LER-1978-031, /01T-0:on 780609,while Moving New Fuel Elevator Test Weight in Spent Fuel Pool with Missile Shield Crane FHCR-7,crane Hook Failed & Dropped Weight.Caused by Personnel Error in Selecting Hook.Procedures to Be Changed |
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EVENT DE5 Cit piton ANu esteHAHi.E i;ONSEQUENCES bo FT] l At 1450, while moving the new ruel elevator test weight in the spent
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i (y_1f)i hook failed d_ropping the test weight.
The uuger.*nd came to rest againsti to is t t an APSR couclino device in fuel assembly A 48.
This event is recorted I
lole>lI in accordance with STS 6.9.1 R.i.
No annar9nt material damage was initiallly note %
io i,i i Redundancy N/A.
No safety hazard.
First occurrence.
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4 CAUSE DESCAIPTION AND COHRECrIVE ACrIONS h o
Cause of this event has been determined to be lack of conservatism in i, n, i i i
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Revisions to orocedurp.:
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Disciolinary acti>'n has been recommended.
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SUPPLEMENTARY INFORMATION i
V Report No.:
50-302/78-031/01T-0 Facility:
Crystal River Unit #3 Report Date:
21 June 1978 Occurrence Date:
9 June 1978 Identification of Occurrence:
Drop of new fuel elevator test weight on fuel assembly A-48 and reported in accognce with Technical Specification 6.9.1.8.i.
Conditions Prior to Occurrence:
Mode 6 refueling.
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Description of Occurrence:
At 1450 hours0.0168 days <br />0.403 hours <br />0.0024 weeks <br />5.51725e-4 months <br />, while lifting the new fuel elevator test weight
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(2050 lbs.) from "Y" up-ender to an empty fuel storage rack with the missile shield crane (FHCR-7) a plant fabricated rigging hook failed, dropping the test weight.
The bottom weighted end of the test weight struck an edge of an empty fuel rack and fell over to its side and the top came to rest against an APSR coupling device v
in fuel assembly A-48.
Initial fuel assembly damage assessment failed to reveal any material damage to the struck fuel assembly.
Subsequent inspections of assembly A-48 have revealed that some deformation has occurred.
It has been decided that this assembly will not be utilized in the reactor in its current state and will be replaced.
The test load was removed and stored in the spent fuel area.
Designation of Apparent Cause:
The cause of this occurrence was due to the lack of conserv'atism in personnel judgment of lifting hook selection.
Analysis of Occurrence:
There was no safety hazard to the plant or general public in that immediate sampling of the spent fuel pit water and airborne activity revealed no change from previous condition.
Subsequent periodic sampling affirmed no change in water or airborne ~ activity.
Corrective Action
A review of procedures controlling load testing and identification of all lifting devices has been completed.
Revisions to these procedures will be initiated to assure proper identification and load capabilities of all such lifting devices.
All use of crane hooks, chokers, slings, and shackles performing safety related work will be procedurally controlled.
Disciplinary action has been recommeded.
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Suppicmentary Information (cont'd) i Failure Data:
This is the first occurrence of an event of this type.
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| 05000302/LER-1978-001, Forwards LER 78-001/03L-0 | Forwards LER 78-001/03L-0 | | | 05000302/LER-1978-001-03, /03L-0:on 780103,3B Emergency Diesel Failed to Start During Maint on 3A Emergency Diesel Generator.Caused by Foreign Matter in Servo Booster Preventing Governor to Function Properly.Servo Booster Cleaned & Tested | /03L-0:on 780103,3B Emergency Diesel Failed to Start During Maint on 3A Emergency Diesel Generator.Caused by Foreign Matter in Servo Booster Preventing Governor to Function Properly.Servo Booster Cleaned & Tested | | | 05000302/LER-1978-001-04, /04X-0:on 780112-13,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 50 kg/24-h ETS Levels. Partially Caused by Coal Barges Entering & Maneuvering in Intake Canal During Sampling | /04X-0:on 780112-13,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 50 kg/24-h ETS Levels. 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Maint on Nitrogen Sys Header.Caused by Leaking MUV-141F & MUV-140 Makeup Tank Valves.Revisions Initiated to Consider Interconnecting Sys Impact | /04X-0:on 780201,unplanned Radioactive Gas Release Occurred During Maint on Nitrogen Sys Header.Caused by Leaking MUV-141F & MUV-140 Makeup Tank Valves.Revisions Initiated to Consider Interconnecting Sys Impact | | | 05000302/LER-1978-004, Forwards Supplemental Info to LER 78-004/04X-0 Re Unplanned Radioactive Gas Release During Maint.Personnel Associated W/Incident & Gaseous Pipe Contents List Encl.List Withheld Per Privacy Act | Forwards Supplemental Info to LER 78-004/04X-0 Re Unplanned Radioactive Gas Release During Maint.Personnel Associated W/Incident & Gaseous Pipe Contents List Encl.List Withheld Per Privacy Act | | | 05000302/LER-1978-004-03, /03L-0:on 780108,reactor Coolant Dose Equivalent I-131 Found Contrary to Tech Spec Limitations.Caused by Transient Spikes Following Reactor Trip & Known Leaking Fuel Pins.Corrective Action Unnecessary | /03L-0:on 780108,reactor Coolant Dose Equivalent I-131 Found Contrary to Tech Spec Limitations.Caused by Transient Spikes Following Reactor Trip & Known Leaking Fuel Pins.Corrective Action Unnecessary | | | 05000302/LER-1978-005-04, /04X-0:on 780127-28,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 51 kg/24-h Tech Spec Level.Partially Caused by Coal Barges Exciting Intake Canal During Sampling Period | /04X-0:on 780127-28,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 51 kg/24-h Tech Spec Level.Partially Caused by Coal Barges Exciting Intake Canal During Sampling Period | | | 05000302/LER-1978-005-03, /03L-0:on 780109,one Sump Pump Failed to Start During Cable Tunnel Sump Pump Operability Test SP-322 Performance.Caused by Failure of Start Control Bulb Switch Due to Inadequate Current Capacity | /03L-0:on 780109,one Sump Pump Failed to Start During Cable Tunnel Sump Pump Operability Test SP-322 Performance.Caused by Failure of Start Control Bulb Switch Due to Inadequate Current Capacity | | | 05000302/LER-1978-005, Forwards LER 78-005/03L-0 | Forwards LER 78-005/03L-0 | | | 05000302/LER-1978-006, Responds to NRC Re Violation Noted in IE Insp Rept 50-302/78-02.Corrective Actions:Problems Re Clearances Not Being Issued,Placed on Equipment or Released Per CP-115 Corrected.One Case Reported in LER 78-006/03L-0 | Responds to NRC Re Violation Noted in IE Insp Rept 50-302/78-02.Corrective Actions:Problems Re Clearances Not Being Issued,Placed on Equipment or Released Per CP-115 Corrected.One Case Reported in LER 78-006/03L-0 | | | 05000302/LER-1978-006-03, /03L-0:on 780111,HPI Isolation Valve MUV-25 Breaker Inadvertantly Opened & Red Tagged Out of Svc During Normal Mode 1 Operations.Clearance Procedure Reviewed W/Personnel | /03L-0:on 780111,HPI Isolation Valve MUV-25 Breaker Inadvertantly Opened & Red Tagged Out of Svc During Normal Mode 1 Operations.Clearance Procedure Reviewed W/Personnel | | | 05000302/LER-1978-006-04, /04X-0:on 780206-07,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2 & 3 Exceeded 50 Kg Per 24-h Reporting Level.Cause Unknown | /04X-0:on 780206-07,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2 & 3 Exceeded 50 Kg Per 24-h Reporting Level.Cause Unknown | | | 05000302/LER-1978-007-01, /01T-2:on 780204,valve Operator FWV-15 Not Changed as Required by Upgrading of Steam Line Rupture Matrix.Caused by Lack of Appropriate Engineering Change Notice.Mod Package Completed.(Supplementary Info Sheet Only.) | /01T-2:on 780204,valve Operator FWV-15 Not Changed as Required by Upgrading of Steam Line Rupture Matrix.Caused by Lack of Appropriate Engineering Change Notice.Mod Package Completed.(Supplementary Info Sheet Only.) | | | 05000302/LER-1978-007, Forwards Revision 2 to LER 78-007/01T-0,consisting of Supplementary Info | Forwards Revision 2 to LER 78-007/01T-0,consisting of Supplementary Info | | | 05000302/LER-1978-007-04, /04X-0:on 780216 & 17,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2 & 3 Exceeded 50 Kg Per 24-h Reporting Level.Coal Barge Exiting Intake Canal During Sampling May Have Been Partial Cause | /04X-0:on 780216 & 17,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2 & 3 Exceeded 50 Kg Per 24-h Reporting Level.Coal Barge Exiting Intake Canal During Sampling May Have Been Partial Cause | | | 05000302/LER-1978-008, Forwards LER 78-008/03L-0 | Forwards LER 78-008/03L-0 | | | 05000302/LER-1978-008-04, /04T-0:on 780305,waste Gas Header Overpressurized & Blew Auxiliary Bldg Loop Seals During RCS Degassing. Caused by Personnel Error.Personnel & Supervisors Instructed | /04T-0:on 780305,waste Gas Header Overpressurized & Blew Auxiliary Bldg Loop Seals During RCS Degassing. Caused by Personnel Error.Personnel & Supervisors Instructed | | | 05000302/LER-1978-008-03, /03L-0:on 780122 During Sampling,Reactor Coolant Dose Equivalent I-131 Found to Be 1.42 Uci Per Gram.Caused by Transient Spikes Following Trip & Leaking Fuel Pins.No Action Needed | /03L-0:on 780122 During Sampling,Reactor Coolant Dose Equivalent I-131 Found to Be 1.42 Uci Per Gram.Caused by Transient Spikes Following Trip & Leaking Fuel Pins.No Action Needed | | | 05000302/LER-1978-009-03, /03L-0:on 780122 Control Rod Driveline Breaker a Failed to Trip During Reactor Protection Sys Functional Test SP-110.Caused by Undercurrent Relay Failure.Breaker Replaced | /03L-0:on 780122 Control Rod Driveline Breaker a Failed to Trip During Reactor Protection Sys Functional Test SP-110.Caused by Undercurrent Relay Failure.Breaker Replaced | | | 05000302/LER-1978-009-04, /04X-0:on 780223-24,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 50 kg/24-h Reporting Level of Ets.Caused by Two Coal Barges Exiting & Coal Barge Entering Intake Canal During Sampling | /04X-0:on 780223-24,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 50 kg/24-h Reporting Level of Ets.Caused by Two Coal Barges Exiting & Coal Barge Entering Intake Canal During Sampling | | | 05000302/LER-1978-009, Forwards LER 78-009/04x-0 | Forwards LER 78-009/04x-0 | | | 05000302/LER-1978-010-03, /03L-0:on 780123,security Alarm Sounded an Unauthorized Entry Into Vital Area Through Unlocked Door. Locking Devices on Vital Area Doors Altered.Key Now Needed for Outside Opening.Doors Cannot Be Left Unlocked | /03L-0:on 780123,security Alarm Sounded an Unauthorized Entry Into Vital Area Through Unlocked Door. Locking Devices on Vital Area Doors Altered.Key Now Needed for Outside Opening.Doors Cannot Be Left Unlocked | | | 05000302/LER-1978-010-04, /04X-0:on 780307-08,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2 & 3 Exceeded 50 Kg Per 24-h Reporting Level.Oil Barge Entering Intake Canal During Sampling Period May Have Been Cause | /04X-0:on 780307-08,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2 & 3 Exceeded 50 Kg Per 24-h Reporting Level.Oil Barge Entering Intake Canal During Sampling Period May Have Been Cause | | | 05000302/LER-1978-010, Forwards LER 78-010/03L-0 | Forwards LER 78-010/03L-0 | | | 05000302/LER-1978-011-04, /04X:on 780303-04,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2, & 3 Exceeded 50 Kg Per 24-h Reporting Level.Cause Undetermined | /04X:on 780303-04,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2, & 3 Exceeded 50 Kg Per 24-h Reporting Level.Cause Undetermined | | | 05000302/LER-1978-011, Forwards LER 78-011/03L-0 | Forwards LER 78-011/03L-0 | | | 05000302/LER-1978-011-03, /03L-0:on 780201,during Mode 3 Operation,Primary Containment Integrity Not Maintained When Nitrogen Valve NGV-81 Open for 3-h 42 Minutes.Caused by Oversight of Tech Spec 3.6.1 1 Requirements.Personnel Instructed | /03L-0:on 780201,during Mode 3 Operation,Primary Containment Integrity Not Maintained When Nitrogen Valve NGV-81 Open for 3-h 42 Minutes.Caused by Oversight of Tech Spec 3.6.1 1 Requirements.Personnel Instructed | | | 05000302/LER-1978-012, Forwards LER 78-012/03L-0 | Forwards LER 78-012/03L-0 | | | 05000302/LER-1978-012-03, /03L-0:on 780203,steamline Rupture Matrix Actuated During Heatup & Before Entry Into Operational Mode 2.Caused by Dead Band Shift of 600 Psig Pressure Switches MS-94,95- PS2.Switches Recalibr & Manual Bypass to Be Installed | /03L-0:on 780203,steamline Rupture Matrix Actuated During Heatup & Before Entry Into Operational Mode 2.Caused by Dead Band Shift of 600 Psig Pressure Switches MS-94,95- PS2.Switches Recalibr & Manual Bypass to Be Installed | | | 05000302/LER-1978-012-04, /04X-0:on 780101-0331,improper Procedures Used in Environ Sample Analyses.Procedures Revised & More Efficient Counting Configurations & Overnight Count Times Being Tested.(Supplementary Info Sheet Only.) | /04X-0:on 780101-0331,improper Procedures Used in Environ Sample Analyses.Procedures Revised & More Efficient Counting Configurations & Overnight Count Times Being Tested.(Supplementary Info Sheet Only.) | | | 05000302/LER-1978-013-03, /03L-0:on 780208,A & B Boric Acid Storage Tanks Found Inoperable While Performing Operability Check of Boron Injection Sources.Caused by Failure to Follow Procedures. Operators Instructed | /03L-0:on 780208,A & B Boric Acid Storage Tanks Found Inoperable While Performing Operability Check of Boron Injection Sources.Caused by Failure to Follow Procedures. Operators Instructed | | | 05000302/LER-1978-013-04, /04X-0:June 1977-Mar 1978 Contractor Environ Sample Analyses Used Incorrect Procedures.Possibly Caused by Insufficient Sample Size & Count Times.Count Times Being Tested.(Supplementary Info Sheet Only.) | /04X-0:June 1977-Mar 1978 Contractor Environ Sample Analyses Used Incorrect Procedures.Possibly Caused by Insufficient Sample Size & Count Times.Count Times Being Tested.(Supplementary Info Sheet Only.) | | | 05000302/LER-1978-013, Forwards LER 78-013/03L-0 | Forwards LER 78-013/03L-0 | | | 05000302/LER-1978-014-04, /04X-0:on 780101-0502,environ Samples Not Analyzed W/Procedures Providing LLDs Equal to or Less than ETS Requirements.Caused by Inadequate Techniques &/Or Equipment. Normal Samples Taken.(Supplementary Info Sheet Only.) | /04X-0:on 780101-0502,environ Samples Not Analyzed W/Procedures Providing LLDs Equal to or Less than ETS Requirements.Caused by Inadequate Techniques &/Or Equipment. Normal Samples Taken.(Supplementary Info Sheet Only.) | | | 05000302/LER-1978-014-03, /03L-0:on 780210,chemical Addition Valves CAV 1 & 2 Failed to Close on Completion of Pressurizer Steam Space Sampling.Caused by Incorrect Torque Switch Setting of Valve CAV-1.Operability restored.CAV-2 Corrective Action Pend | /03L-0:on 780210,chemical Addition Valves CAV 1 & 2 Failed to Close on Completion of Pressurizer Steam Space Sampling.Caused by Incorrect Torque Switch Setting of Valve CAV-1.Operability restored.CAV-2 Corrective Action Pending | | | 05000302/LER-1978-014, Forwards LER 78-014/03L-0 | Forwards LER 78-014/03L-0 | | | 05000302/LER-1978-015-04, /04T-0:on 780511,20 Uci Radioactive Liquid Released During Spent Resin Transfer to Vendor Vehicle. Caused by Line Rupture.Transfer Terminated & Radioactive Protection Measures Implemented.Corrective Action Pending | /04T-0:on 780511,20 Uci Radioactive Liquid Released During Spent Resin Transfer to Vendor Vehicle. Caused by Line Rupture.Transfer Terminated & Radioactive Protection Measures Implemented.Corrective Action Pending | | | 05000302/LER-1978-015-03, /03L-0:on 780215,during Reactor Trip Chemical/ Radiation Sampling Revealed Reactor Coolant Dose Equivalent Exceeded Limits.Caused by Expected Transient Spikes Following Trip & Leaking Fuel Pins.No Action Needed | /03L-0:on 780215,during Reactor Trip Chemical/ Radiation Sampling Revealed Reactor Coolant Dose Equivalent Exceeded Limits.Caused by Expected Transient Spikes Following Trip & Leaking Fuel Pins.No Action Needed | | | 05000302/LER-1978-015, Forwards LER 78-015/04T-1.LER 78-015/04T-0 Encl | Forwards LER 78-015/04T-1.LER 78-015/04T-0 Encl | | | 05000302/LER-1978-016, Forwards LER 78-016/01T-0 | Forwards LER 78-016/01T-0 | | | 05000302/LER-1978-016-01, /01T-0:on 780310,in Mode 5 Operation,Unplanned Reactivity Insertion of 4.3% of Delta K/K.Caused by Dilution of RCS Upon Draining.Rcs Boron Sampling Surveillance Increased | /01T-0:on 780310,in Mode 5 Operation,Unplanned Reactivity Insertion of 4.3% of Delta K/K.Caused by Dilution of RCS Upon Draining.Rcs Boron Sampling Surveillance Increased | | | 05000302/LER-1978-016-04, /04L-0 (Supplementary Info Sheet):On 780404, Sample Not Obtained from Test Well 5 for Months of Apr & May.Caused by Well Being Inadvertently Covered by Const Debris.Well to Be Available for June Sampling | /04L-0 (Supplementary Info Sheet):On 780404, Sample Not Obtained from Test Well 5 for Months of Apr & May.Caused by Well Being Inadvertently Covered by Const Debris.Well to Be Available for June Sampling | | | 05000302/LER-1978-017-01, /01T-0:on 780306,17 Loose Parts Identified as Coupling & Spider Assembly of BPR- B-47,discovered in B once-through Steam Generator.Caused by Assembly Failure. Corrective Action to Be Determined | /01T-0:on 780306,17 Loose Parts Identified as Coupling & Spider Assembly of BPR- B-47,discovered in B once-through Steam Generator.Caused by Assembly Failure. Corrective Action to Be Determined | | | 05000302/LER-1978-017, Forwards LER 78-017/01T-0 | Forwards LER 78-017/01T-0 | |
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