ML19282C173

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LER 79-007/04T-0 on 790228:sulfuric Acid Was Discharged Onto Ground Via Storm Drains Near Storage Tank.Caused by Pipe Weld Failure.Spill Isolated & Contained,Leak Located & Welded
ML19282C173
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 03/14/1979
From: Eherts R
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19282C169 List:
References
LER-79-007-04T, LER-79-7-4T, NUDOCS 7903210134
Download: ML19282C173 (2)


Text

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DATE EVENT DESCRIPTION AND PROSA8LE CONSEQUENCES h ,

I O I 21 l During nomal operations a watchstander observed what acceared to be acid on l O i31 l the ground in the vicinity of the sulfuric acid storace tank. Acid lines in 1 0 4 the area were isolated and the flow of liould arrested. Chemical analyses were  !

IO isi Iperformed on the suspect material which was verified to be acid. It is esti- 1 j

i o is l l mated that less than 5 gallons of sulfuric acid was discharoed to the bay via i

O 7 l the storm drains. No environmental impact is considered due to the small amount I j i

I O 8 lof acid released.

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[Njg 42 43 L lg l Xl 9 l 9 l 9lg 44 47 CAUSE DESCRIPTION ANo CORRECTIVE ACTIONS

[i l0 l lCause has been detemined to be failure of a pipe weld. Imediate corrective i it i,i l action consisted of isolating and containing the spill. Subseouent corrective 1 ii ,,, laction consisted of locating and sealing the leak by welding. l .

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DISCOVERY DESCRIPTION  !

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