ML19275A727

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IE Insp Repts 50-338/79-33 & 50-339/79-43 on 790723-0810.No Noncompliance Noted.Major Areas Inspected:Previously Identified Enforcement Matters,Unresolved & Open Items & Licensee Response to LERs
ML19275A727
Person / Time
Site: North Anna  Dominion icon.png
Issue date: 08/30/1979
From: Kellogg P, Kidd M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML19275A726 List:
References
50-338-79-33, 50-339-79-43, NUDOCS 7910190037
Download: ML19275A727 (11)


See also: IR 05000338/1979033

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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REGION ll

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101 MARIETTA ST

N.W., sulTE 3100

ATLANTA GEORGIA 303o3

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Report Nos. 50-338/79-33 and 50-339/79-43

Licensee: Virginia Electric and Power Company

P. O. Box 26666

Richmond, Virginia 23261

Facility Name: North Anna Units 1 and 2

Docket Nos. 50-338 and 50-339

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License Nos. NPF-4 and C!SR-78

Inspected at North Anna Site near Mineral Virginia

Inspected by:

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M. S. Kidd, Rpirident Inspecto

Date Signed

Approved by:

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P.J.KellogfSectionChief,)tDNSBranch

Date' Signed

SUMMARY

Inspected on July 23 - August 10, 1979

Unit 1 Areas Inspected

This routine inspection by the resident inspector involved 25 manhours onsite of

previously identified enforcement matters, unresolved items and open items; licensee

event reports; controls for maintenance of the control room complex emergency venti-

lation pressure boundary; and plant tours.

Unit 1 Findings

Within the areas inspected, no items of noncompliance or deviations were identified.

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Unit 2 Areas Inspected

This routine inspection by the resident inspector involved 25 manhours onsite

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of previously identified enforcement matters, unresolved items and open items;

reports per 10 CFR 50.55(e) and 10 CFR 21; plant tours; plant readiness for

ini+.ial fuel loading; and fuel storage.

Unit 2 Findings

Within the areas inspected, no items of noncompliance or deviations were

identified.

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DETAILS

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1.

Persons Contacted

Licensee Employees

D. L. Benson, Supervisor Nuclear Operations

W. R. Cartwright, Station Manager

S. L. Harvey, Operating Supervisor

  • J. R. Harper, Instrument Supervisor
  • J. D. Kellams, Superintendent of Operations

E. G. Lifrage, Project Engineer - Unit 2

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  • V. R. Hadision, NRC Coordinator

P. A. Slatter, Resident QA Engineer - Construction

  • E. H. Smith, Superintendent of Technical Services

Other licensee employees contacted included two engineers, and three office

personnel.

  • Attended one or more exit interviews.

2.

Exit Interview

The inspection scope and findings were summarized on July 27 and August 3,

and 10, 1979 for those persons denoted in paragraph 1.

All subjects in

these Details were discussed.

3.

Licensee Action on Previous Inspection Findings

(Closed) Infractica (338/78-42-01)-

Turbine Generator Auto Stop Oil

Functional Test.

Corrective measures described in the licensee's response of January 26,

1979, were verified to be complete.

Operating procedures 1-0P-1.5 and

1-0P-1.6 were revised January 31 and January 22, 1979, respectively.

This matter is closed.

(Closed) Infraction (338/78-42-02):

Procedure Deviation Reviews by

Station Nuclear Safety and Operating Committee (SNSOC).

Corrective measures discussed in the licensee's response of January 26,

1979 were verified to be c)mplete.

Additionally, the minutes of some

twenty five SNSOC meetings held in 1979 were reviawed. No instances of

procedure deviations being received later than required were observed.

This matter is closed.

(0 pen) Infraction (339/19-28-09):

Untimely Review of a Potentially

Reportable Item.

Corrective measures discussed in the licensee's response of July 17,

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1979 (letter co. 532) were reviewed and diJ ussed with station and corpo-

rate personnel.

Item 1.1 states that con. ruction personnel have been

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reinstructed op phe proepdures for initiqtriRS 9 TeViFW of P0fF9fi 11

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reportable items.

Discussions revealed this statement to be misleading

in that only two individuals had been reinstructed.

Libensee: personnel

were informed that broader corrective and preventive measures should be

taken particularly in view of a similar delay in notification of Power

Station Engineering of a potentially reportable matter discussed in IE

Report 50-339/79-35-02 (apparent Infraction 79-35-02). A licensee repre-

sentative stated that the response would be amended to clarify actions

previously taken and more closely define further actions planned. This

item remains open.

Followup of corrective actions involving equipment

is discussed in paragraph 5.d.

(Closed) Unresolved Items (338/78-37-04 and 339/78-32-03): Class I Structures

Settlement honitoring.

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Theae unresolved items were initiated to determine whether the Unit 1 Techni-

cal Specifications surveillance requirements would be met in light of lack of

baseline data for certain points and resetting of other points after baseline

establishment. For Unit 2, a review by licensee personnel to assure that

proposed Specifications could be met was inferred. The general problem was

addressed by EPC0 in letters to NRR dated November 22 and December 6,1978,

and May 17, 1979. This was preceded by a letter of June 13, 1978 (no. 329)

which requested an amendment to the Unit 1 Specifications with regard to

settlement of the service water pump house (SWPH).

Other inspections of the settlement monitoring program for Unit I were documented

in IE Reports 50-338/78-44 and 50-339/79-13. These reports discuss reviews of

the methods used to reconstruct or estimate settlement values for points reset or

not surveyed because of inaccessibility.

On June 28, 1979, Amendment 12 to the Unit 1 Technical Specifications was issued

by NRR. This amendment revised baseline dates for certain settlement points in

Table 3.7-5 revised allowable total or differential settelement values for certain

points, and provided a mechanism for estimating settlement of inaccessible points

based on nearby points in the Bases for Specification 3/4.7.12. The Amendment

also requires monitoring of additional points namely on the Units I and 2 casing

cooling tanks and two pipe hangers in the service water reservoir and the calcula-

tion of out-of plane distortion for the SWPH floor. Review of 1-PT-112, Category

I Structures - Settlement Monitoring, completed July 25, 1979, based on surveys

performed May 7-29, 1979 and other site calculations revealed that all limits of

Table 3.7-5, including the new points were met. Also, calculation of out-of place

distortion on July 10, 1979 showed this to be in compliance with the new limit.

A revision to' 1-PT-112 to incorporate the new survey points was approved July 30,

1979. A new procedure,1-PT-113, Service Water Pumphouse Settlement Monitoring,

was also approved July 30, 1979 and will cover all settlement calculations for

the SWPH including the out-of plane distortion calculations.

Table 3.75 of the Unit 2 Proof and Reviev (proposed) Technical Specifications was

revised May 30, 1979 to clarify baseline dates for certain survey points. A review

of previous data on file at the station sonfirmed that the required data exists. A

new procedure, 2-PT-112, will be used to compute settlement valves for Unit 2 survey

points to be required by Technical Specifications. This procedure was in draft form

at the conclusion of the inspection period.

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Another aspect of the unresolved items involved significant delays in analysis of

survey data by station personnel after surveys were made. The ingpector observed

that for the May 7-30 surveys, data was received from the surveyor in a timely

fashion and analyzed by mid June,1979, representing a significant improvement in

this area.

Licensee personnel were informed that since it appeared that the Unit 1 Specifi-

cations as amended, could be met and that data exists to allow calculations to

be made as required by Unit 2 Specifications, these unresolved items (338/78-37-

-04 and 339/78-32-03) were considered closed.

4.

Unresolved Items

Unresolved items are natters about which more information is required to determine

whether they are acceptable or may involve noncompliance or deviations. One new

unresolved item identified during this inspection is discussed in paragraph 9.

5.

Followup on Previously Identified Open Items

Records Storage Facility (338/77-57-04)

a.

This item concerned VEPCO's commitment in its Topical Report, Quality

Assurance Program, Operations Phase (VEP-1-3A) to provide a records

storage facility meeting the reluirements of ANSI N45.2.9,1974 by June

of 1978. This commitment was ameided by letter no. 260 of May 5, 1978

to the NRC stating that the facility would be built by July of 1979.

On July 26, 1979, VEPC0 submitted lettar no. 250A stating that due to

certain construction delays, the facility would not be completed until

about September 15, 1979. Item 338/77-57-04 remains open.

b.

Onsite and Offsite Organizations (338/79-01-02 and 339/79-01-01)

These open items concerned differences in FSAR and other organization

charts and that of proposed Technical Specification change no. 14. As

noted in Report nos. 50-338/79-31 and 50-339/79-39, FSAR Figures 13.1.2-1

and 13.1.2-2 were then in agreement with Technical Specification Figures

6-2 and 6-3 as given in Amendment 11. Station Administrative Procedure

(ADM) 1.0, Station Organization and Responsibility, was revised July 20,

1979 to define responsibilities in accordance with revised section 13.1.2

of the FSAR. ADM 2.0, Station Nuclear Safety and Operating Committee, was

also revised July 10, 1979. This revision was effected to implement the

new membership and quorum requirements of Amendment 11 of the Technical

Specification. A further review of Figure 1.1 of the Nuclear Power Station

Quality Assurance Manual revealed that no revision of it was needed. These

open items are considered closed.

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c.

Operation of Reactor Coolant Pumps (338/79-07-02)

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This item concerned the laci< of reference by an operating procedure to the

requirement for having all ree reactor coolant pumps in operation prior to

entering e. ode 2 (critical) . zocedures 1-0P-1.5 and 1-CP-1.6, dated June 4,

and March 14, 1979, were each observed to contain an initial condition

requiring that three pumps be operating prior tc Mode 2 operation. This

implements Operating License condition 2.D.(3).c.

Item 338/79-07-02 is

closed.

d.

Diesel Generator Exhaust Duct Braces (338/79-20-04 and 339/79-28-09)

Unit 1 Licensee Event Report (LER) 79-062/01T-0 discussed the discovery of

temporary iron braces used for fitup during construction found left in the

diesel generator exhaust ducts. Review of the shift supervisor's log for

the time frame involved and completed Maintenance Reports N1-7905030800 and

N1-7905031625 confirmed removal of the braces as described in the LER.

Removal was independently confirmed by in place observation of the ducts

by the inspector. Item 338/79-20-04 is closed.

This problem was also reported per 10 CFR 50.55(e) and 10 CFR 21 for Unit 2

by letter no. 336 dated May 23, 1979. Review of associated documentation

and inspection of the ducts confirmed removal of the braces in Unit 2 also.

The apparent Ir.'raction associated with lack of timely review of the problem

for reportability on Unit 2 is discusred in paragraph 2 of these Details.

Item 339/79-28-09 remains open.

6.

Process / Protection System Integrated Circuit Card Failures

During the inspection period, licensce personnel discovered two mechanisms for

potential generic failure of certain types of process cards in the Westinghouse

7300 series Process / Protection System. These discoveries were reported per

Unit 1 Technical Specifications,10 CFR 50.55(e), and 10 CFR 21 as noted below:

Heat Sink Shorting Failure (Unit 1 LER 79-089)

a.

As noted in the LER, station Instrument Department personnel discovered

that a heat sink on card types NMB, NVP, and NCB could short to rack card

guides, causing a change in output of the cards. Certain of these cards

could fail non-conservatively. An investigation was made to determine

where the cards were used and plans formulated for replacing them, starting

with those which would fail non-conservatively. Replacement cards had been

ordered at the conclusion of the inspection period. They will be replaced

with a newer design card, on which the heat sink has been moved such that

potential for shorting no longer exists. This problem was also reported

per 10 CFR 21 and per 10 CFR 50.55(e) per letter 638 on August 3,1979, for

Unit 2, which utilizes similar cards. The investigation and corrective

actions will be reviewed in more detail during a subsequent inspection

(open items 338/79-33-01 and 339/79-43-01).

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b.

Type NAL Card Transistor Failure (Unit 1 LER 79-091) ,

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During a detailed review of process card failures following discovery of the

problem discussed in paragraph 6.1, station personnel discovered a number of

failures ot type NAL cards due to failure of an output transistor. This was

reported as LER '9-091 for Unit 1, also per 10 CFR 21 per letter nr. 632

dated August 6,1979, for Unit I and per 10 CFR 21 and 50.55(e) f:,r Unit 2 by

letter.no. 637 dated August 3,1979. The review conclu:':' that all failures

had been associated with an older integrated circuit, which had been replaced

by Westinghouse as new parts were ordered.

A program was initiated to determine where the NAL cards were used and if

the transistors involved (component W-104) were defective, and's'phedule

replacement of them accordingly. It was noted that all failures or sus-

pected failures had been discovered during surveillance test. This problem

will be reviewed further during a subsequent inspection (open items

338/79-

33-02 and 339/79-43-02).

7.

IE Bulletin 79-13 - Cracking in Feec. water System Piping

Although not specifically required, the licensee's response to this IEB, letter

no. 530 dated July 13, 1979, covered North Anna 2 as well as VEPCO's other

nuclear units. This response was observed to be accurate in item 5.a. , implying

that more examinations had been performed on Unit 2 than actually conducted.

This was discussed with station management on August 2,1979. Management was

aware of the discrepancy and had initiated measures to correct it. A supplement

response, via letter no. 530A, was submitted August 8,1979. In an unrelated

manner, VEPCO decided to perform all examinations required of operating plants

by this IEB on Unit 2, starting August 10, 1979. Results will be reviewed by IE

Region II personnel.

8.

IE Bulletin 79-06C - Nuclear Incident at Three Mile Island - Supplement

The immediate requirements of this IEB, tripping of all reactor coolant pumps

(RCP) upon initiation of high pressure injection, and providing a second licensed

operator in the central room to trip the RCP's, were telephoned to VEPCO manage-

ment by IE:II on July 26, 1979. On July 27, 1979, the inspector confirmed that

at least two licensed operators, not including the shift supervisor, were being

stationed in the central room at all times. This was also confirmed by subsequent

visits and the central room during the inspection period. An entry was made in

the Shift Order Book July 27, implementing the requirements of the IEB and a

copy of the IEB was placed in the required reading file for operators. The

inspector had no questions regarding immediate implementation of the Bulletin.

Other aspects of it will be reviewed following the licensee's response.

9.

Plant Tours

Tours of selected plant areas were conducted on July 26, 1979, and other dates

during the inspection period in conjunction with other inspection activities.

During the tours, the following items, as available, were observed:

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a.

Fire Equipment

Operability and evidence of periodic inspection of fire suppression equipment.

b.

Housekeeping

Minimal accumulations of debris and maintenance of required cleanliness levels

in systems under or following testing.

c.

Equipment Preservation

Maintenance of special preservative measures for installed equipment as

applicable.

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d.

Component Tagging

Implementation and observance of equipment tagging for safety or equipment

protection.

e.

Communication

Effectiveness of public address system in all areas toured.

f.

Equipment Controls

Effectiveness of jurisdictional controls in precluding unauthorized work on

systems turned over for initial operations or preoperational testing.

g.

Foreign Material Exclusion

Maintenance of controls to assure systems which have been cleaned and flushed

are not reopened to admit foreign material.

h.

Security

Implementation of security provisions for both Units.

Within the above areas, no items of noncompliance or deviations were observed when

compared to the applicable station programs and procedures.

During the tour of July 26, during Unit I full power operation, the inspector

observed a door from the Unit 2 emergency switchgear room to the turbine building

to be open with hoses running through it (fire door S 54-11). The immediate

area appeared to be isolated effectively from the Unit 1 switchgear room fire

protection-wise, but the door also serves as part of the Units 1 and 2 centrol

room pressure boundary envelop. Integrity of the envelop is required to assure

operability of the control room emergency bottled air pressurization system as

required by Unit 1 Technical Specification (TS) 3.7.7.1.

The TS does not speci-

fically require that envelop penetrations be maintained in a closed position,

but requires that the emergency habitability systems, including bottled air, be

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operable during modes 1, 2, 3 and 4.

Thus, compliance with the action statement

of TS 3.7.7.1 could only be determined by performance of a ' functional test of

the bottled air system. In this case, the door was closed upon notification of

operating personnel by the inspector.

During discussions on this matter in an exit interview on July 27, 1979, the

inspector was informed that operator logs 1-LDG-6C and 2-LOG-6c were being

revised to r.equire checks of the doors in the pressure envelop every four hours.

The revised logs, approved July 30, 1979, were in final typing at the conclusion

of the inspection period. Also on July 27, the inspector informed licensee

personnel that TS coverage of pressure boundary penetration <, would be identified

as an unresolved item (338/79-33-03) and would be discussed with other NRC

offices to determine whether modifications to existing TS or creationgof a new

TS is needed to assure habitability of the control room.

10.

New Fuel Storage

New fuel for Unit 2 initial loading and a portion of the new fuel for Unit I

second cycle were in storage in the Units 1 and 2 fuel building during a tour of

the building on July 27, 1979, to verify that provisions for physical security

and environmental protection of the fuel were in agreement with those of the

application for the Unit 2 Special Nuclear Materials (SNM) License dated October 3,

1977 (serial no. 148).

Security measures were found to be equal to or greater than the commitments of

the SNM application and the Station Security Plan. Protection of the fuel from

dust, debris and physical damage ess also found to be adequate. Observation of

fire extinguishers in the area revealed them to have recent inspection dates.

Housekeeping was in order.

Within the areas inspected, no items of noncompliance or deviations were iden-

tified.

11.

Unit 2 Status - Readiness for Operation

At the conclusion of the inspection period, construction of Unit 2 was reported

to be complete. Licensee personnel estimated that it would be ready for initial

fuel loading in early September 1979, not considering any additional activities

or modifications required by NRC as a result of the Three Mile Island incident.

IE Report 50-339/79-28, Details paragraph 8 listed activities to be completed

and problems to be resolved prior to IE:II making a finding that Unit 2 would be

ready for an operating license. A revised listing is given below including

certain new problems. Resolution of certain old items was discussed in IE

Report Nos. 50-339/79-33, 35, 39, and 40. Items remaining to be completed or

otherwise resolved are categorized below by milestone:

Items to be Resolved Prior to Fuel Loading

a.

1). Completion of preoperational testing and satisfactory resolution of

test deficiencies. As of August 9,1979, 95 of 103 tests had been

completed and the results of 70 approved.

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2). Station Nuclear Safety Operating Committee review and develop schedule

to resolve significant preoperational test deficiencieg and master defi-

ciency list items acceptable to Region II.

3).

Complete development of operational procedures recommended by R.G.1.33.

(Three procedures not approved.)

4).

Complete implementaiton of industrial security program in accordance

with the North Anna Modified Amended Security Plan.

5). Resolve Quality assurance program outstanding items (IE Report 339/79-11).

b.

Item to be Resolved Prior to Two Unit Operation in Modes 4 of Above

1).

Modify the electrical transfer buses to eliminate overloading during

two unit operation (LER 79-57/01T-0 for Unit 1; Unit 2 open item

79-28-10).

Items to be Resolved Prior to Initial Criticality

c.

1). Verify that no mechanical interferences exist between incore guide

tubes or modified insulation supports and the reactor vessel lower

head insulation due to themal growth during precritical testing

(78-24-02).

2). Visual verification of hydraulic snubber operability at operating

temperature (79-26-02).

3). Revise operating procedures and system drawings to assure electrical

independence between redundant subsystems for control room air

conditioning (79-12-02).

4). Resolve lack of seis:nic supports and missile protection for the

emergency diesel generator exhausts and mufflers (79-12-02).

5). Demonstrate operability of safety related AC and DC solenoid valves

which may have parts missing (79-21-02).

6).

Complete modifications to control room air conditioner chillers

required as a result of the increase in projected service water

temperature which resulted from reevaluation of the spray pond

efficiency (79-21-01).

7). Verify adequate seismic stress analysis of safety related piping per

IE Bulletin 79-07 (79-28-07).

8).

Complete installation of reactor vessel shielding to prevent excessive

radiation levels in containment (78-12-02).

9). Verify adequacy of service water and component cooling water pipe

supports to resist thermal loadings over service water temperature

range (78-36-01).

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10). Verify service water flow to charging pump coolers is sufficient

(79-12-01).

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11). Determine if atypical weld material used in the reactor vessel seam

welds (IE Bulletin 78-12A).

12). Verify that piping and support loads are within limits for systems

where erroneous Velan check valve weights were used (79-21-03; also

sie lE Bulletin 79-04).

13). Resolve error found in DNBR analysis for single dropped control rod.

14). Resolveinsiderecirculationspraypumpmotorbearingfaifuredue

to shaf t seizure (79-38-03).

15). Verify that pipe support base plates using concrete expansion anchor

bolts are adequate in accordance with IE Bulletin 79-02 (79-28-06).

16). Resolution of potential non-conservative failure of type NAL Process /

Protection signal comparator cards due to failure of W-104 transistors

(79-43-02).

d.

Items to be Resolved Prior to Exceeding 25% Power

1). Develop surveillance program for fiberglass spray pond piping and

supports (R.G.1.72) .

2).

Complete environmental qualification testing and resolve any defici-

encies identified for electrical ecmponents inside containment (IE

Circular 78-08/78-28-01 and IE Bulletin 79-01).

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