05000333/LER-1980-051-03, /03L-0:on 800521,during Surveillance Testing, Recorder for SRM Channels a & C Found Operating in Degraded Mode.Caused by Instrument Drift.Recorder Recalibr & Tested Satisfactorily in SRM Functional Test

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/03L-0:on 800521,during Surveillance Testing, Recorder for SRM Channels a & C Found Operating in Degraded Mode.Caused by Instrument Drift.Recorder Recalibr & Tested Satisfactorily in SRM Functional Test
ML19318A140
Person / Time
Site: FitzPatrick Constellation icon.png
Issue date: 06/13/1980
From:
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19318A139 List:
References
LER-80-051-03L, LER-80-51-3L, NUDOCS 8006180503
Download: ML19318A140 (1)


LER-1980-051, /03L-0:on 800521,during Surveillance Testing, Recorder for SRM Channels a & C Found Operating in Degraded Mode.Caused by Instrument Drift.Recorder Recalibr & Tested Satisfactorily in SRM Functional Test
Event date:
Report date:
3331980051R03 - NRC Website

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NRC DOMM 344 U. S. feucLEAR REGULATORY COMMISSION

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LICENSEE EVENT REPORT CONTROL BLCCK: l l

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60 on DCCKET NUMSER 68 69 EVENT CATE 74 75 REPORT QATE So EVENT DESCRIPT1CN AND PROBA8LE CCNSECUENCES h Io!2i l During normal shutdown operations while conductino surveillar.ce tests. recorder for l

t o 131 l SRM channels A and C Indicated 80,000 CPS when it should.'iave indicated 100.000 CPS.

I This failure is considered operation in a degraded mode permitted by TS Table 3.2.6.

I lo tal i SRM indicators (local and remote) and trip units were not effected and the plant l

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lo is l l was in the cold condition preparing for refuel.

The event did not represent a lo irl i significant hazard to public health and safety.

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CC E SLBC E COMPONENT CODE SUSC00E SU E

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Following recalibration, orocer operationt li ii i I was demonstrated by satisfactory completion of Operations Surveillance Test F-ST-50 i

p 1, i : j l titled "SRM Functional Test".

No additional action is requi red.

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