05000237/LER-1979-039-03, /03L-0 on 790528:125 Volt Dc Switch 2,reserve Feed Bus 22, Was Opened Causing Trip of 282 Recirculation Motor Generator Set Oil Pump.Caused by Inadvertent Opening of Switch.Switch Marked to Caution Against Opening

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/03L-0 on 790528:125 Volt Dc Switch 2,reserve Feed Bus 22, Was Opened Causing Trip of 282 Recirculation Motor Generator Set Oil Pump.Caused by Inadvertent Opening of Switch.Switch Marked to Caution Against Opening
ML19270H019
Person / Time
Site: Dresden 
Issue date: 06/15/1979
From: Ammer A
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17173A928 List:
References
LER-79-039-03L, LER-79-39-3L, NUDOCS 7906220373
Download: ML19270H019 (1)


LER-1979-039, /03L-0 on 790528:125 Volt Dc Switch 2,reserve Feed Bus 22, Was Opened Causing Trip of 282 Recirculation Motor Generator Set Oil Pump.Caused by Inadvertent Opening of Switch.Switch Marked to Caution Against Opening
Event date:
Report date:
2371979039R03 - NRC Website

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8 6J G1 DOCKET NUM8;n 64 G3 EVENT DATg 74 75 REPoHT DATE 80 EVEN T DESCRIPTION ATJO PROB AOLE CONSEQUENCES h g uring normal operation, the 125V DC switch No. 2, " Reserve Feed, Bus 22,"

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