 830620,fire Detection Zone Reactor Coolant Pump 1-2,containment Level 603 Ft Alarmed & Could Not Be Reset.Caused by Faulty Detector String.Zone Will Be Restored During Next Refueling outage.W/830801 Ltr ML20024B8351983-07-0101 July 1983 LER 83-028/03L-0:on 830603 & 17,fuel Handling Area Radiation Monitors RE8446 & 7 Found Deenergized.Caused by Blown Radiation Monitoring Cabinet Fuse.Fuse replaced.W/830701 Ltr ML20024B0471983-06-21021 June 1983 LER 83-026/03L-0:on 830524,one Half Channel Trip in Steam & Feedwater Rupture Control Sys (Sfrcs) Channel 2 Received. Caused by Component Failure.Input Buffer replaced.W/830621 Ltr ML20024A3621983-06-0909 June 1983 LER 83-024/03L-0:on 830511,while Starting Up from 830510 Reactor Trip,Quadrant Power Tilt in Quadrant Yz Exceeded Tech Spec steady-state Limit.Caused by Inherent Design of B&W NSSS & Negative Moderator Temp coefficient.W/830609 Ltr ML20024A5341983-06-0808 June 1983 LER 83-023/03L-0:on 830510,120-volt Ac Essential Bus Y4 Lost,Resulting in Deenergizing Reactor Protection & Safety Features Actuation Sys Channel 4.Caused by Blown Fuse in Inverter YV4.Power Restored to bus.W/830608 Ltr ML20024A5481983-06-0707 June 1983 Revised LER 83-002/03X-2:on 830115,18,0409,10 & 0510,RCS Dose Equivalent I-131 Exceeded Tech Spec Limit.Caused by Slight Fission Product Leakage Through Fuel Cladding.Level of I-131 monitored.W/830607 Ltr ML20023D9051983-05-26026 May 1983 LER 83-027/03L-0:on 830428,valve RC240B Would Not Close W/O Repeated Signals from Control Room.Caused by Valve Operator Torquing Out Due to Dirty & Improperly Lubricated Stem.Stem Cleaned & Torque Switch reset.W/830526 Ltr ML20023C3241983-05-0505 May 1983 LER 83-016/03L-0:on 830407,determined That Amplifier of Startup Level Transmitter LT-SP9A3 for Steam Generator 1-2 Failed.Caused by Component Failure within Amplifier. Amplifier Replaced ML20023C3021983-05-0505 May 1983 Revised LER 83-002/03X-1:on 830115,RCS Dose Equivalent I-131 Exceeded Tech Spec Limit of 1.0 Uci/Gm.Caused by Leakage of Fission Products Through Fuel cladding.I-131 Monitored Until Level Dropped ML20028E9581983-01-19019 January 1983 LER 82-068/03L-0:on 821220,core Imbalance Vs Core Power Limit Computer Alarm C963 Inoperable.Caused by Mistake in Alarm Subroutine.Alarm Statement Corrected So Limits & Value for Imbalance Scaled Same ML20028D2291983-01-0707 January 1983 Revised LER 81-045/03X-1:on 810730,after Unit Trip,Three Action Statements Entered.Auxiliary Feedwater Pump 1-2 Did Not Operate Properly.Shield Bldg Integrity Lost When Panel Blown Out.Main Steam Safety Valve Lifted at Low Setpoint ML20028C1231983-01-0303 January 1983 LER 82-064/03L-0:on 821129,decay Heat Cooler Component Cooling Water Outlet Valve on CCW Train 1 Would Not Open. Caused by Mfg Error.Flanged Bearing Missing from Actuator Mounting Plate.Flanged Bearing Installed on 821215 ML20028C3111982-12-30030 December 1982 Revised LER 81-031/03X-6:on 810512,following Reactor Trip, RCS Sample Level Peaked Above Microcurie Limit.Other Iodine Spikes Occurred 810730,0902,1016 & 23 & 1228.Caused by Slight Leakage of Fission Products Through Fuel Cladding ML20028C1971982-12-30030 December 1982 Revised LER 82-045/03X-1:on 820904 & 1203,auxiliary Feedwater Pump 1-1 Suction Valve FW786 Closed for No Apparent Reason W/O Operator Touching Close Button.Cause Unknown.Valve FW786 Reopened Upon Discovery ML20028C2591982-12-30030 December 1982 LER 82-065/03L-0:on 821201,discovered That Control Room Not Placed in Recirculation Mode within 1 H of Ventilation Sys Chlorine Detector Being Taken Out of Svc.On 821203,chlorine Detector Failed.Caused by Personnel Error ML20028B0291982-11-19019 November 1982 LER 82-054/03L-0:on 821021,Door 107 to Radiation Equipment Found Partially Open & Blocked by Hose When Personnel Attempted to Perform Routine Flush on RE-1878.Caused by Personnel Error.Personnel Counseled ML20028B2281982-11-16016 November 1982 LER 82-053/03L-0:on 821018,half Trip Alarm on Steam & Feedwater Rupture Control Sys Channel 2 Received Due to Failure of Steam Generator Level Instrument Cabinet Channel 2,24-volt Dc Power Supply.Caused by Component Failure ML20027E7891982-11-0404 November 1982 Revised LER 82-052/03X-1:on 820928,reactor Quadrant Power Tilt in Wx Quadrant Exceeded Tech Specs.Caused by Xenon Oscillation Producing Large Negative Imbalance.Control Rod Group 7 Borated Out to Reduce Negative Imbalance ML20027C9551982-10-19019 October 1982 LER 82-049/03L-0:on 820920 & 22,Channels 2 & 3 on Containment post-accident Radiation Monitor Re 4597BA Were Reading High.Caused by Problem in Microprocessor Software. New Set of Software Installed & Faulty Actuator Replaced ML20027C5381982-10-0404 October 1982 LER 82-045/03L-0:on 820904,auxiliary Feedwater Pump 1-1, Suction Valve FW786 Observed Closed for No Apparent Reason W/O Operator Touching Close Button.Cause Unknown. Valve Reopened ML20027A9471982-09-0707 September 1982 LER 82-036/03L-0:on 820808,hole Discovered in Fire Barrier Wall Above Door 309.Caused by Snubber EBD125R43 Penetrating Wall Through Pipe Shell.Hole Left by Workers After Work on Snubbers.Fire Watch Established & Hole Filled ML20052G6651982-05-0707 May 1982 LER 82-020/03L-0:on 820409,while in Mode 6,station Experienced Loss of 120-volt Ac Distribution Panel Y2.Caused by Blown YV2 Inverter Fuse When Short to Ground Occurred During Maint on Control Room Emergency Ventilation Sys ML20052E6231982-04-30030 April 1982 LER 82-019/01T-0:on 820426,some Steam Generator Tubes Adjacent to Auxiliary Feedwater Header Showed Potential Interaction W/Header Support Sys.Header Found Insecurely Fastened & Damaged.Cause & Corrections Being Investigated ML20052E8761982-04-29029 April 1982 LER 82-016/03X-1:on 820312,door 108 Found W/Both Door Closure Mechanisms Broken.Caused by Improper Operation of Door Closure Mechanisms by Personnel.Mechanisms Temporarily Repaired & New Parts Ordered ML20052C4151982-04-23023 April 1982 LER 82-018/03L-0:on 820326,electrician Cut High Voltage Cable on Source Range Detector NI-2,while Working in Containment Penetration Box P1L1L1.Caused by Problem in Coordination of Work Performed.Cut Cable Reconnected 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046C0661993-07-30030 July 1993 LER 92-009-01:on 920910,deficiencies Discovered During Dynamic Testing of Motor Operated Valves in Response to Generic Ltr 89-10.MOVs W/Deficiencies Modified or Repaired. W/930730 Ltr ML20046B6011993-07-26026 July 1993 LER 93-004-00:on 930428,plant Entered Mode 2 W/Afw Pump Turbine Main Steam Line Crossover Check Valve MS735 in Open Position.Caused by Inappropriate Use of Engineering Judgement.Valve MS735 closed.W/930726 Ltr ML20045D2451993-06-17017 June 1993 LER 93-003-00:on 930520,plant Experienced Trip from Approx & Continuity Between Fuse & Fuseholder Lost,Resulting in Loss of Selected RCS Average Temp Input to Ics.Faulty Fuse Cap & Fuse replaced.W/930617 Ltr ML20044B1681990-07-10010 July 1990 LER 90-002-01:on 900126,reactor Coolant Pump Current Monitor Inputs to Sfrcs ACH1 & Reactor Pressure Sys Channel 1 Experienced Reactor Trip.Probably Caused by Inadequate Test Switches & Isolation plug.W/900710 Ltr ML20043H3201990-06-18018 June 1990 LER 90-010-00:on 900518,station Experienced Inadvertent Safety Features Actuation Signal Level 1-4 Actuation W/Injection of 1,000 Gallons of Borated Water.Caused by Loss of 120-volt Ac Bus Y3.W/900618 Ltr ML20043B5711990-05-25025 May 1990 LER 90-008-00:on 900425,safety Features Actuation Sys Level 1 Actuation Occurred,Resulting in Trip of Containment Radiation Monitors.Caused by High Radiation Fields While Lifting Core Support Assembly.Mod initiated.W/900525 Ltr ML20043B8051990-05-25025 May 1990 LER 90-009-00:on 900426,source-check of Station Vent Radiation Monitors Not Performed Per Tech Spec 3.3.3.10. Caused by Use of Outmoded Light Emitting Dioide as Check Source.Source Check Procedures revised.W/900525 Ltr ML20042F2811990-05-0303 May 1990 LER 90-007-00:on 900403,inadvertent,inconsequential Safety Features Actuation Signal Occured While Defueled.Caused by Incidental Contact W/Monitor in Containment.Temporary Barriers Built Around monitors.W/900503 Ltr ML20042F2791990-05-0303 May 1990 LER 90-006-00:on 900403,station Experienced Safety Features Actuation Sys Levels 1 Through 5 Actuation.Caused by Contact W/Breaker Switch HAAE2 in High Voltage Switchgear Room 2. Meetings Held W/Craft personnel.W/900503 Ltr ML20042E4891990-04-16016 April 1990 LER 90-005-00:on 900314,determined That Some Class 1E Circuits That Pass Through Containment Electrical Penetrations Do Not Have Adequate Backup Fault Protection. Caused by Inadequate Design control.W/900416 Ltr ML20012D0341990-03-19019 March 1990 LER 90-004-00:on 900217,fuel Assembly Moved in Spent Fuel Pool While Emergency Ventilation Inoperable.Caused by Personnel Error.Personnel Involved Counseled & Subj LER Part of Required reading.W/900319 Ltr ML20012C7151990-03-14014 March 1990 LER 90-003-00:on 900212,station Entered Mode 6,refueling,w/o Operable Audible Source Range Indication.Caused by Personnel Error.Individual counseled.W/900314 Ltr ML20012B4851990-03-0606 March 1990 LER 83-039/03X-2:on 830726,discovered That Handwheel for Inner Door of Personnel Airlock in Shut Position & Partially Opened.Caused by Excessive Use of Door During Outages.Door Repaired & Returned to Operable status.W/900306 Ltr ML20011F3831990-02-26026 February 1990 LER 90-002-00:on 900126,reactor Tripped from 73% Power. Caused by Spurious Reactor Coolant Pump Monitor Signal Indicating Only One Pump Running in Each Loop.Pump Seal to Be Replaced During Sixth Refueling outage.W/900226 Ltr ML20006E6861990-02-20020 February 1990 LER 90-001-00:on 900118,reactor Protection Sys Channel 2 Bypassed Temporarily During Performance of DB-MI-03207. Caused by Inadequate Procedure Re Inoperable Channel Removal.Procedure SP1105.02 revised.W/900220 Ltr ML20011E2251990-01-30030 January 1990 LER 86-032-01:on 860802,inadvertent Start of High Pressure Injection Pump 1-2 Occurred.Caused by Open Relay Coil. Failed Relay Replaced & Procedure Change Initiated. W/900130 Ltr ML20005G1091990-01-0909 January 1990 LER 89-015-01:on 891026,concluded That Transmitter Was Out of Tolerance When Reactor Protection Sys Channel 2 Returned to Operable Status on 890924.Caused by leak-by in Instrument Manifold.Transmitter Recalibr successfully.W/900109 Ltr ML20042D4011990-01-0202 January 1990 LER 89-010-01:on 890612,control Room Ventilation Sys Declared Inoperable Due to Compressor High Pressure Trips. Caused by Tripping of Refrigerant Pressure Switch on High Pressure.Switch Reset & Sys retested.W/900102 Ltr ML19354D7361989-12-22022 December 1989 LER 89-018-00:on 891123,hydrogen Dilution Blower 1-1 Casing Drain Line Broke Off at Casing,Declaring Blower Inoperable. Caused by Drain Line Being Accidentally Stepped On.Drain Removed & Pipe Plug installed.W/891222 Ltr ML19332F8951989-12-13013 December 1989 LER 89-017-00:on 891113,containment Spray Pump 1-1 Inadvertently Started During Monthly Functional Test in Safety Features Actuation Sys (Sfas) Channel 1.Caused by Failed Relay in Sfas Channel 3.Relay replaced.W/891213 Ltr ML19332E7521989-12-0404 December 1989 LER 89-016-00:on 890917,unplanned Release of Radioactive Resin to Onsite Settling Basin Occurred.Caused by Personnel Error.Standing Order 89-051 Generated on 890920 to Direct Use of Working Copy of procedures.W/891204 Ltr ML19332D3111989-11-27027 November 1989 LER 89-015-00:on 890924,RCS Flow Transmitter Out of Tolerance When Reactor Protection Sys Channel 2 Returned to Operable Status.Caused by leak-by in Instrument Manifold Seen as Zero Shift.Transmitter recalibr.W/891127 Ltr ML19324C2081989-11-10010 November 1989 LER 89-014-00:on 891011,plastic Sheeting Blocked Off Fire Detectors in Auxiliary Feedwater Pump 1-1 Room & High Voltage Switchgear Room B,Making Fire Detectors Inoperable. Caused by Personnel Oversight.Event reviewed.W/891110 Ltr ML19325D4671989-10-16016 October 1989 LER 89-004-01:on 890411,determined That Circulating Water Line Break Would Result in Loss of Svc Water as Result of Concerns Raised on 890206.Cause Unknown.Standing Order 89-026 in Place to Plug Floor drains.W/891016 Ltr ML19325C8531989-10-13013 October 1989 LER 89-013-00:on 890913,hourly Fire Watch Patrol Exceeded Allowed Interval,Violating Tech Spec 3.7.10,Action a.2. Caused by Personnel Error.Individual Counseled & Event Info Distributed to Fire Watch personnel.W/891013 Ltr ML20024E2591983-08-0101 August 1983 LER 83-033/03L-0:on 830620,fire Detection Zone Reactor Coolant Pump 1-2,containment Level 603 Ft Alarmed & Could Not Be Reset.Caused by Faulty Detector String.Zone Will Be Restored During Next Refueling outage.W/830801 Ltr ML20024B8351983-07-0101 July 1983 LER 83-028/03L-0:on 830603 & 17,fuel Handling Area Radiation Monitors RE8446 & 7 Found Deenergized.Caused by Blown Radiation Monitoring Cabinet Fuse.Fuse replaced.W/830701 Ltr ML20024B0471983-06-21021 June 1983 LER 83-026/03L-0:on 830524,one Half Channel Trip in Steam & Feedwater Rupture Control Sys (Sfrcs) Channel 2 Received. Caused by Component Failure.Input Buffer replaced.W/830621 Ltr ML20024A3621983-06-0909 June 1983 LER 83-024/03L-0:on 830511,while Starting Up from 830510 Reactor Trip,Quadrant Power Tilt in Quadrant Yz Exceeded Tech Spec steady-state Limit.Caused by Inherent Design of B&W NSSS & Negative Moderator Temp coefficient.W/830609 Ltr ML20024A5341983-06-0808 June 1983 LER 83-023/03L-0:on 830510,120-volt Ac Essential Bus Y4 Lost,Resulting in Deenergizing Reactor Protection & Safety Features Actuation Sys Channel 4.Caused by Blown Fuse in Inverter YV4.Power Restored to bus.W/830608 Ltr ML20024A5481983-06-0707 June 1983 Revised LER 83-002/03X-2:on 830115,18,0409,10 & 0510,RCS Dose Equivalent I-131 Exceeded Tech Spec Limit.Caused by Slight Fission Product Leakage Through Fuel Cladding.Level of I-131 monitored.W/830607 Ltr ML20023D9051983-05-26026 May 1983 LER 83-027/03L-0:on 830428,valve RC240B Would Not Close W/O Repeated Signals from Control Room.Caused by Valve Operator Torquing Out Due to Dirty & Improperly Lubricated Stem.Stem Cleaned & Torque Switch reset.W/830526 Ltr ML20023C3241983-05-0505 May 1983 LER 83-016/03L-0:on 830407,determined That Amplifier of Startup Level Transmitter LT-SP9A3 for Steam Generator 1-2 Failed.Caused by Component Failure within Amplifier. Amplifier Replaced ML20023C3021983-05-0505 May 1983 Revised LER 83-002/03X-1:on 830115,RCS Dose Equivalent I-131 Exceeded Tech Spec Limit of 1.0 Uci/Gm.Caused by Leakage of Fission Products Through Fuel cladding.I-131 Monitored Until Level Dropped ML20028E9581983-01-19019 January 1983 LER 82-068/03L-0:on 821220,core Imbalance Vs Core Power Limit Computer Alarm C963 Inoperable.Caused by Mistake in Alarm Subroutine.Alarm Statement Corrected So Limits & Value for Imbalance Scaled Same ML20028D2291983-01-0707 January 1983 Revised LER 81-045/03X-1:on 810730,after Unit Trip,Three Action Statements Entered.Auxiliary Feedwater Pump 1-2 Did Not Operate Properly.Shield Bldg Integrity Lost When Panel Blown Out.Main Steam Safety Valve Lifted at Low Setpoint ML20028C1231983-01-0303 January 1983 LER 82-064/03L-0:on 821129,decay Heat Cooler Component Cooling Water Outlet Valve on CCW Train 1 Would Not Open. Caused by Mfg Error.Flanged Bearing Missing from Actuator Mounting Plate.Flanged Bearing Installed on 821215 ML20028C3111982-12-30030 December 1982 Revised LER 81-031/03X-6:on 810512,following Reactor Trip, RCS Sample Level Peaked Above Microcurie Limit.Other Iodine Spikes Occurred 810730,0902,1016 & 23 & 1228.Caused by Slight Leakage of Fission Products Through Fuel Cladding ML20028C1971982-12-30030 December 1982 Revised LER 82-045/03X-1:on 820904 & 1203,auxiliary Feedwater Pump 1-1 Suction Valve FW786 Closed for No Apparent Reason W/O Operator Touching Close Button.Cause Unknown.Valve FW786 Reopened Upon Discovery ML20028C2591982-12-30030 December 1982 LER 82-065/03L-0:on 821201,discovered That Control Room Not Placed in Recirculation Mode within 1 H of Ventilation Sys Chlorine Detector Being Taken Out of Svc.On 821203,chlorine Detector Failed.Caused by Personnel Error ML20028B0291982-11-19019 November 1982 LER 82-054/03L-0:on 821021,Door 107 to Radiation Equipment Found Partially Open & Blocked by Hose When Personnel Attempted to Perform Routine Flush on RE-1878.Caused by Personnel Error.Personnel Counseled ML20028B2281982-11-16016 November 1982 LER 82-053/03L-0:on 821018,half Trip Alarm on Steam & Feedwater Rupture Control Sys Channel 2 Received Due to Failure of Steam Generator Level Instrument Cabinet Channel 2,24-volt Dc Power Supply.Caused by Component Failure ML20027E7891982-11-0404 November 1982 Revised LER 82-052/03X-1:on 820928,reactor Quadrant Power Tilt in Wx Quadrant Exceeded Tech Specs.Caused by Xenon Oscillation Producing Large Negative Imbalance.Control Rod Group 7 Borated Out to Reduce Negative Imbalance ML20027C9551982-10-19019 October 1982 LER 82-049/03L-0:on 820920 & 22,Channels 2 & 3 on Containment post-accident Radiation Monitor Re 4597BA Were Reading High.Caused by Problem in Microprocessor Software. New Set of Software Installed & Faulty Actuator Replaced ML20027C5381982-10-0404 October 1982 LER 82-045/03L-0:on 820904,auxiliary Feedwater Pump 1-1, Suction Valve FW786 Observed Closed for No Apparent Reason W/O Operator Touching Close Button.Cause Unknown. Valve Reopened ML20027A9471982-09-0707 September 1982 LER 82-036/03L-0:on 820808,hole Discovered in Fire Barrier Wall Above Door 309.Caused by Snubber EBD125R43 Penetrating Wall Through Pipe Shell.Hole Left by Workers After Work on Snubbers.Fire Watch Established & Hole Filled ML20052G6651982-05-0707 May 1982 LER 82-020/03L-0:on 820409,while in Mode 6,station Experienced Loss of 120-volt Ac Distribution Panel Y2.Caused by Blown YV2 Inverter Fuse When Short to Ground Occurred During Maint on Control Room Emergency Ventilation Sys ML20052E6231982-04-30030 April 1982 LER 82-019/01T-0:on 820426,some Steam Generator Tubes Adjacent to Auxiliary Feedwater Header Showed Potential Interaction W/Header Support Sys.Header Found Insecurely Fastened & Damaged.Cause & Corrections Being Investigated ML20052E8761982-04-29029 April 1982 LER 82-016/03X-1:on 820312,door 108 Found W/Both Door Closure Mechanisms Broken.Caused by Improper Operation of Door Closure Mechanisms by Personnel.Mechanisms Temporarily Repaired & New Parts Ordered ML20052C4151982-04-23023 April 1982 LER 82-018/03L-0:on 820326,electrician Cut High Voltage Cable on Source Range Detector NI-2,while Working in Containment Penetration Box P1L1L1.Caused by Problem in Coordination of Work Performed.Cut Cable Reconnected 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & PNPP QA Program ML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1998-011, :on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle1999-09-0303 September 1999
- on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle
ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1999-003, :on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With1999-08-26026 August 1999
- on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With
ML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-013, :on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With1999-06-24024 June 1999
- on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With
ML20212H9961999-06-22022 June 1999 Safety Evaluation Supporting Amend 233 to License NPF-3 ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G6661999-06-0808 June 1999 Safety Evaluation Supporting Amend 232 to License NPF-3 ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U7371999-05-19019 May 1999 Safety Evaluation Supporting Amend 231 to License NPF-3 ML20207E8011999-05-19019 May 1999 Non-proprietary Rev 2 to HI-981933, Design & Licensing Rept DBNPS Unit 1 Cask Pit Rack Installation Project ML20207F4351999-05-0404 May 1999 Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504 ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1999-002, :on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With1999-03-0505 March 1999
- on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With
ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U2441999-02-0909 February 1999 Safety Evaluation Supporting Amend 229 to License NPF-3 ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20205K5781998-12-31031 December 1998 Waterhammer Phenomena in Containment Air Cooler Swss ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-012, :on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With1998-11-17017 November 1998
- on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With
05000346/LER-1998-009, :on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With1998-11-13013 November 1998
- on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With
05000346/LER-1998-011, :on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With1998-11-13013 November 1998
- on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With
ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process 05000346/LER-1998-010, :on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with1998-10-26026 October 1998
- on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with
05000346/LER-1998-008, :on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With1998-10-0101 October 1998
- on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With
ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-007, :on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With1998-09-22022 September 1998
- on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With
ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With 05000346/LER-1998-006, :on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources1998-08-21021 August 1998
- on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources
ML20237E3171998-08-21021 August 1998 ISI Summary Rept of Eleventh Refueling Outage Activities for Davis-Besse Nuclear Power Station ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236U5011998-07-23023 July 1998 Special Rept:On 980624,Unit 1 Site Damaged by Tornado & High Winds.Alert Declared by DBNPS Staff,Dbnps Emergency Response Facilities Activiated & Special Insp Team Deployed to Site by Nrc,As Result of Event ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-004, :on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired1998-07-13013 July 1998
- on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired
05000346/LER-1998-005, :on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations1998-07-11011 July 1998
- on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations
ML20236M9411998-07-0707 July 1998 Safety Evaluation Supporting Amend 225 to License NPF-3 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236K4321998-06-30030 June 1998 Safety Evaluation Supporting Amend 224 to License NPF-03 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-003, :on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure1998-06-18018 June 1998
- on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure
1999-09-30
[Table view] |