05000321/LER-1980-030-03, /03L-0:on 800330,w/mode Switch in Run Position & Reactor at 2,432 Mwt,Discovered Analyzer B of Primary Containment Hydrogen & Oxygen Analyzer Inoperable.Caused by Personnel Error.Problem Corrected.Analyzer Returned to Svc

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/03L-0:on 800330,w/mode Switch in Run Position & Reactor at 2,432 Mwt,Discovered Analyzer B of Primary Containment Hydrogen & Oxygen Analyzer Inoperable.Caused by Personnel Error.Problem Corrected.Analyzer Returned to Svc
ML19309E618
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 04/17/1980
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19309E598 List:
References
LER-80-030-03L-01, LER-80-30-3L-1, NUDOCS 8004220710
Download: ML19309E618 (2)


LER-1980-030, /03L-0:on 800330,w/mode Switch in Run Position & Reactor at 2,432 Mwt,Discovered Analyzer B of Primary Containment Hydrogen & Oxygen Analyzer Inoperable.Caused by Personnel Error.Problem Corrected.Analyzer Returned to Svc
Event date:
Report date:
3211980030R03 - NRC Website

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60 61 DOC A ET NUVH ER t>d 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2 I With the mode switch in the run oosition and the reactor at 2432 MWt, it I

o 3 l was discovered that the "B" analyzer of the Primary Containment Hydrogen l

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and Oxygen Analyzer was inoperative.

The "A" analyzer was functioning l

l o 151 l properly. This is a repetitive occurrence as last reported on Reportable l

Io is l l Occurrence Report 50-321/1979-097.

There was no effects upon public l

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33 34 36 36 31 40 43 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS IiIo1 I The cause of this occurrence is attributed to personnel error. The sample l

11 liI i pre-filter was incorrectly installed during initial installation and allow-1 i1 I 21 I ed moisture to collect in the sample line.

The problem was corrected and l

l i l 31 I the analyzer returned to service.

The "A" analyzer filter was found cor-l 1 4 l

rectly installed. This problem is not applicable to Unit II.

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REPORT

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Georgia Power Company Plant E. I. Hatch Baxley, Georgia 31513 Reportable Occurrence Report No. 50-321/1980-030.

With the mode switch in run and the reactor at 2432 MWt, it was discovered that the "B" analyzer of the Primary Containment Hydrogen and Oxygen analyzer was inoperative. The "A" analyzer was functioning properly. The failure of the analyzer is repetitive as last reported on Reportable Occurrence Report 50-321/1979-097. However, this is the first failure that can be attributed to the pre-filter installation. There were no effects upon the public health or safety.

The cause of this occurrence is attributed to personnel error.

Upon investi-gation of the problem, moisture was found in the sensing lines.

The. sample pre-filter was found incorrectly installed and it is believed it was installed incorrectly during initial installation and start-up.

The problem was corrected and the analyzer returned to service.,

The "A" analyzer was inspected and it was determinbd that the pre-filter was correctly installed in it. Because the Unit I analyzer is made by Haye and the Unit II analyzer is made by Cumsto-Delphi, this problem is

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not applicable to Unit II.

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