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LER-1980-012, /03L-0:on 800122,while Reactor Core Isolation Cooling Sys Was Tagged Out for Maint,Hpci Was Found Inoperable,Requiring Orderly Shutdown.Caused by Leak in Line to HPCI Booster Pump Discharged Pressure Gauge |
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| 3211980012R03 - NRC Website |
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[ The HPCI Systern was found to bn inoperablo on January 22, 1980 while the RCIC Syste I
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This rendered RCIC and HPCI inonerable sirnultaneousiyi 10141 [ requiring an orderly shutdown to be started per Technical Soecifications 3.5.E.3.
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MAN FA T TEH 3J J4 35 34 31 40 44 cAu s ot:crurTION AND CORRECTIVE ACTICNS h 4;2 43 44 47 ig IThe RCIC System was tacned out for N
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CAUSE DESCRIPTIO 1 AttD CORRECTIVE ACTIOlls When the HPCI operability demonstration was started on 1-22-80, a leak was discovered on a 1/2 inch line to the HPCI booster pump discharge pressure gauge 1E41-R675.
Personnel declared HPCI inoperable at 0600 hours0.00694 days <br />0.167 hours <br />9.920635e-4 weeks <br />2.283e-4 months <br /> on 1-22-80.
This rendered both HPCI and RCIC inoperable.
Tech. Specs. 3.5 E.3 requires an orderly shutdown be initiated and the Reactor be depressurized to less than 113 psig within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after declaring both systems (RCIC and HPCI) inoperable.
An orcerly shutdown was initiated immediately.
The HPCI leak was repaircd at 1135 hours0.0131 days <br />0.315 hours <br />0.00188 weeks <br />4.318675e-4 months <br /> on 1-22-80.
The shutdown was terminated and the unit returned to normal power operation.
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~ NARRATIVE REPORT On 1-21-80, at 0500 hours0.00579 days <br />0.139 hours <br />8.267196e-4 weeks <br />1.9025e-4 months <br /> the RCIC System was tagged out for maintenance to repair several small packing leaks on RCIC valves.
Tech. Specs. 4.5.E.2 requires that when the RCIC System is made or found to be inoperable, the HPCI System shall be demonstrated to be operable immediately and daily there-after until the RCIC System is returned to operable status. When RCIC was tagged out on 1-21-80, the surveillance for HPCI was performed successfully and operability was demonstrated.
The RCIC System remained tagged out until 1740 hours0.0201 days <br />0.483 hours <br />0.00288 weeks <br />6.6207e-4 months <br /> on 1-22-80.
Therefore, HPCI surveillance was required to be per-formed again on 1-22-00 due to RCIC still being inoperable.
While performing the HPCI surveillance, a leak was discovered on a 1/2 inch line to the HPCI booster pump discharge pressure gauge lE41-R675.
The line was cracked and
' spraying water badly.
Personnel declared the HPCI System inoperable at 0600 hours0.00694 days <br />0.167 hours <br />9.920635e-4 weeks <br />2.283e-4 months <br /> on 1-22-80.
Thus, HPCI and RCIC were inoperable simultaneously. Tech.
Specs. 3.5.E.3 requires an orderly shutdown be initiated and the Reactor be depressurized to less than 113 psig within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> from the tin.e that both (RCIC and HPCI) Systems are made or found to be inoperable.
Personnel im-mediately initiated an orderly shut 'own when declaring HPCI inoperative.
However, the HPCI leak was repaired oy Maintenance and the HPCI surveillance was performed successfully.
HPCI was declared operable at 1135 hours0.0131 days <br />0.315 hours <br />0.00188 weeks <br />4.318675e-4 months <br /> on 1-22-80.
The Reactor shutdown wa; terminated and 'the unit returned to normal power operation. The RCIC System was returned to operable status at 1740 on 1-22-80.
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| 05000321/LER-1980-001-01, /01T-0:on 800103,while Performing Maint on RHR LPCI Injection Valve,Clevis Pin Found Missing from Strut on Drywell Penetration Restraint.Caused by Improper Installation.New Clevis Pin Installed | /01T-0:on 800103,while Performing Maint on RHR LPCI Injection Valve,Clevis Pin Found Missing from Strut on Drywell Penetration Restraint.Caused by Improper Installation.New Clevis Pin Installed | | | 05000366/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000366/LER-1980-001-03, /03L-0:on 800102,while Performing Narrow Range Torus Water Level Functional Test & Calibr,Level Transmitter 2T48-N021B Found Out of Tolerance.Caused by Range Drift. Transmitter Recalibr & Returned to Svc | /03L-0:on 800102,while Performing Narrow Range Torus Water Level Functional Test & Calibr,Level Transmitter 2T48-N021B Found Out of Tolerance.Caused by Range Drift. Transmitter Recalibr & Returned to Svc | | | 05000321/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000321/LER-1980-002-03, /03L-0:on 800112,while Performing HNP-1-3655,fan lT46-C001B Would Not Meet Flow Requirements Per Tech Specs. Ten Days Later,While Venting Drywell Per HNP-1-1500,flow Did Not Meet Tech Specs.Equipment Recalibr | /03L-0:on 800112,while Performing HNP-1-3655,fan lT46-C001B Would Not Meet Flow Requirements Per Tech Specs. Ten Days Later,While Venting Drywell Per HNP-1-1500,flow Did Not Meet Tech Specs.Equipment Recalibr | | | 05000321/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000366/LER-1980-002, Forwards LER 80-002/01T-0 | Forwards LER 80-002/01T-0 | | | 05000366/LER-1980-002-01, /01T-0:on 800128,during Cold Shutdown,Ae Notified Util That Single Mode Failure Existed for Torus Gravity Fill Isolation Valve 2G51-F013.Caused by Design Deficiency. Standing Order Issued | /01T-0:on 800128,during Cold Shutdown,Ae Notified Util That Single Mode Failure Existed for Torus Gravity Fill Isolation Valve 2G51-F013.Caused by Design Deficiency. Standing Order Issued | | | 05000366/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000366/LER-1980-003-03, /03L-0:on 800117,while Applying Equalizing Charge to 125/250-volt Dc Station Svc Batteries,Hpci Automatic Flow Control Power Inverter Tripped.Caused by Instrument Drift. Instrument Recalibr Satisfactorily | /03L-0:on 800117,while Applying Equalizing Charge to 125/250-volt Dc Station Svc Batteries,Hpci Automatic Flow Control Power Inverter Tripped.Caused by Instrument Drift. Instrument Recalibr Satisfactorily | | | 05000321/LER-1980-003-03, While Performing RHR Valve Operability Procedure,Outboard Shutdown Cooling Isolation Valve F008 Opened in 25.8-S.Caused by Normal Wear & Human Reaction Time.Valve Operator Adjusted | While Performing RHR Valve Operability Procedure,Outboard Shutdown Cooling Isolation Valve F008 Opened in 25.8-S.Caused by Normal Wear & Human Reaction Time.Valve Operator Adjusted | | | 05000321/LER-1980-003, Forwards Revised LER 80-003/03X-1 | Forwards Revised LER 80-003/03X-1 | | | 05000321/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000321/LER-1980-004-03, /03L-0:on 800106,during Startup Mode,Main Steam Line Inboard Isolation Drain Valve Failed in mid-position. Caused by Failure of Valve Motor Winding.Motor Replaced & Valve Returned to Operable Status | /03L-0:on 800106,during Startup Mode,Main Steam Line Inboard Isolation Drain Valve Failed in mid-position. Caused by Failure of Valve Motor Winding.Motor Replaced & Valve Returned to Operable Status | | | 05000366/LER-1980-004-03, /03L-0:on 800118,during Steady State Power Operation Hydrogen Recombiner Inlet Valve 2T49-F003A Did Not Open.Caused by a Failed Torque Switch.Sys Returned to Operation After Switch Was Replaced | /03L-0:on 800118,during Steady State Power Operation Hydrogen Recombiner Inlet Valve 2T49-F003A Did Not Open.Caused by a Failed Torque Switch.Sys Returned to Operation After Switch Was Replaced | | | 05000366/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000321/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000321/LER-1980-005-03, /03L-0:on 800109,w/reactor Mode Switch in Run Mode,Discovered That Surveillance Procedure HNP-1-3007, Turbine Control Valve Fast Closure,Was Not Performed in Grace Period.Caused by Personnel Error | /03L-0:on 800109,w/reactor Mode Switch in Run Mode,Discovered That Surveillance Procedure HNP-1-3007, Turbine Control Valve Fast Closure,Was Not Performed in Grace Period.Caused by Personnel Error | | | 05000366/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000366/LER-1980-005-03, /03L-0:on 800119,during Power Operation,Tech Specs 4.8.1.1.1.a & 4.8.1.1.2a4 for Electrical Power Sources Were Not Performed within 1-h.Caused by Personnel Misinterpretation of Tech Spec Requirements | /03L-0:on 800119,during Power Operation,Tech Specs 4.8.1.1.1.a & 4.8.1.1.2a4 for Electrical Power Sources Were Not Performed within 1-h.Caused by Personnel Misinterpretation of Tech Spec Requirements | | | 05000321/LER-1980-006-03, /03L-0:on 800113,one Standby Gas Treatment Sys Rendered Inoperable W/Both Units in Power Operation.Unit Not Proven Operable within Required 4-h.Caused by Inability to Prove Filter Train Operable within 4-h | /03L-0:on 800113,one Standby Gas Treatment Sys Rendered Inoperable W/Both Units in Power Operation.Unit Not Proven Operable within Required 4-h.Caused by Inability to Prove Filter Train Operable within 4-h | | | 05000321/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000321/LER-1980-007-03, /03L-0:on 800114,while Testing Standby Svc Water Pump,Pump Would Not Meet Criteria.Caused by Disengagement of Pump First Stage Impeller Lock Collet.Lock Collet Replaced & Pump Reinstalled | /03L-0:on 800114,while Testing Standby Svc Water Pump,Pump Would Not Meet Criteria.Caused by Disengagement of Pump First Stage Impeller Lock Collet.Lock Collet Replaced & Pump Reinstalled | | | 05000321/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000366/LER-1980-007-01, /01T-0:on 800130,while Performing High Drywell Pressure Instrument (Reactor Protection Sys) Functional Test & Calibr,Instruments 2C71-N002A,B & D Exceeded Tech Specs.Caused by Instrument Drift | /01T-0:on 800130,while Performing High Drywell Pressure Instrument (Reactor Protection Sys) Functional Test & Calibr,Instruments 2C71-N002A,B & D Exceeded Tech Specs.Caused by Instrument Drift | | | 05000366/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000366/LER-1980-008-03, While Increasing Reactor Power by Rod Withdrawal,Operator Noticed Rod Select Matrix Backlighted & Rod Sequence Control Sys Not Initiating Rod Blocks Properly.Caused by Design Change | While Increasing Reactor Power by Rod Withdrawal,Operator Noticed Rod Select Matrix Backlighted & Rod Sequence Control Sys Not Initiating Rod Blocks Properly.Caused by Design Change | | | 05000366/LER-1980-008, Forwards LER 80-008/03L-1 | Forwards LER 80-008/03L-1 | | | 05000321/LER-1980-008-03, /03L-0:on 800115,during Steady State Power Operation,Secondary Containment Integrity Violated When Personnel Opened 164-ft Elevation Reactor Bldg & Turbine Bldg Airlock Doors Simultaneously.Procedure Revised | /03L-0:on 800115,during Steady State Power Operation,Secondary Containment Integrity Violated When Personnel Opened 164-ft Elevation Reactor Bldg & Turbine Bldg Airlock Doors Simultaneously.Procedure Revised | | | 05000321/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000366/LER-1980-009-03, /03L-0:on 800130,while Performing Procedure HNP-2-33-3,HPCI Min Flow Valve 2E41-F012 Failed to Close. Caused by Sticking Switch Contacts on Flow Switch 2E41-N006. Switch Contacts Cleaned & Procedure HNP-2-3303 Performed | /03L-0:on 800130,while Performing Procedure HNP-2-33-3,HPCI Min Flow Valve 2E41-F012 Failed to Close. Caused by Sticking Switch Contacts on Flow Switch 2E41-N006. Switch Contacts Cleaned & Procedure HNP-2-3303 Performed | | | 05000321/LER-1980-009-03, /03L-0:on 800118,during Normal Operation,Drywell/ Torus Temp Recorder 1T47-R611 Found Stamping Erratically, Making Drywall & Torus Air Temps & Water Temp Difficult to Ascertain.Caused by Failure of Microswitch.Switch Replace | /03L-0:on 800118,during Normal Operation,Drywell/ Torus Temp Recorder 1T47-R611 Found Stamping Erratically, Making Drywall & Torus Air Temps & Water Temp Difficult to Ascertain.Caused by Failure of Microswitch.Switch Replaced | | | 05000366/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000321/LER-1980-010-03, /03L-0:on 800118,during Normal Operation While Performing Standby Liquid Control Pump Operability Test & Relief Valve Test,Pump a Discharge Relief Valve 1C41-F029A Operated at 1,225 Psig.Caused by Setpoint Drift.Valve Reset | /03L-0:on 800118,during Normal Operation While Performing Standby Liquid Control Pump Operability Test & Relief Valve Test,Pump a Discharge Relief Valve 1C41-F029A Operated at 1,225 Psig.Caused by Setpoint Drift.Valve Reset | | | 05000321/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000366/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000366/LER-1980-010-03, /03L-0:on 800131,during Reactor Startup,At 58% Power,Max Total Peaking Factor Was Calculated at 3.0 Compared to Design Value of 2.38.Caused by Lower than Normal Xenon Distribution During Startup | /03L-0:on 800131,during Reactor Startup,At 58% Power,Max Total Peaking Factor Was Calculated at 3.0 Compared to Design Value of 2.38.Caused by Lower than Normal Xenon Distribution During Startup | | | 05000321/LER-1980-011-03, /03L-0:on 800120,while at Steady State Power, torus-to-drywell Differential Pressure recorder,LT48-R631B Had Low Reading.Cause Not Stated | /03L-0:on 800120,while at Steady State Power, torus-to-drywell Differential Pressure recorder,LT48-R631B Had Low Reading.Cause Not Stated | | | 05000366/LER-1980-011-03, /03L-0:on 800202,while Performing Reactor Core Isolation Cooling Shutdown Flow Test,Power Inverter for Remote Flow Control Loop Found to Be Tripped.Caused by Defective Input Filter Capacitors | /03L-0:on 800202,while Performing Reactor Core Isolation Cooling Shutdown Flow Test,Power Inverter for Remote Flow Control Loop Found to Be Tripped.Caused by Defective Input Filter Capacitors | | | 05000321/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000366/LER-1980-012-03, /03L-0:on 800214,while at Full Power,Rhr & Plant Svc Water Min Flow Line Found to Be Inadequately Supported. Caused by Design Deficiency.Design Change Request & Maint Request Implemented to Add Supports | /03L-0:on 800214,while at Full Power,Rhr & Plant Svc Water Min Flow Line Found to Be Inadequately Supported. Caused by Design Deficiency.Design Change Request & Maint Request Implemented to Add Supports | | | 05000321/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000366/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000321/LER-1980-012-03, /03L-0:on 800122,while Reactor Core Isolation Cooling Sys Was Tagged Out for Maint,Hpci Was Found Inoperable,Requiring Orderly Shutdown.Caused by Leak in Line to HPCI Booster Pump Discharged Pressure Gauge | /03L-0:on 800122,while Reactor Core Isolation Cooling Sys Was Tagged Out for Maint,Hpci Was Found Inoperable,Requiring Orderly Shutdown.Caused by Leak in Line to HPCI Booster Pump Discharged Pressure Gauge | | | 05000321/LER-1980-013, Forwards Updated LER 80-013/03X-1 | Forwards Updated LER 80-013/03X-1 | | | 05000321/LER-1980-013-03, Reactor Recirculation Pump a Tripped Causing Power Reduction.Caused by Electrical Short Circuit Due to Steam Leak in Drywell.Terminal Board Replaced & Tested | Reactor Recirculation Pump a Tripped Causing Power Reduction.Caused by Electrical Short Circuit Due to Steam Leak in Drywell.Terminal Board Replaced & Tested | | | 05000366/LER-1980-013-03, /03L-0:on 800203,while Maint Was Performed on 2082-K002 Static Inverter,Emergency Control Transfer Switch Was Placed in Emergency Position.Reactor Core Isolation Cooling Was Rendered Inoperable.Caused by Personnel Error | /03L-0:on 800203,while Maint Was Performed on 2082-K002 Static Inverter,Emergency Control Transfer Switch Was Placed in Emergency Position.Reactor Core Isolation Cooling Was Rendered Inoperable.Caused by Personnel Error | | | 05000366/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000366/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000366/LER-1980-014-03, /03L-0:on 800204,while Performing HNP-2-3054, Average Power Range Monitor C Failed.Caused by Instrument Drift.Instrument Adjusted Per Procedure & Returned to Svc | /03L-0:on 800204,while Performing HNP-2-3054, Average Power Range Monitor C Failed.Caused by Instrument Drift.Instrument Adjusted Per Procedure & Returned to Svc | |
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