05000317/LER-1980-019-03, /03L-0:on 800327,during Normal Operation,Channel B Loss of Load Trip Occurred Intermittently.Caused by Auxiliary Master Trip Relay end-of-life Type Failure

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/03L-0:on 800327,during Normal Operation,Channel B Loss of Load Trip Occurred Intermittently.Caused by Auxiliary Master Trip Relay end-of-life Type Failure
ML19309F449
Person / Time
Site: Calvert Cliffs 
Issue date: 04/25/1980
From: Lagiewski J, Rizzo P
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19309F435 List:
References
LER-80-019-03L, LER-80-19-3L, NUDOCS 8004290472
Download: ML19309F449 (2)


LER-1980-019, /03L-0:on 800327,during Normal Operation,Channel B Loss of Load Trip Occurred Intermittently.Caused by Auxiliary Master Trip Relay end-of-life Type Failure
Event date:
Report date:
3171980019R03 - NRC Website

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LICENSEE EVENT REPORT 80 0429 0 Q

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7 8 9 LICENSEE CODE 14 15 LICENSE NUMSER 25 26 LICENSE TYPE JO CON'T 10111 5O,y lL l@l 0! 510 l 0 l 0 ] 311 l 7 l@l 013 l 217 ] 8 l 0 l@l0l4l2l5]8l0]@

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8 60 61 QOCKET NuvaER 6d 69 EVENT CATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CGNSEQUENCES h 10121l At 0910. durino nomal oceration. channal A ina nr 1nna +rin im4t so33 i

LO i a i l bypassed for corrective maintenanco nor T3-111 1 channo1.a in n nf i

1014 l l load trip was returned to service at 1410. At 1040 on 4/1/80 channel B loss I

i O i s i L of load trip unit was again bypassed for additional maintenance.

Channel B l

10 te i i loss of load was returned to service at 1400.

All three redundant channale i

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10171I remained operable throuahout these events. This hac nnt heon a

1 I O is I I occurrence.

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10 11 12 13 13 19 20 SEQUENTI AL OCCUR AENCE REPORT REVISION LER RO EVENTvEAR REPORT NO.

CODE TYPE N O.

O agg 180l 01 l-l 10l1191

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,21 22 23 24 26 27 23 29 30 31 32 T K N A ON ON PLANT E

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J3 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTICN AND CORRECTIVE ACTIONS l i l o t i The cause of the intarmittant inu nfinRd tring,ses dete-ined te be 3 I

til3j l faulty auxiliary master trio relav (General Electric Co. Model CR l'20 HF A7.1 10 ai l

1 within the Main Turbine EHC cabinet. This is considered to be a natural end i

i,,2i l i 131 I of life tvoe of failure due to comoonent ace for the 24 VDC relay. The relay I

ii i4 i i was replaced with a spare.

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% POWER OTH ER STATUS ISCOV Y DISCOVERY DESCRIPTION It IsI[C.j@ l0l9l5l@l NA l

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44 as as 80 8JTiviTY eORTENT AMOUNT OF ACTIVITY @ l LOCATION CF RELEASE li is I W @o On aELEASEW@l REtEASE NA l

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7 8 9 to 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE CESCRIPTION I i I 7 l 1010 10 l@l 2 l@i NA I

8 PE RSONNE'L iN3u'lES oESCRiPTiON@

Nuv8Ea li la l 101010 l@l NA l

7 8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY TYPE DE SCRIPTICN I119I(Z_j@l NA I

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8 9 10 12101 ((L [@ DESCRIPTION ISSUE l

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8 9 10 d. S. LaQiewski/P. G. Rizzo psCns:(3011269 47a7/47A6 2

NAME OF PREPARER l

LER N0.

80-19/3L DOCKET NO.

50-317 i

EVENT DATE 03/37/80 REPORT DATE 04/25/80 ATTACHMENT CAUSE DESCRIPTION AND CORRECTIVE ACT.IdNS:

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No preventive action is deemed necessary.

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