ML19322A920

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Forwards Insp Rept 50-269/73-07 on 730620-21 Per Rc Paulus Telcon
ML19322A920
Person / Time
Site: Oconee 
Issue date: 07/17/1973
From: Murphy C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Thornburg H
US ATOMIC ENERGY COMMISSION (AEC)
Shared Package
ML19322A903 List:
References
NUDOCS 7911270685
Download: ML19322A920 (1)


See also: IR 05000269/1973007

Text

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, UNITED STATES

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ATOMIC ~ ENERGY COMMISSION

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DIRECTORATE OF REGUIATCRY OPEPATICNS

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AT L, ANT A, GEoRos A 30303

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H. D. Thornburg, Chief, Field Support and Enforcement Branch

Directorate of Regulatory Operations, Headquarters

DUKE POWER COMPANY (OCONIE 1), LICENSE NO. DPR'38, DOCKET No.

50-269 - ENFORCEMENT CORRESPCNDENCE

As dir, cussed during a telecon with R. C. Paulus and in

accordance with Manual Chapter 0800, Section 0860.08 f, enclosed

for Headquarters' review and dispatch is the inspection report and

enforce =ent correspendence to the licensee as a result of a site

inspection on June 20-21, 1973, and a manage =ent meeting between

the Region II Director and DPC corporate management on July 19, 1973

7-

.

C. E. Murp. , .ief

RO:II:CEM

Facilities Test and Startup Branch

Enclosures:

1.

Draft ltr to DPC

2.

RO Rpt. No. 50-269/73-7

cc v/ encl. 2:

RO:HQ (5)

-u =3DR Central Files

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Regulatory Standards (3)

Directorate of Licensing (13)

cc encl. 2 only:

'PDR

' Local PDR

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'DTIE,'OR

' State

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"To be lispatched at a later date.

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DETAILS

Prepared by:

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F. Jape, Reactor d'nspdctor

Date

Facilities Test and Startup

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Branch

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R. F. Warnick, Reactor Inspector

Date

Facilities Test and Startup

Branch

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C. E. Murphy,,Ch,ief

Dat'e

Facilities Test and Startup

Branch

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Dates of Inspection: June 20-21, 1973

Reviewed by:,

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C. E. Murphy, Chief

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Facilities Test and Startup

Branch

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1.

Individuals Contacted

Duke Power Company (DPC)

J. E. Smith - Plant Superintendent

J. W. Hampton - Assistant Plant Superintendent

O. S. Bradham - Instrument and Control Engineer

D. M. Thompson - Assistant Maintenance Supervisor

J. W. Sigman - Maintenance Supervisor

D. Laning - Assistant Maintenance Supervisor -

L. E. Summerlin - Staff Engineer

J. W. Cox - Assistant Plant Engineer

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2.

General

The purpose of this inspection was to examine the management

system for handling plant problems and plant modifications,

the use of miscellaneous test procedures, and the functioning

of the Station Review Cot =nittee (SRC) .

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3.

Review of Administrative Controls for Processing Desien Changes

The administrative controls for processing station design

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changes were reviewed by the inspector. The applicable

controls in effect at the station include the following:

a.

Administrative Procedure No.10, " Station Modifications,"

dated June 14, 1973, waich presents six steps to follow

when a change is to be implemented. The steps are summarized

below:

Step 1 requires the change to be submitted as a station

problem report to the SRC for review.

Step 2 requires the' proposed change to be reviewed by

the SRC.

Step 3 requires the station superintendent to review the

change and determine if installation can proceed with his

approval or if additional approval is required from the

Assistant Vice President, Steam Production and if review

by the Nuclear Safety Review Committee (NSRC) is required.

Step 4 requires approval by the organization or an

equivalent organization which was responsible for

the original design.

Step 5 requires the use of approved checklists, in-

structions, procedures, and drawings to perform the

work.

Step 6 allows the work to be completed on verbal approval

provided the change is documented within five days.

b.

Technical Specification 6.1.2.1.d (5) , " Station Review

Committee, Responsibilities," requires the SRC to review

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proposed changes or modifications to the station design.

c.

Technical Specification 6.1.2.2.a, '.' Nuclear Safety Review

Committee," states, in part , that the NSRC will ". . . review

important proposed plant changes and tests . . . ."

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d.

Paragraphs 6 and 7 of Technical Specification 6.4, " Station

Operating Procedures", describe the review and approval require-

munts for major changes to the facility.

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Criterion V of Appendix B to 10 CFR 50 and paragraph 50.59(b)

of 10 CFR 50 were used by the inspector as the basis for this

review. Criterion V requires that activities that affect quality

be accomplished in accordance with appropriate instructions, pro-

cedures, or drawings . Paragraph 50.59(b) requires a written

safety evaluation which provides the basis for the determination

that the change does not involve an unreviewed safety question.

The period of plant operation reviewed was between February 6,1973,

to June 19, 1973. During this period, the records for the following

plant changes were audited:

a.

Control Rod Drive Gas Vent Piping

This change was made as shown on Engineering Change Order No. 236,

dated March 16, 1972. The SRC concurred with this change on

March 29, 1973, over a year af ter the change order. No other

documentation was available at the site regarding this change.

The change was made contrary to Steps 1 and 3 of Administrative

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Procedure No.10 (AP-10) as relates to reviews and approvals.

The failure to follow approved instructions appears to be in

violation of the requirements of Criterion V of Appendix B to

10 CFR 50.

b.

RCP Oil Drain System

This change was made as shown on Engineering Change Order

No. 343, dated March 16, 1973, and Steam Production Depart-

ment Notice of Design Chant,e No. 47, dated March 24, 1973.

The SRC reviewed the proposed change on March 30,1973, and

recommended that the oil slinger-catcher, designed by

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Vestinghouse, be installed on all reactor coolant pumps. The

committee also recocmended that censideration be given to

installation of a large backup overflow pipe on the upper

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bearing reservoirs to deflect oil from the reactor coolant

piping in case of an oil cooler rupture.

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There is no documentation regarding action on the SRC's

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recommendation nor is there any followup in the minutes

of the SRC since March 30, 1973.

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This change was made contrary to Steps 1 and 3 of AP-10.

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Failure to follow instructions appears to be in violation

of the requirements of Criterion V of Appendix B to 10 CFR 50.

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The safety evaluation required by paragraph 50,59(b) of

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10 CFR 50 apparently was not completed. Failure to perform

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the safety evaluation appears to be in violation of paragraph

50.59(b) of 10 CFR 50.

Turbine Bypass Control Modification

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c.

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This change was made as shown on Engineering Change Order 243,

dated May 8, 1973. The change was reviewed by the SRC with

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final approval to be granted after completion of the power

escalation tests.

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This change was made contrary to Steps 1 and 3 of AP-10.

Failure

to follow instructions appears to be in violation of the require-

ments of Criterion V of Appendix B to 10 CFR 50.

The safety evaluation required by paragraph 50.59(b) of 10 CFR 50

apparently was not completed. Failure to perform the safety

evaluation appears to be in violation of paragraph 50.59(b) of

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10 CFR 50.

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Feedwater Flow-Turbine Trih!

d.

This change was rude as shown on an engineering sketch dated

June 12, 1973. SRC reviewed this proposed change on June 12,

1973, and recommended that it be made.

The change was made contrary to Steps 1 and 3 of AP-10.

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The failure to follow approved instructions appears to be in

violation of the requirements of Criterion V of Appendix B to

10 CFR 50.

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1/ See RO Inspection Report No. 50-269/73-6, Details, paragraph 2.

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The safety evaluation required by paragraph 50.59(b) of 10 CFR 50

apparently was not completed. Failure to perform the safety

evaluatien appears to be in violation of paragraph 50.59(b)

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of 10 CFR 50.

Electrical Auxiliary Transfer 1!

e.

This change was made as shown on'an engineering sketch dated

June 12, 1973. SRC reviewed this proposed change on June 12,

1973, and recommended that it be made.

Failure

This change was made contrary to Steps 1 and 3 of AP-10.

to follow instructions appears to be in violation of the require-

ments of Criterion V of Appendix B to 10 CFR 50.

The safety evaluation required by paragraph 50.59(b) of 10 CFR 50

apparently was not completed. Failure to perform the safety

evaluation appears to be in violation of paragraph 50.59(b) of

10 CFR 50.

f.

CRD Motor Fault Time Delay

This change was made as shown on Steam Production Department

Notice of Design Change No. 59, dated June 19, 1973. SRC

reviewed this proposed change on June 19, 1973, and recommended

that it be made, stating thag it was an interim fix until the

auxiliaries transfer probles- is resolved. DPC design

engineering also acproved this change on Jane 18, 1973. A

procedure with a e ecklist was prepared and used to install

this change. The installation was audited by the station QC

personnel.

The change was cade contrary to Steps 1 and 3 of AP-10.

Failure

.to folicw instructions appears to be in violation of the require-

ments of Criterion V of Appendix B to 10 CFR 50.

The safety evaluation required by paragraph 50.59(b) of 10 CFR 50 '

apparently was not completed. Failure to perform the safety

evaluation appears to be in violations of paragraph 50.59(b)

of 10 CFR 50.

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1/ See RO Inspection Report No. 50-269/73-6, Details, paragraph 2.

2_/ See Design Change, " Electrical Auxiliary Transfer," above.

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The results of the RO inspector's audit indicate a general failure

to follow established procedures in accomplishing plant changes

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that affect quality. The handling of design changes is not con-

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sistent, and it appears to vary depending on who initiates the

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change and the priority of the change.

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All changes initiated within the Steam Production Department

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are not handled identically. For example, the instrument and

control section numbers design changes and uses a " Notice of

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Design Change" form to document the change. The plant maintenance

section of the Steam Production Department has no formal method for

handling design changes.

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In all cases, the inspector found that the failure to follow

instructions appears to be in viola' tion of Criterion V, " Instructions,

Procedures, and Drawings," of Appendix B to 10 CFR 50. When

this finding was discussed with the licensee's representative,

he stated that a more formal method for obtaining the necessary

reviews and approvals will be developed, and the station

instructions will be revised to cover this problem area.

In addition,10 CFR 50.59(b) requires that the licensee perform

a safety evaluation and maintain written records of the safety

evaluation which provides the bases for the determination that

the change in facility or procedures does not involve an un-

reviewed safety question.

Contrary. to this requirement, written safety evaluations were

not performed for the modifications to the safety related equip-

ment reviewed by the inspector.

4.

Review of SRC

The inspector examined the records of the SRC and compared the

committee's performance with the require =ents of Technical Specifications 6.1.2.1 and 6.2.

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The minutes of the SRC meetings held since the operating license

was issued (February 6,1973, through June 19, 1973) were examined

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by the inspector. The results are described in the following

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paragraphs:

a.

Membership of the SRC

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The SRC is composed of the assistant plant superintendent,

the operating engineer, the technical support engineer, and

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two other members of the station supervisory staff appoiated

by the plant superintendent. The maintenance supervisor and

the health physics supervisor are the two appointed members.

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The assistant plant superintendent is the SRC chairman, but

when he has been absent, an acting chairman has been appointed

by the superintendent.

This meets Technical Specification 6.1.2.1.a., which specifies

the membership requirements of the SRC.

b.

Meeting Frequency of the SRC

The SRC is required to meet at least once each month and, as

required, on call by the chairman. The committee met more

frequently than required. The inspector reviewed minutes

for 58 meetings which were held between the date the operating

license was issued, February 6,1973, and June 19, 1973.

The frequency of the meetings complies with the requirements

of Technical Specification 6.1.2.1.b.

c.

Attendance at SRC Meetings

During March, all members of the SRC attended 13 out of the 15

meetings . In April, all SRC members attended 6 out of 15

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meetings . In thy, the full committee attended 2 out of 10

meetings, and only 1 out of 11 meetings so far in June. One

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committee member attended only 36 out of 58 meetings. The

change in the record of attendance is significant but does

not violate any regulatory requirement.

Technical Specification 6.1.2.1.c states that the SRC meetings

shall be attended by a quorum made up of a chairman plus two

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members at each meeting. The minutes of the SRC meetings show

a quorum was in attendance in 57 out of the 58 meetings. The

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meeting on June 8,1973, was attended by two members plus the

plant superintendent, who is not an SRC member. This appears

to be in violation of Technical Specification 6.1.2.1.c.

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Records

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The master file of SRC meeting minutes did not contain the

minutes for meetings held on April 10, 1973, and May 5, 1973.

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The inspector found evidence where the committee had reviewed

die following incidents, but minutes were not available for

these meetings:

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(1) Engineered safeguards (ES) valve not fully open (Valve CF-1).l*'

(2) ES valves (BS-1 and -2) failed to open. /

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(3) Violation of TS 4.11.1 - Keowee River continuous sample. !

(4) Violation of Nonradiological Technical Specification 1.2 -

Wastewater collection basin pH.$/

e.

Responsibilities of the SRC

(1) Procedure Reviews

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Technical Specification 6.1.2.1.d (1) requires the SRC to

review all new procedures or proposed changes to existing

procedures which affect operational safety.

(According to

DPC's operational quality assurance manual, an "A" in the

procedure number indicates the procedure is safety related.)

Contrary to this requirement, the SRC meeting minutes of

March 29, April 5, 10, 16, 19, 25, 27 and 30, May 8 and

22, and June 15, 1973, state that changes to procedures

(of which approxi=ately 75 were labeled safety related by

DPC) were presented to the SRC but were not reviewed by the

SRC.

Each of the changes had been reviewed by one member of the

SRC but the results of each review had not been reported to

the committee. This apparent violation of Technical Specification 6.1.2.1.d (1) was discussed at the management

interview.

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1/ See RO Inspection Report No. 50-269/73-4, Details I, paragraph 13.

2/ See RO Inspection Report No. 50-269/73-4, Details I, paragraph 14,

3/ See RO Inspection Report No. 50-269/73-4, Details I, paragraph 4.

4/ See RO Inspection Report No. 50-2o9/73-3, Details I, paragraph 4.

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(2) Review of Station Operation and Safety Considerations

Technical Specification 6.1.2.1.d (2) requires the SRC to

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review station operation and safety considerations.

Contrary to this requirement, the minutes of the SRC

meetings do not reflect that the SRC reviewed:

(1) the

oil fire

RCP-1A1 (the second reactor coolant pump

oil fire)gy; nor (2) the lifting of the main-steam relief

valvea at 15% of full power (during whic} time part of the

turbine building siding was blown off) .2

(DPC management

was not certain whether or not the main steam relief valves

should have lifted at 15% of full power.) (See paragraph 10

below.)

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(3) Review of Abnormal Occurrences, Unusual Events, and

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Violations of Technical Specifications

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Tecanical Specification 6.1.2.1.d (3) requires the SRC to

review abnormal occurrences and violations of the Technical

Specifications and to make recommendations to prevent

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recurrence. Technical Specification 6.2.2 requires the

superintendent to cause the SRC to review abnormal occur-

rences (AO) and unusual events (UE), prepare written reports,

and make reco=mendations concerning corrective and preventive

actions.

Contrary to these requirements, the SRC meeting minutes do

not reflect that the following A0's, UE's or violations of

technical specifications were reviewed by the SRC:

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(a) Violation of Technical Specification 4.12.1 " Quarterly

Test of Control Room Filtering System Components"

This specification requires the flow to be measured

across each bank of control room filters. No in-

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strumentation was installed to facilitate measuring

the flow. The deficiency was found on April 26, 1973.

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1,/ See RO Inspection Report No. 50-269/73-3, Details I, paragraph 5.

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2/ See RO Inspection Report No. 50-269/73-6,Section VI, " Unusual

Occurrences."

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Ob) Violation of Technical Specification Table 4.1-3,

3 1nimum Sampling Frequency"

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This spe.cification requires samples to be obtained and

analyzed for boron after each makeup to dhe core flood

tanks, the borated water storage tank, and the spent

fuel pool. A 7PC audit on June 4-6, 1973, reported

violations of this specification.

(c) Violation of Technical Specification 3.4.3, " Turbine

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Bypass System"

This specifications requires all four valves to be

operable when the reactor coolant system is above

250*F.

One valve was out of service on May 4 and

one was out of service on May 5,1973. Operation

with a turbine bypass valve out of service is a

violation of a limiting condition for operation and

is reportable as an abnormal occurrence.

(d) Abnormal Occurrence - Leak in Incore Instrument Line

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On May 18,1973, a leak was discovered on one of the

incore instrument lines.

(These lines constitute a part

of the reactor coolant system boundary and are designed

to contain the radioactive materials resulting from the

fission process.) DPC first stated that this was an AO,

then questioned whether or not it actually was; however,

in a subsequent phone conversation with the inspector

DPC management agreed to report this as an AO.

(e) Unusual Event - Oil Fire at RCP-1A1

See RO Inspection Report No. 50-269/73-3, Details I,

paragraph 5.

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The inspector noted four other items (two technical specification

violations and two UE's) that were not recorded nor discussed in

the SRC meeting minutes. Although not found in the minutes of the

SRC meetings, documentation at the site indicated these items may

have been reviewed by the SRC. The four items are:

(a) Engineered safyguards (ES) valve not fully open

TValve CF-1).1

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1/ See RO Inspection Report No. 50-269/73-4, Details I, paragraph 13.

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(b) ES valves (BS-1 and -2) failed to open.-

(c) Violation of Technical S peification 4.11.1 - Keowee

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River continuous sample

(d) Violation of Nonradiological Technical Specification 1.2 -

Wastewater collection basin pH /

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These examples of the apparent violations.of Technical Specifications 6.1.2.1.d (3) and 6.2.2 were discussed

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at the management interview.

5.

Miscellaneous Test Procedures

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Genecal

DPC's Administrative Policy Manual for Operational Quality

Assurance (APM/NS), Section 4.4, provides administrative

instructions for permanent station procedures.

Paragraph 4.4.1 lists the following types of procedures

which must meet the QA requirements for permanent station

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procedures:

(1) Emergency Procedures (EP)

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(2) Instrument Procedures (IP)

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(3) Maintenance Procedure (MP)

(4) Operating Procedures (OP)

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(5) Periodic Test Procedures (PT)

At the Oconee Nuclear Station, a sixth category of procedures

has been established. These are designated as miscellaneous

test procedures and are not required to receive the level of

reviews and approvals that the permanent plant procedures

receive. Additionally, the results of the miscellaneous

tests are not required to receive the same level of reviews

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and approvals that the permanent station tests receive.

1/ See, RO Inspection Report No. 50-269/73-4,' Details I, paragraph 14.

2/ See RO Inspe~ction Report No. 50-269/73-4, Details I, paragraph 4.

1/ See RO Inspection Report No. 50-269/73-3, Details I, paragraph 4.

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The inspector reviewed the master file of miscellaneous test

procedures to deternine if any dealt with the testing of

safety related systems and, if so, whether or not the prep-

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aration of the procedures and the conduct of the tests conformed

to DPC and regulatory requirements. The extent and level of the

reviews and approvals given the procedures and test results

varied widely from procedure to procedure. The results of

the inspector's review for each specific test are summarized

below,

b.

Specific Tests

(1) 4160 v Bus Transfer Time Test

The stated purpose of the test was to determine the transfer

time of 4160 volt breakers BlTl and BlT3. These breakers

are a part of the engineered safeguards switchgear and the

automatic transfer of the breakers is required in the event

.of the loss of power to the 4160 volt bus.

The procedure had not been previously classified as

safety related and assigned an alpha-numeric designation

as required by paragraph 4.4.4.2 of the APM/NS to assure

proper reviews and approvals. The failure to follow the

approved administrative procedures appears to be in

violation of Criterion V af Appendix B to 10 CFR 50.

The procedure did not adequately define acceptance limits

contained in applicable design documents and that the test

coordinator or data taker could determine that the test

had been successful. Failure to define acceptance limits

appears to be contrary to Criterion XI of Appendix B

to 10 CFR 50.

When questioned, a member of tha station manage =ent advised

the inspector that the documentation of the test results

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had not been reviewed by the SRC but had been forwarded

to DPC design engineering for their review. Failure

of the SRC to review the tests appears to be a violation

of Section 6.1.2.1.d (1) of the Technical Specifications.

(2) Emergencv Feedvater Pump Functional. Test

The st5ted purpose of this test was:

(a) To determine the proper valve lineup of the emergency

feedwater system (EFWS).

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(b) To demonstrate the ability of the EFW pump to deliver

water to the steam generator through the auxiliary

nozzle utilizing main steam.

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(c) To demonstrate auto start and to measure the response

time of the EFW pump.

(d) To verify main turbine trip on loss of the main

feedwater pumps (MWP) .

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The EFWS is required for the addition of water to the steam

generator on a trip of the MFWP's and is a safety related

system.

The procedure had not been properly classified as safety

related and assigned an alpha-numeric designation as

required to assure proper reviews and approvals by

paragraph 4.4.4.2 of the APM/NS. The failure to follow,

approved administrative procedures appears to be a

violation of Criterion V of Appendix B to 10 CFR 50.

A revision to the procedure had been penciled into the

body of the procedure. A procedure revision form had

not been completed for this revision as required by

paragraph 4.4.6.1 of the APM/NS. Failure to follow the

approved administrative procedures appears to be a

violation of Criterion V of Appendix B to 10 CFR 50.

A revision to the procedure which changed the trip

point of the main turbine generator from 600 psig to

800 psig had been approved by M. D. McIntosh, Operating

Engineer, on June 10, 1973. The APM/NS, paragraph 4.4.2.2.3,

specifies that the plant superintendent shall approve safety

related procedure revisions. Failure to properly approve

procedure revisions appears to be a violation of Criterion VI

of Appendix B to 10 CFR 50.

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The APM/NS, paragraph 4.4.6.l(a), requires that a " Proposed

Procedure Revision" form be completed for each proposed

revision to a safety related procedure. This form re-

quires that a safety analysis be performed for the revision.

Contrary to this requirement, documentation was not avail-

able ,to indicate that safety analyses were performed for

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the revisions to this procedure. The failure to follow

the requirements of the administrative procedures appears

to be a violation of Criterion V of Appendix B to 10 CFR 50.

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Documentation was not available to verify that Section 10

and Steps 12.9 and 12.10 of the test procedure had been

completed . In addition, the test data sheets did not

indicate the dates during which the tests were conducted

nor to which power level the data applied.

Failure to

maintain adequate quality assurance records appears to be

a violation of Criterion XVII of Appendix B to 10 CFR 50.

Paragraphs 4.4.6.l(c) and (g) of the APM/NS specify that

revisions to procedyres shall be approved within seventy-two

hours and filed with the = aster file copy. Revision 4 to

the procedure had not been approved within the seventy-two

hours specified and a copy of the change had not been filed

in the master file. The failure to obtain the proper revision

approvals and to control the distribution of the revision

appears to be a violation of Criterion VI of Appendix B to

10 CFR 50.

The SRC review of the original procedure listed J. E. Smith

as one of three members present. The membership of this

committee does not include J. E. Smith. The Technical Specifications, Section 6.12.1.c. states that a quorum of

the committee is the chairman and two members. Failure to

have a quorum of the committee while conducting committee

business appears to be a violation of the technical specifi-

cations.

(3) Check of Safety and Shim Control Rod Actuators for

Frictional Binding

The purpose of this procedure was to' determine, through

weight differential measurements, that the control rod

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actuator and its coupled rod were not binding. Although

the proccdure was initialed as being reviewed by the SRC

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on February 17, 1973, the review appeared to be superficial

in that the deficiencies listed below were not identified.

The failure to review safety related procedures appears to

be contrary to the requirements of Technical Specification 6.1.2.1.d (1) .

Operation of '*te control rods and actuators are required to

effect orderly control of the reactor and are classified as

safety feature syste=s.

Contrary to the requirements of

paragraph 4.4.4.2 of the APM/NS, this procedure had not

been properly classified as safety related and assigned

an alpha-numeric designator to assure proper reviews and

approvals. The failure to follow the approved administrative

procedures appears to be a violation of Criterion V of

Appendix B to 10 CFR 50.

The procedure was inadequate in that the following were not

included:

(a) The minimum boron concentration of the reactor coolant

was not specified.

(b) 'The verification of proper operation of the nuclear

instrumentation was not specified.

(c) The qualifications of the hoist operator were not

specified.

(d) There was no limitation on the number of control rods

that could be in the "Out" position at any one time.

(e) There was no requirement that the reinsertion of the

control rod be verified.

(f) There was no requirement that the position indication

be verified at any time during the operatica.

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(g) The procedure did not provide any method, such as check

sheets, to assure that the procedure steps were followed

or to document that the procedure was followed.

(h) The procedure did not specify the steps to be followed

in the event of an emergency.

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(i) The procedure did not require that a licensed operator

manipulate the controls or to be present when the con-

trols were manipulated.

(Controls in this case being

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the air hoist.)

Failure to provide adequate procedures appears to be contrary

to the requirements of Criterion V of Appendix B to 10 CFR 50.

The method prescribed in the procedure for the conduct of the

test specified that the hoist operator lif t each control rod

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with an air hoist and, by measuring the pounds of force

required, determine the friction drag on the drives and rod.

The procedure required that voice co=munication be main-

tained between the hoist operator and a licensed reactor

operator in the control building.

Part 50.54(i) of 10 CFR 50 provides that the licensee

not permit the manipulation of the controls of any facility

by any one who is not a licensed operator or senior operator

unless the manipulation is done under the direction of and

in the presence of a licensed operator or senior operator.

An unlicensed maintenance technician operated the hoist in

conducting this test. The manipulation of the control rods

by an unlicensed person appears to be a violation of

Part 50.54(1) .

(4) Auto Transfer From IT to CT1 Transfor er Without Generator

Lockout

The purpose of this test was to verify that the time required

for the transfer of station power from the unit station service

transformer IT to the reserve station service transfer CT1

would not cause a lockout of the main generator.

This procedure was approved by Smith on February 3,1973,

and was perfor=ed on February 4,1973. The procedure

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required the disabling of the emergency start relay for

the Keowee Hydro Station. The operating license for

Oconee 1 was issued on February 6,1973, and the Keowee

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Hydro Station provides emergency power for the Oconee

Nuclear Station.

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The procedure did not require that the emergency start

relays be restored to service nor whether their correct

operation need be verified. Failure to identify the status

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of the individual items of equipment appears to be contrary

to the requirements of Criterion XIV of Appendix B to

10 CFR 50.

(5) Inspection of Retainer Nuts on Engineered Safeguards (ES)

Valves

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On April 9, 1973, the yoke locking nuts on two ES valves

in the core flood system were found to be loose preventing

proper operation of the valve position indication switches

and proper operation of the valves. The purpose of this

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procedure was to determine if other ES valves also had

loose and/or improperly staked lock nuts. The following

valves were checked:

BS-1, BS-2, CS-5, HP-24, HP-25, HP-26, LP-3, LP-17,

LP-19, LP-20, LP-21, LP-22, PR-1, PR-6, PR-7, PR-9,

CC-7, CF-1, CF-2, FDW-103, EDW-104, GWD-12, LPSW-5,

.LPSW-6, and LPSW-18.

The procedure was approved on April 14,1973, by the

maintenance supervisor. Documentation was not available

to verify that the procedure had been reviewed by the SRC.

The APM/NS, paragraph 4.3.2.2.8, requires that safety

related procedures receive the approval of the plant

superintendent and be reviewed by the SRC. The failure

to follow approved administrative procedures appears to

be a violation of Criterion V of Appendix B to 10 CFR 50.

The data for approximately ten valves had been marked

over such that the record of the "as. found" condition

of the locking nut could not be determined. The revisions

to the data were neither initialed nor dated. Failure to

provide records to furnish evidence of activities affecting ,

quality appears to be in violation of Criterion XVII of -

Appendix B to 10 CFR 50.

(6) Hydro of RC-48

The. purpose of this procedure was to hydro a replacement

valve located in the 1B loop drain and pressure transducer

line. This valve is one of two valves that would form the

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second boundary of the reactor coolant system (RC System)

if the line were removed from service. The valve normally

sees the reactor coolant system pressure.

This procedure is for the test of a safety related component

and the development of the procedure and the hydro of the

valve and it appe es that this test should have conformed

to the requirements specified in the APM/NS. An alpha-

numeric designator indicating that the test was safe +.y

related and would obtain the proper reviews and approvals

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was not assigned this test. A centrolling procedure for

conducting hydro tests on the RC and SC systems is available.

The procedure actually used for conducting this test is

entitled " Controlling Procedure for Hydrostatic Test

(Excluding RC System and SC System) ." The apparent failure

to follow the approved administrative procedures is a violation

of Criterion V of Appendix B to 10 CFR 50.

(7) Shuffling Control Components in Spent Fuel Pool

This procedure was designed to control the removal and

reinstallation of control rods in the fuel assemblies.

The procedure was approved by McIntosh and initialed by

Smith. No documentation was available to verify that the

procedure had been reviewed by the SRC. The apparent

failure to review the procedure is a violation of Technical Specification 6.1.2.1.d (1) . The procedure had not received

an alpha-numeric designator as required by the APM/NS. The

apparent failure to follow approved administrative procedures

is a violation of Criterion V of Appendix B to 10 CFR 50.

The above deficiencies were discussed in detail in the management

interview. Smith and Powell were advised that time had not been

available to review all of the miscellaneous tests, but that

numerous others appeared to have safety significance. Smith

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assured the inspectors that a review of all of the tests would

be made to formalize those required by the APM/NS.

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6.

NSRC Minutes

The inspector reviewed the minutes of the NSRC which were in the

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Oconee master file. The minutes of the most recent meeting con-

tained in these files were for a meeting conducted on January 30, 1973.

Attached to these minutes was a list of recommendations and requests

for information that the NSRC indicated had not yet been resolved.

This list contained eighteen items which dated from November 1971

to January 30, 1973, and which, according to the technical specifi-

cations, are provided to appropriate members of management. The

failure to obtain resolution of these items is indicative that the

management reviews as required by Criterion II of Appendix B to

10 CFR 50 appear to be inade,quate.

The inspector questioned the station management about other NSRC

meetings . He was advised initially that a second meeting had been

held in May 1973, but in the management interview, two additional

meetings were indicated. Minutes of these meetings were not available.

Section 6.5.o. of the technical srecifications requires that copies

of the NSRC minutes be retained in the plant files.

Failure to

retain these files appears to be a violation of this requirement.

The inspector advised members of DPC management during the management

interview that the records did not indicate that the NSRC had reviewed

any of the deficiencies revealed by the AEC inspections.

Although

this is not a specific requirement of the committee, the inspection

reports and letters could be a source of information that would aid

the com=ittee in its operation. The inspector was advised that his

comment would be considered.

The inspector, in reviewing the NSRC minutes, also observed that

the committee had only. requested to review two safety related

procedures in recent months. He urged that the committee give

more attention to this area since the review of such procedures

is a responsibility of the group. He was assured that this would

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be done.

7.

Failure to Obtain Clearances for Maintenance

Time did not permit a complete review of the station logs during

this inspection. The inspector quickly read the shif t supervisor's

log for the period from January to April 1973.

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This log contained almost daily entries pertaining to Unit 2

events that were not related to Unit 1 operations. Licensee

manatement assured the inspector that this discrepancy had been

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recently corrected and should not occur again.

An entry on March 23, 1973, stated that an equipment manufacturer's

representative and an engineer from the DPC Design Department had

removed the strainer on the oil lift system for the 1B1 reactor

coolant pump. This operation was performed without obtaining

clearance from the control room operator and without the pump

being deenergized. Oil was spilled from the system as a result

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of these operations. This event was discussed in the management

interview. Licensee management stated that the individuals who

had removed the strainer were violating plant administrative pro-

cedures, the individuals were severely reprimanded and that

all personnel were cautioned against unauthorized operation of

equipment .

8.

Steam Relief Valve Operation

During plant testing the week of June 10, 1973, the main steam

relief valves had relieved subsequent to reactor scrams and the

released steam had blown the siding off the auxiliary building in

the area of the valves. The valves had operated when the turbine

had tripped from power levels as low as 15%. As a part of the

inspection followup, Murphy questioned members of the plant staff

about these occurrences. None of the staff members could answer

relatively basic questions about the operation of the valves such

as:

a.

Which valves relieved during scrams from 15% power level and

from 40% power levels?

b.

Did the valves relieve in the expected se,quence?

c.

Was relief valve operation expected on a trip at 15% power,

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i.e., did analyses indicate that the valves should release at

trips from this power level?

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If valves were expected to relieve, did the proper number

relieve?

e.

In every case, did the valves relieve at the set pressure?

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Was the relieving of the valves at 15% pcwer analyzed to

determine if the event was considered to be safety related

as an unusual event or abnormal occurrence as defined in the

technical specifications?

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The inspector was given the following information relating to

the safety valves.

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a.

The plant staff had previously determined that the set points

of the valves had drifted downward from the points at which

they had been originally set to relieve, i.e. , they lifted

at a lower system preesure. The staff was not concerned since

this drift was in the " conservative" direction. It had not

been determined the extent of the drift or if the drif t was

continuing, nor had the undesired effects of the unanticipated

operation been considered.

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b.

The SRC had not reviewed the occurrence.

c.

The cause of the valve setpoint drift had not been determined.

It had not been ascertained how much might be "one time" drif t,

such as would occur by the permanent relaxation of the spring

after being heated, nor how much might be repeatable and cyclic

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such as changes caused by the temperature fluctuations experienced

by the valves.

The inspectors expressed concern during the management interview

about the lack of action as related to the valve operations.

Licensee's management agreed that a review would be made of this

area and any corrective actions required would be taken. RO:II

will be advised of the resuits of the study, and if the study

indicates that the operation of the valves at the lower power

levels is a reportable event, then the report will be issued.

This item will be included as an unresolved item until DPC

completes this study.

9.

Plant Reporting Reouirements

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The inspector was advised by members of the plant staff that each

event which was potentially reportable to the AEC was investigated

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by a me=ber of the plant staff to determine if the event was indeed

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reportable. The plant superintendent assigned a staff member to

perform the 12vestigation. Upon further questioning, the inspector

determined that there was no formal method for assuring that the

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revealed which had not been reviewed, it does not appear that

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the licensee has an adequate procedure to assure that reportable

occurrences are recognized at the time of the event and that

management is apprised of the occurrences (paragraph 4). The

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apparent failure to provide adequate methods to identify

deficiencies, deviations and malfunctions appears to be contrary

to the requirements of Criterion XVI of Appendix B to 10 CFR 50.

In addition, recorder charts were not indexed with actual time

marks at a frequency that would permit correlation of the charts

accurately enough to reconstruct the details.of an event. One

method of indexing the charts would be to have the operators mark

the actual time at eac;i shift change. Management agreed to consider

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this method. These items were discussed in the management interview.

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