LER-1978-004, /03L-0:on 780108,reactor Coolant Dose Equivalent I-131 Found Contrary to Tech Spec Limitations.Caused by Transient Spikes Following Reactor Trip & Known Leaking Fuel Pins.Corrective Action Unnecessary |
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| 3021978004R03 - NRC Website |
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LICENSEE EVENT REPORT EXHIBIT A J
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E I Coolant Dose Eouivalent I-131 was 1.11 microcuries per tram contrary to the r Lo_14}I14"4tations as set by Tech. Spec. 3.4.8. No safety implicatip.7s. Redundancy i
fo"Til I *f A. ' Third neem venen o f *S f e event as renarted by TM 's 77-67 and 77-91.
i m iThe DE-I131 returned to acceptable lever at 1000 on 8 January 1978.
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SUPPLE 12NTARI INFORMATION eport No.:
50-302/78-04/03L-0 2.
Facility:
Crystal River Unic #3 3.
Raport Date:
31 January 1978 4
Occurrence Date:
8 January 1978 3.
Identification of Occurrence:
The Dose Equivalent I-131 was greater than 1.0 nicrocurie per gram of primary coolant contrary to Technical Specification 3.4.8.
6.
Conditions Prior to Occurrence:
Mode 1 operation.
7.
Description of Occurrence:
At 0600, following a reactor trip and in the process of plant startup, operations was notified by the CHEM / RAD section that the Primary Coolant Dose Equivalent I-131 was 1.11 microcuries per gram. Action scacement 3.4.8.a was entered and the four hour sampling frequency was initiated. The Dose Equivalent I-131 had returned to acceptable technical specification limit of.73 microcuries per gram at the 1000 sampling. The action statement was satisfied and plant operations proceeded uneventful.
.gDesignation of Apparent Cause:
This event was caused by the expected transient spikes following a reactor trip and known leaking fuel pins.
9.
Analysis of Occurrence:
There was no safety hazard to the plant or general public due to this event as sampling demonstrated reducing levels of Dose Equivalent I-131.
10.
Cotractive Action:
Ne corrective action necessary as reactor coolant cleanup returned the Dose Equivalent I-131 to acceptable levels within four hours.
11.
Failure Data:
This is the third occurrence of this event as reported by LER's 77-67 and 77-91.
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REACTOR POWER HISTORY OF PRIOR FORTT-EIGT HOURS ITEM I e
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DATE-1.
4,73 HOUR MWHT NI RATIO (N753)
'(P723)
NI/MT
- ~ ~ *
- /*FP 1:00 100.041 100.700 1.007 2:00 100.122 100.700 1.006
- ~ ~
- 3:00 100.082 100.700 1.006 4:00 100.000 100.600 1.006 5:00 99.878 100.600 1.00<
<6:00 99 873 100.600 1.007 7:00 99.755 100.500 1.007 3:00
- - 99.796 100.400 1.006 9:00 99.633 100.300 1.007 10:00 99.592 100.200 1.004
- ~11:00 99.633 100.300 f.007
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12:00 99.592 100.400 1.008 13:00 99.633 100.300
- 1. 0 0.'
I4: 00 99.592-- -
100.400 1.003
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15:00
! ~. !"5 9F. 6 100.400 1.512 16:00
' d. !"5 99. 6 100.400 1.512
' 17:00
.366
- ~-
13:00 99.470 100.300 1.003 19:00 99.511 100.400 1.009 20:00 99.592 100.500 I.009 21:00 99.796 100.700 1.009 22:00 99.837 100.700 1.009 23:00 99.755 100.500 1.007 24:00 99.551 100.400 1.009 i
AVERAGE. DAILY MWTH POWER 97.640 */*FP 4
- - AVERAGE DAILY NUCLEAE INST. POWER 100.471 */3FP -'
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' - ' RATIO OF NI TO MWHT = 1.029
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.DATE 1,
7,78 7
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HOUR MWHT NI RATIO (N753).
_ */*FP
,NI/MT.
(P723)
. */*FP
1:00 99.592 100.500 1.009 2.:00
__.99.551 __
_.1.C 0 5 0 0 1.010 3:00 99.551 100.500 1.010 0
4:00
.-ess-9ts.sv 10 0. 0 0 0 5 : 0 0__.._9 9. 551... ___. 10 0_, j5 0 0.
...__.1. 010 6:00 99.551 100.600 1.011 O
7:00 99.429, 100.400 1.010 B.LO 0_.. _.9.9_,.10 3 100.100. _.... 1.010...
9:00 98.980 100.000 1.010 0
10:00 99.021 100.000 1.010
.?___. 1 1.:_0 O__ _ 9 9.,.0 2 1...._
10.0_i.0.0.0
_ 1 01_0_
12:00 99.062 100.000 1.009 O
13:00 99.062 100.000 1.009
.._1_4:00
... 99.021
._10.0.000 __
1.0_10 15:00 98.980 100.000 1.010 0
16:00 98.980 100.000 1.010 17:00 99.062 100.100 1.010 18:00 99.103, 100.200 1.011 0
19:00 99.225 100.300 1.011 20:00 99.184 100.300 1.011
_=
21:00 99.134 100.400 1.012 0
22:00 96.336 97.600 1.013
\\23:00 72.471 75.100 1.036 s
24:00 59.625 62.700 1.052 O'
O AVERAGE DAILY MWTH POWER 92.202 */*FP AVERAGE D AILY NUCLEA R INST... POWER
.. ___9.7.J+92._*/ *F_P__.
O RATIO OF NI TO MWHT = 1.057.
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DATE 1.
8,78 0(m'
\\O' HOUR MWHT NI RATIO (N753)
.. ( P.7 2 3 ) _ _ _ _._. N I / M T.___ _.
=/*FP
1:00 58.809 69.400 1.180
.. 2:00
.000.
...0.000
.0.000 3:00
.000 0.000 0.000 O-4:00
.000 0.000 0.000
__ 5:00.__ __.000
.._.0 000._
0 0.0 0.
=_
6:00 10.359 8.800
.850 0
7:00 16.395 16.600 1.013
.S:00_.._20.634
'8.300.._
_. 1 371 9:00 30.914 39.300 1.271 0
10:00 48.940 57.200 1.169
_ _11.:00.
50.000
..._55.700
... _1.114._ -
0_..
12:00 52.610 57.500 1.093 13:00 67.333 71.900 1.068
.__14 : 0 (L.. 6 9. 841
.72.900 1.043 15:00 70.024 73.200 1.045 O
16:00 49.209 72.600 1.049
. 17:00... 88.091
- 90. 200 1.024 f.
18:00 91.028 92.300 1.014 O
19:00 91.150 92.300 1.013 20:00 91.109 92.100 1.011 21:00 89.927 91.200 1.014 22:00 63.214 66.700 1.055 23:00 61.419
. _ _6 5. 0 0 0 ___. _ __ 1. 0 5 8....__.
24:00 61.705 65.200 1.057 O
OI AVERAGE DAILY MWTH POWER 50.114 */*FP
_ AVERAGE._ DAILY NUCLEAR. INS ~f' POWER _. _._53.267__ab RE O' '
. RATIO OF NI TO MWHT = 1.063 O.-
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FUEL BURNUP BY CORE REGION ITEM 2 i
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ITEM 2 i
i the burnup was calculated at 227.1 EFPD for the three enrichment regions.
l REGION NUMBER OF FA BURNLT A
56 0043 mfd /Mr B
61 8166 MID/MT C
60 4457 NHD/Mr AVE.
6870 Mwu/Mr l
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CLEAN-UP FLOW HISTolti ITEM 3 r
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e ITEM 3 DATE TIME DEMIN IN SERVICE LETDOWN FLOW uci/ GRAM i
8 Jm. 78 0600 B
100 GPM 1.1 8 Jm. 78 1000 B
100 GPM
.73 8 Jm. 78 1435 B
100 GPM
.51 4
8 Jm. 78 1950 3
100 GPM
.28 9 Jm. 78 0130 B
100 GPM
.35
- i 9 Jm. 78 0615 3
100 GPM
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l NO HISTORY OF DECASSING OPERATIONS FOR THIS REPORT ITEM 4 i
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1 TDE DURATION WHEN DEI-131 EXC2DED 1.0 uci/ CRAM AND I-131 ANALYSIS Rt.SULTS I
ITEM 5
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e As per Technical Specification 3.4.8:
i The 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> sampling frequency was initiated at 0600 on 8 January 1978 and the dose aquivelant I-131 was 1.11 microcuries per gram. The 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> sampling frequency was terminated at 1000 when the DEI-131 was determined to be.73 microcuries per gram.
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| 05000302/LER-1978-001, Forwards LER 78-001/03L-0 | Forwards LER 78-001/03L-0 | | | 05000302/LER-1978-001-03, /03L-0:on 780103,3B Emergency Diesel Failed to Start During Maint on 3A Emergency Diesel Generator.Caused by Foreign Matter in Servo Booster Preventing Governor to Function Properly.Servo Booster Cleaned & Tested | /03L-0:on 780103,3B Emergency Diesel Failed to Start During Maint on 3A Emergency Diesel Generator.Caused by Foreign Matter in Servo Booster Preventing Governor to Function Properly.Servo Booster Cleaned & Tested | | | 05000302/LER-1978-001-04, /04X-0:on 780112-13,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 50 kg/24-h ETS Levels. Partially Caused by Coal Barges Entering & Maneuvering in Intake Canal During Sampling | /04X-0:on 780112-13,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 50 kg/24-h ETS Levels. Partially Caused by Coal Barges Entering & Maneuvering in Intake Canal During Sampling | | | 05000302/LER-1978-002-03, /03L-0:on 780104,one Cable Tunnel Sump Pump Failed to Start During Operability Verification.Caused by Packaged Sump Pump Electric Motor Portion Failure.Pump Replaced | /03L-0:on 780104,one Cable Tunnel Sump Pump Failed to Start During Operability Verification.Caused by Packaged Sump Pump Electric Motor Portion Failure.Pump Replaced | | | 05000302/LER-1978-002, Forwards LER 78-002/03L-0 | Forwards LER 78-002/03L-0 | | | 05000302/LER-1978-002-04, /04X-0:on 780103-04,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 50 kg/24-h ETS Levels. Partially Caused by Oil Barge Entering Intake Canal During Sampling | /04X-0:on 780103-04,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 50 kg/24-h ETS Levels. Partially Caused by Oil Barge Entering Intake Canal During Sampling | | | 05000302/LER-1978-003-03, /03L-O:on 780104,Unit 2 Battery Failed to Meet Quarterly Battery Test SP-511 Criteria.Caused by Electrolyte Stratification Due to Battery No Lead Condition.Request for Engineering Info Initiated to Evaluate & Recommend Solut | /03L-O:on 780104,Unit 2 Battery Failed to Meet Quarterly Battery Test SP-511 Criteria.Caused by Electrolyte Stratification Due to Battery No Lead Condition.Request for Engineering Info Initiated to Evaluate & Recommend Solution | | | 05000302/LER-1978-003, Forwards LER 78-003/03L-0 | Forwards LER 78-003/03L-0 | | | 05000302/LER-1978-003-04, /04X-0:on 780119-20,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding ETS Levels.Cause Undetermined | /04X-0:on 780119-20,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding ETS Levels.Cause Undetermined | | | 05000302/LER-1978-004-04, /04X-0:on 780201,unplanned Radioactive Gas Release Occurred During Maint on Nitrogen Sys Header.Caused by Leaking MUV-141F & MUV-140 Makeup Tank Valves.Revisions Initiated to Consider Interconnecting Sys Impact | /04X-0:on 780201,unplanned Radioactive Gas Release Occurred During Maint on Nitrogen Sys Header.Caused by Leaking MUV-141F & MUV-140 Makeup Tank Valves.Revisions Initiated to Consider Interconnecting Sys Impact | | | 05000302/LER-1978-004, Forwards Supplemental Info to LER 78-004/04X-0 Re Unplanned Radioactive Gas Release During Maint.Personnel Associated W/Incident & Gaseous Pipe Contents List Encl.List Withheld Per Privacy Act | Forwards Supplemental Info to LER 78-004/04X-0 Re Unplanned Radioactive Gas Release During Maint.Personnel Associated W/Incident & Gaseous Pipe Contents List Encl.List Withheld Per Privacy Act | | | 05000302/LER-1978-004-03, /03L-0:on 780108,reactor Coolant Dose Equivalent I-131 Found Contrary to Tech Spec Limitations.Caused by Transient Spikes Following Reactor Trip & Known Leaking Fuel Pins.Corrective Action Unnecessary | /03L-0:on 780108,reactor Coolant Dose Equivalent I-131 Found Contrary to Tech Spec Limitations.Caused by Transient Spikes Following Reactor Trip & Known Leaking Fuel Pins.Corrective Action Unnecessary | | | 05000302/LER-1978-005-04, /04X-0:on 780127-28,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 51 kg/24-h Tech Spec Level.Partially Caused by Coal Barges Exciting Intake Canal During Sampling Period | /04X-0:on 780127-28,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 51 kg/24-h Tech Spec Level.Partially Caused by Coal Barges Exciting Intake Canal During Sampling Period | | | 05000302/LER-1978-005-03, /03L-0:on 780109,one Sump Pump Failed to Start During Cable Tunnel Sump Pump Operability Test SP-322 Performance.Caused by Failure of Start Control Bulb Switch Due to Inadequate Current Capacity | /03L-0:on 780109,one Sump Pump Failed to Start During Cable Tunnel Sump Pump Operability Test SP-322 Performance.Caused by Failure of Start Control Bulb Switch Due to Inadequate Current Capacity | | | 05000302/LER-1978-005, Forwards LER 78-005/03L-0 | Forwards LER 78-005/03L-0 | | | 05000302/LER-1978-006, Responds to NRC Re Violation Noted in IE Insp Rept 50-302/78-02.Corrective Actions:Problems Re Clearances Not Being Issued,Placed on Equipment or Released Per CP-115 Corrected.One Case Reported in LER 78-006/03L-0 | Responds to NRC Re Violation Noted in IE Insp Rept 50-302/78-02.Corrective Actions:Problems Re Clearances Not Being Issued,Placed on Equipment or Released Per CP-115 Corrected.One Case Reported in LER 78-006/03L-0 | | | 05000302/LER-1978-006-03, /03L-0:on 780111,HPI Isolation Valve MUV-25 Breaker Inadvertantly Opened & Red Tagged Out of Svc During Normal Mode 1 Operations.Clearance Procedure Reviewed W/Personnel | /03L-0:on 780111,HPI Isolation Valve MUV-25 Breaker Inadvertantly Opened & Red Tagged Out of Svc During Normal Mode 1 Operations.Clearance Procedure Reviewed W/Personnel | | | 05000302/LER-1978-006-04, /04X-0:on 780206-07,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2 & 3 Exceeded 50 Kg Per 24-h Reporting Level.Cause Unknown | /04X-0:on 780206-07,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2 & 3 Exceeded 50 Kg Per 24-h Reporting Level.Cause Unknown | | | 05000302/LER-1978-007-01, /01T-2:on 780204,valve Operator FWV-15 Not Changed as Required by Upgrading of Steam Line Rupture Matrix.Caused by Lack of Appropriate Engineering Change Notice.Mod Package Completed.(Supplementary Info Sheet Only.) | /01T-2:on 780204,valve Operator FWV-15 Not Changed as Required by Upgrading of Steam Line Rupture Matrix.Caused by Lack of Appropriate Engineering Change Notice.Mod Package Completed.(Supplementary Info Sheet Only.) | | | 05000302/LER-1978-007, Forwards Revision 2 to LER 78-007/01T-0,consisting of Supplementary Info | Forwards Revision 2 to LER 78-007/01T-0,consisting of Supplementary Info | | | 05000302/LER-1978-007-04, /04X-0:on 780216 & 17,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2 & 3 Exceeded 50 Kg Per 24-h Reporting Level.Coal Barge Exiting Intake Canal During Sampling May Have Been Partial Cause | /04X-0:on 780216 & 17,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2 & 3 Exceeded 50 Kg Per 24-h Reporting Level.Coal Barge Exiting Intake Canal During Sampling May Have Been Partial Cause | | | 05000302/LER-1978-008, Forwards LER 78-008/03L-0 | Forwards LER 78-008/03L-0 | | | 05000302/LER-1978-008-04, /04T-0:on 780305,waste Gas Header Overpressurized & Blew Auxiliary Bldg Loop Seals During RCS Degassing. Caused by Personnel Error.Personnel & Supervisors Instructed | /04T-0:on 780305,waste Gas Header Overpressurized & Blew Auxiliary Bldg Loop Seals During RCS Degassing. Caused by Personnel Error.Personnel & Supervisors Instructed | | | 05000302/LER-1978-008-03, /03L-0:on 780122 During Sampling,Reactor Coolant Dose Equivalent I-131 Found to Be 1.42 Uci Per Gram.Caused by Transient Spikes Following Trip & Leaking Fuel Pins.No Action Needed | /03L-0:on 780122 During Sampling,Reactor Coolant Dose Equivalent I-131 Found to Be 1.42 Uci Per Gram.Caused by Transient Spikes Following Trip & Leaking Fuel Pins.No Action Needed | | | 05000302/LER-1978-009-03, /03L-0:on 780122 Control Rod Driveline Breaker a Failed to Trip During Reactor Protection Sys Functional Test SP-110.Caused by Undercurrent Relay Failure.Breaker Replaced | /03L-0:on 780122 Control Rod Driveline Breaker a Failed to Trip During Reactor Protection Sys Functional Test SP-110.Caused by Undercurrent Relay Failure.Breaker Replaced | | | 05000302/LER-1978-009-04, /04X-0:on 780223-24,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 50 kg/24-h Reporting Level of Ets.Caused by Two Coal Barges Exiting & Coal Barge Entering Intake Canal During Sampling | /04X-0:on 780223-24,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 50 kg/24-h Reporting Level of Ets.Caused by Two Coal Barges Exiting & Coal Barge Entering Intake Canal During Sampling | | | 05000302/LER-1978-009, Forwards LER 78-009/04x-0 | Forwards LER 78-009/04x-0 | | | 05000302/LER-1978-010-03, /03L-0:on 780123,security Alarm Sounded an Unauthorized Entry Into Vital Area Through Unlocked Door. Locking Devices on Vital Area Doors Altered.Key Now Needed for Outside Opening.Doors Cannot Be Left Unlocked | /03L-0:on 780123,security Alarm Sounded an Unauthorized Entry Into Vital Area Through Unlocked Door. Locking Devices on Vital Area Doors Altered.Key Now Needed for Outside Opening.Doors Cannot Be Left Unlocked | | | 05000302/LER-1978-010-04, /04X-0:on 780307-08,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2 & 3 Exceeded 50 Kg Per 24-h Reporting Level.Oil Barge Entering Intake Canal During Sampling Period May Have Been Cause | /04X-0:on 780307-08,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2 & 3 Exceeded 50 Kg Per 24-h Reporting Level.Oil Barge Entering Intake Canal During Sampling Period May Have Been Cause | | | 05000302/LER-1978-010, Forwards LER 78-010/03L-0 | Forwards LER 78-010/03L-0 | | | 05000302/LER-1978-011-04, /04X:on 780303-04,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2, & 3 Exceeded 50 Kg Per 24-h Reporting Level.Cause Undetermined | /04X:on 780303-04,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2, & 3 Exceeded 50 Kg Per 24-h Reporting Level.Cause Undetermined | | | 05000302/LER-1978-011, Forwards LER 78-011/03L-0 | Forwards LER 78-011/03L-0 | | | 05000302/LER-1978-011-03, /03L-0:on 780201,during Mode 3 Operation,Primary Containment Integrity Not Maintained When Nitrogen Valve NGV-81 Open for 3-h 42 Minutes.Caused by Oversight of Tech Spec 3.6.1 1 Requirements.Personnel Instructed | /03L-0:on 780201,during Mode 3 Operation,Primary Containment Integrity Not Maintained When Nitrogen Valve NGV-81 Open for 3-h 42 Minutes.Caused by Oversight of Tech Spec 3.6.1 1 Requirements.Personnel Instructed | | | 05000302/LER-1978-012, Forwards LER 78-012/03L-0 | Forwards LER 78-012/03L-0 | | | 05000302/LER-1978-012-03, /03L-0:on 780203,steamline Rupture Matrix Actuated During Heatup & Before Entry Into Operational Mode 2.Caused by Dead Band Shift of 600 Psig Pressure Switches MS-94,95- PS2.Switches Recalibr & Manual Bypass to Be Installed | /03L-0:on 780203,steamline Rupture Matrix Actuated During Heatup & Before Entry Into Operational Mode 2.Caused by Dead Band Shift of 600 Psig Pressure Switches MS-94,95- PS2.Switches Recalibr & Manual Bypass to Be Installed | | | 05000302/LER-1978-012-04, /04X-0:on 780101-0331,improper Procedures Used in Environ Sample Analyses.Procedures Revised & More Efficient Counting Configurations & Overnight Count Times Being Tested.(Supplementary Info Sheet Only.) | /04X-0:on 780101-0331,improper Procedures Used in Environ Sample Analyses.Procedures Revised & More Efficient Counting Configurations & Overnight Count Times Being Tested.(Supplementary Info Sheet Only.) | | | 05000302/LER-1978-013-03, /03L-0:on 780208,A & B Boric Acid Storage Tanks Found Inoperable While Performing Operability Check of Boron Injection Sources.Caused by Failure to Follow Procedures. Operators Instructed | /03L-0:on 780208,A & B Boric Acid Storage Tanks Found Inoperable While Performing Operability Check of Boron Injection Sources.Caused by Failure to Follow Procedures. Operators Instructed | | | 05000302/LER-1978-013-04, /04X-0:June 1977-Mar 1978 Contractor Environ Sample Analyses Used Incorrect Procedures.Possibly Caused by Insufficient Sample Size & Count Times.Count Times Being Tested.(Supplementary Info Sheet Only.) | /04X-0:June 1977-Mar 1978 Contractor Environ Sample Analyses Used Incorrect Procedures.Possibly Caused by Insufficient Sample Size & Count Times.Count Times Being Tested.(Supplementary Info Sheet Only.) | | | 05000302/LER-1978-013, Forwards LER 78-013/03L-0 | Forwards LER 78-013/03L-0 | | | 05000302/LER-1978-014-04, /04X-0:on 780101-0502,environ Samples Not Analyzed W/Procedures Providing LLDs Equal to or Less than ETS Requirements.Caused by Inadequate Techniques &/Or Equipment. Normal Samples Taken.(Supplementary Info Sheet Only.) | /04X-0:on 780101-0502,environ Samples Not Analyzed W/Procedures Providing LLDs Equal to or Less than ETS Requirements.Caused by Inadequate Techniques &/Or Equipment. Normal Samples Taken.(Supplementary Info Sheet Only.) | | | 05000302/LER-1978-014-03, /03L-0:on 780210,chemical Addition Valves CAV 1 & 2 Failed to Close on Completion of Pressurizer Steam Space Sampling.Caused by Incorrect Torque Switch Setting of Valve CAV-1.Operability restored.CAV-2 Corrective Action Pend | /03L-0:on 780210,chemical Addition Valves CAV 1 & 2 Failed to Close on Completion of Pressurizer Steam Space Sampling.Caused by Incorrect Torque Switch Setting of Valve CAV-1.Operability restored.CAV-2 Corrective Action Pending | | | 05000302/LER-1978-014, Forwards LER 78-014/03L-0 | Forwards LER 78-014/03L-0 | | | 05000302/LER-1978-015-04, /04T-0:on 780511,20 Uci Radioactive Liquid Released During Spent Resin Transfer to Vendor Vehicle. Caused by Line Rupture.Transfer Terminated & Radioactive Protection Measures Implemented.Corrective Action Pending | /04T-0:on 780511,20 Uci Radioactive Liquid Released During Spent Resin Transfer to Vendor Vehicle. Caused by Line Rupture.Transfer Terminated & Radioactive Protection Measures Implemented.Corrective Action Pending | | | 05000302/LER-1978-015-03, /03L-0:on 780215,during Reactor Trip Chemical/ Radiation Sampling Revealed Reactor Coolant Dose Equivalent Exceeded Limits.Caused by Expected Transient Spikes Following Trip & Leaking Fuel Pins.No Action Needed | /03L-0:on 780215,during Reactor Trip Chemical/ Radiation Sampling Revealed Reactor Coolant Dose Equivalent Exceeded Limits.Caused by Expected Transient Spikes Following Trip & Leaking Fuel Pins.No Action Needed | | | 05000302/LER-1978-015, Forwards LER 78-015/04T-1.LER 78-015/04T-0 Encl | Forwards LER 78-015/04T-1.LER 78-015/04T-0 Encl | | | 05000302/LER-1978-016, Forwards LER 78-016/01T-0 | Forwards LER 78-016/01T-0 | | | 05000302/LER-1978-016-01, /01T-0:on 780310,in Mode 5 Operation,Unplanned Reactivity Insertion of 4.3% of Delta K/K.Caused by Dilution of RCS Upon Draining.Rcs Boron Sampling Surveillance Increased | /01T-0:on 780310,in Mode 5 Operation,Unplanned Reactivity Insertion of 4.3% of Delta K/K.Caused by Dilution of RCS Upon Draining.Rcs Boron Sampling Surveillance Increased | | | 05000302/LER-1978-016-04, /04L-0 (Supplementary Info Sheet):On 780404, Sample Not Obtained from Test Well 5 for Months of Apr & May.Caused by Well Being Inadvertently Covered by Const Debris.Well to Be Available for June Sampling | /04L-0 (Supplementary Info Sheet):On 780404, Sample Not Obtained from Test Well 5 for Months of Apr & May.Caused by Well Being Inadvertently Covered by Const Debris.Well to Be Available for June Sampling | | | 05000302/LER-1978-017-01, /01T-0:on 780306,17 Loose Parts Identified as Coupling & Spider Assembly of BPR- B-47,discovered in B once-through Steam Generator.Caused by Assembly Failure. Corrective Action to Be Determined | /01T-0:on 780306,17 Loose Parts Identified as Coupling & Spider Assembly of BPR- B-47,discovered in B once-through Steam Generator.Caused by Assembly Failure. Corrective Action to Be Determined | | | 05000302/LER-1978-017, Forwards LER 78-017/01T-0 | Forwards LER 78-017/01T-0 | |
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