05000348/LER-1979-003-03, /03L-0 on 790116:following Reactor Trip,Turbine Driven Auxiliary Feedwater Pump Failed to Start.Caused by Trip/Throttle Valve Which Tripped Shut

From kanterella
(Redirected from ML19274D661)
Jump to navigation Jump to search
/03L-0 on 790116:following Reactor Trip,Turbine Driven Auxiliary Feedwater Pump Failed to Start.Caused by Trip/Throttle Valve Which Tripped Shut
ML19274D661
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 02/13/1979
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19274D655 List:
References
LER-79-003-03L, LER-79-3-3L, NUDOCS 7902210233
Download: ML19274D661 (1)


LER-1979-003, /03L-0 on 790116:following Reactor Trip,Turbine Driven Auxiliary Feedwater Pump Failed to Start.Caused by Trip/Throttle Valve Which Tripped Shut
Event date:
Report date:
3481979003R03 - NRC Website

text

tJRC FORM 3GG U. S. NUCLE AR HEGULATOR Y COMMISSION LICENSEE EVENT REPORT CON TROL BLOCK: l l

l l

l l

lh (PLE ASE PRINT OR TYPE ALL REQUIRED iNFORMATION) t 6

jo lil i ^l Li JI Ml Fl 1l@l 0l 0l -l 0l 0l 0l 0l 0] -l 0l 0l@26l 4l 1l 1l Il 1l@l l

l@

8 9 LICENSEE CODL I4 15 LICENSE NUMBER 2b LICENSE TYPE Ju b7 CAI bS E.ON'T

"$nN dl 0I 5 l 0 l 0 l 0 l 114 l 3]@l 0 l 1 l 1 l 6 l 7 l 9J@l 0 l 2 l 1 l 3 l 7 l 9 l@

o 1

e I

8 60 61 DOC <ET NUY9ER 68 61 EVENT DATE 74 75 HEPORT D AT E 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l Following a reactor trip at 0130 on 1/16/79 the turbine driven aux. feedwater pump l

o 2

[ o ; 3 y l (TDAFP) f ailed to start when the trip / throttle valve tripped shut.

T.S. 3.7.1.2 l

l o 14 l l requires at least 3 independent steam generator aux. feedwater pumps and associated l

[o jsg flow paths shall be operable. The trip /thrittle valve was manually opened and the TDAFP was verified operable. The T.S. 1. s. l.2 action statement was met.

The health j o o l o l 7 l l and safety of the put.lic were not af f ec.ted.

A similar occurrence was reported in l,

l LER-021/01T-0.

l o

a 60 7

8 9 SYSTEM

CAUSE

CAUSE C O*M.

VALVE CODE CODE SU8 CODE COMPONENT CODE SUSCODE SUBCODE lo191 i s I n l@ LIj@ Lx_1@ l v l ^ l 1. I v I o I e l@ LJ_J @ 13 @

7 8

9 10 11 12 IJ 18 19 20 SEQUENTI AL OCCURRENCE REPORT REVISION LE R/RO EVENTYEAR REPORT NO.

CODE TYPE NO.

hR l7 l9 l

- l l0l0l3l y

l0 l3 l W

[-]

W

_ 21 22 23 24 26 21 28 23 30 al 32 O [PL NT T1 HOURS SUB IT ED FO 1 8.

SU PLIE MAN FACTLRER

,b^

[J_j@lzl@

Lzj@

lzl@

l 01010 l 0 I [N l@

lNl@

lAl@

l H l 0 l 3 l 5 l@

TAKEN AC O

,34 35 36 3/

40 41 42 43 44 47 33 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h ltlollSubseauent investication deter.nined that the trip / throttle valve had tripped due to al Il I i l 1TDATP Overspeed Trip.

The overspeed condition was caused by the TDAFP nini fL w valvel Ispring tension being insufficient to hold the valve full open (valve was 25% open).

1 i

2 lil3l l The spr'ing tension was adjusted to fully open the AOV and the turbine did not overspedd lil41 lon subsequent overspeed tests.

7 8 9 83 ST S

% POWER OTHER STATUS btSCO R

DISCOVERY DESCRIPTION Lcj@ l01010 l@l NA l

[A_j@l NA l

i s 7

8 9 10 12 ti 44 45 46 80 ACilvlTY CONTENT RELE ASED OF RE LE ASE AMOUNT OF ACTivlTY LOCATION OF RELE ASE NA l

l NA l

li Ic l Lzj @ Lz_l@l 7

8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUV8ER TYPE

DESCRIPTION

l 1 l 7 l l 0 l 0 l 0 l@[7]@l NA j

,E RS.NE L imu'iES oESCRiPTiO~@

NUv8Ee FG 110101 Ol@l NA I

7 8 9 11 12 80 LOSS OF OR DAVAGE TO FACILITY Q

( TT1 LzJ@l TYPE DE.SCRIPTION v

ri NA I

7 8 9 10 80 iSSui"hl*L'SCRiPTiO~ @

7902910#'3O' [N_j NA l l l l l l l l l l l 1 l ';*

~

2 o 7

8 0 10 63 69 80 5 NAME OF PREPARER U. C. Hairston, III (205) 899-5156 pygyg.