ML19316A602

From kanterella
Jump to navigation Jump to search
Monthly Operating Rept for Feb 1975
ML19316A602
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 03/07/1975
From:
DUKE POWER CO.
To:
Shared Package
ML19316A599 List:
References
NUDOCS 8001130114
Download: ML19316A602 (3)


Text

'

4

.O Oconee Unit 2 UNIT March 7, 1975 DATE 50-270 DOCKET NO.

OPERATING STATUS February 28, 1975 February 1, 1975

_ TilROUGH 1.

REPORTING PERIOD.

HOURS IN REPORTING PERIOD:

671.00 2.

CURRENTLY AUTHORIZED POWER LEVEL (MWthe MAN. DEPENDAliLE CAI ACITY (Mwe. NET, R71 None 3.

LOWEST POWER LEVEL TO WHICH SPECIFICALL) RESTRICTED (It ANY (MWe. NET):

4.

REASONS FOR RESTRICTION (IF ANY):

THIS CL MULATIVE REPORTING Pi RIOD YR TO DATE TO D ATE 0

437.4 2383.5 5.

HOURS REACTOR WAS CRITICAL.

0 O_

0 6.

REACTOR RESERVE SHUTDOWN HOLRS 0

. :;. 3 2304.7 7.

HOURS GENERATOR ON LINE.

0 0

0 8.

UNIT RESERVE SHUTDOWN HOURS,

9.

GRO'4 THERMAL ENERGY 0

1055278 5362176 GENERATED (MWH) 10.

GROSS ELECTRICAL ENERGY 0

357490 1826466 GENER ATED (MWH) 11.

NET ELECTRICAL ENERGY GENER STED

(-2905) 334678 17???na iMWH) 12.

RLACTOR AVAILABILITY F ACTOR (1, 0

30.9 57.4 O

30.3 55.5 13.

UNIT AVAILABILITY F ACTOR (2)

O 27.2 47.6 14.

UNIT CAPACITY F ACTOR (3i 15.

UNIT FORCED OUTAGE RATE (4) 100.0 69.7 44.4 16.

SHUTDOWNS SCHEDULED TO BEGIN IN NEXT 6 MONTHS (STATE TYPE.DATE. AND CUR AT!ON OF E ACH1:

17.

IF SHUT DOWN AT END OF REPORT PERIOD. ESTIM ATED DATE 01 STARTUP:

March 7, 1975 18.

UNITS IN TEST STATUS (PislOR TO COMMERCIAL OPERATION) RE PORT THE FOLLO4 tNG:

DATE LAST D4TE FORECAST ACH'IEVED INITI AL CRITIC ALITY INITIAL ELECTRIC AL POWER GENE R ATION COMMERCIAL OPLR ATION

^

^

(1)

REACTOR AVAILABILITY FACTOR =

X 100 (2)

UNIT AVAILABILITY F ACTOR X 100 H

1 NFT EllrTRICAL POWFR tiF NER ATED (3) UNIT CAPACITY FACTOR

=

MAX. DLPENDABLL CAPAt'IT) :MWe.blT) X HOURS IN REPOR flNU PERIOD l

(4)

UNIT FORCED OUTAGl: R ATE OR R

M + I'ORCFD OUT4GE HOURS te00,,aojjy gygQ$$fff$$

,~

DOCKET NO. 50-270 Oconee Unit 2 UNIT DATE 3/7/75 AVERAGE DAILY UNIT POWER LEVEL MONTH February, 1975 AVERAGE DAILY POWER LEVEL AVERAGE DAILY POWER LEVEL DAY (MWe-net)

DAY (MWe-net) 0 1

0 17 0

2 0

18 0

0 39 3

o 0

g 4

0 0

21 5

0 0

22 6

0 0

23 7

0 24 0

8 0

25 0

9 0

0 26 10 0

0 27 11 0

0 28 12 0

29 13 14 0

30 15 0

31 0

16 DAILY UNIT POWER LEVEL FORM INSTRUCTIONS On this form, list the average daily unit power level in MWe-net for each day in the reporting month.

Compute to the nearest whole megawatt.

These figures will be used to plot a graph for each reporting month. Note that by using maximum dependable capacity for the net electrical rating of the unit, there may be occasions when the daily average power level exceeds the 1007c line tor the restricted power level lincl. In such cases, the average daily unit power output sheet should be footnoted to explain the apparent anomaly.

IXK'KET NO.30-270 Oconee Unit 2 UNIT SHUTDOWNS UNil' N AMli DATI:

March 7, 1975 REPORT MONTil February, 1975 TYPE METHOD OF F FORCED DURATION SHUTTING DOWN NO.

DATE S-SCHEDULED (HOURS)

REASON {1)

THE REACTOR (2)

CORRECTIVE ACTIONS / COMMENTS T

2 750119 F

671.0 A

1 Replacement of leaking pressurizer relief valves and reactor coolant pump motor repairs (l) REASON (2) MET 110D A EQUIPMENT I ALLURE (EXPLAIN) 1-MANUAt B - M AINT. OR TEST.

2-MANUAL C-RLI UI LING M R AM D-REGULATORY RES1RICTION 3-AUTOM AllC E-OPFR ATOR lRAINING AND S( R AM LirlNSE EXAMINATION 1'- ADMINISTR AllVE G-OPE R AllON AL I R ROR li.XPL AIN) 11-01111 R IEXPl.AIN)

SUMMARY

.. -. _ _ _ - - _