05000317/LER-1979-007-04, /04T-0 on 790228:sulfuric Acid Was Discharged Onto Ground Via Storm Drains Near Storage Tank.Caused by Pipe Weld Failure.Spill Isolated & Contained,Leak Located & Welded

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/04T-0 on 790228:sulfuric Acid Was Discharged Onto Ground Via Storm Drains Near Storage Tank.Caused by Pipe Weld Failure.Spill Isolated & Contained,Leak Located & Welded
ML19282C173
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 03/14/1979
From: Eherts R
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19282C169 List:
References
LER-79-007-04T, LER-79-7-4T, NUDOCS 7903210134
Download: ML19282C173 (2)


LER-1979-007, /04T-0 on 790228:sulfuric Acid Was Discharged Onto Ground Via Storm Drains Near Storage Tank.Caused by Pipe Weld Failure.Spill Isolated & Contained,Leak Located & Welded
Event date:
Report date:
3171979007R04 - NRC Website

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EVENT DESCRIPTION AND PROSA8LE CONSEQUENCES h I O I 21 l During nomal operations a watchstander observed what acceared to be acid on l O i31 l the ground in the vicinity of the sulfuric acid storace tank. Acid lines in 1

the area were isolated and the flow of liould arrested. Chemical analyses were 0

4 IO isi Iperformed on the suspect material which was verified to be acid.

It is esti-1 i o is l l mated that less than 5 gallons of sulfuric acid was discharoed to the bay via j

i O 7 l the storm drains. No environmental impact is considered due to the small amount I

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it i,i l action consisted of isolating and containing the spill. Subseouent corrective 1

laction consisted of locating and sealing the leak by welding.

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8 9 to R. F. Eherts (301) 234-7941 N AME OF PREPARER PHONE: