LER-1979-002, Forwards LER 79-002/01X-1 |
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| 2371979002R00 - NRC Website |
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I-a Commonweal-dison.
Dresden Nuclear PTer Station R.R. #1 Morris, Illinois 60450 Telephone 815/942-2920 BBS LTR t/79-449 June 5, 1979 James G. Keppler, Regional Director Directorate of Regulatory Operations - Region III U.S. Nuclear Regulatory Connnission 799 Roosevelt Road Glen Ellyn, IL 60137 Revised Reportable Occurrence Report 1179-02/0lX-l, Docket t/050-237 is hereby submitted to your office in accor:dance with Dresden.Nuclear Power, Station Technical Specification 6.6.B.l(e), failure or malfunction of one or more components which prevents or could preve~t, by itself, the. fulfi:J._lment of. the functional requirements of. system(s) used to cope.
with accidents analyzed in the SAR *., Futµre action code 19 has been changed to reflect action to be taken as a result of new information.
BBS:lcg Enclosure
..
F B.B. Stephenson.*
- station Superintendent Dresden Nuclear Power Station cc:, Director of Inspection & Enforcement Director of Management Information & Program Control File/NRC
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..a.!CE£\\lSEE EVENT REPOl~T UPDATE REPORT I
9vrous REPORT DATE:
1-17-79 CONTROL ElLOCI(: L I l_=J f,\\
(PLEASE PRINT OR TYPE ALL. REQUIRED INFORMATION)
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60 61 DOCKET !<UMBER GS 69 EVENT DATE 74 75 REPORT DATE BO EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@
[)))) I During normal operation, HPCI turbine failed to start during quarterly f] ow_ test. HPCI I declared inoperable and required ECCS surveillances (T. S. 3. 5. C. 2) commenced.
During
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HPCI then declared
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operable.
Required $urveillances except auto blowdoWQ. were completed satisfactorily.
This is the first occurrence of this type.
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19 RE?ORT TYPE LU 30 VALVE SUBCODE w@
20 31 l'.CTION FUTURE TAKEr-1 ACTION EFFECT ON PLAl~T SHUTDOWN METHOD HOURS
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[iJTI ~pe~:~_in?._~ever.. Lever adjusted.
HPCI started to verify operability.
During re-I fueling outage 4/79 found control oil restriction in motor speed changer pilot valve. I [JJ}] I prevented full electric positioner piston travel.
Relieved restriction.
Will insp~ctJ
[ 1 [j] I Unit 3 HPCI controls.
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9 FACILITY STATUS*
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ATTACHMENT TO LICENSEE EVENT REPORT 79-02/0lX-l COMHONWEALTH EDISON COMPANY (CWE)
DRESDEN UNIT (ILDRS-2)
DOCKET II 050-237 With the unit operating at steady load, the HPCI turbine failed to start during performance of quarterly 'flow test surveillance DOS 2300-3.
~*lhen the motor speed changer was run from the low speed stop to the high speed stop, the turbine control valves did not open~
As a result the HPCI system was declared inoperable and the required ECCS surveillances (T.S. 3.5.C.2) commenced.
At 1430 the HPCI surveillance was performed again and the HPCI turbine started on the second attempt... Six con*secutive turbine startups were performed and the surveillance successfully completed.
l'he HPCI system was declared operable.
This event has minimal safety significance since the required ECCS surveillances with the exception of auto blo.\\-ldown were *completed.
The auto blowdown surveillance was terminated when HPCI was declared operable.
On 1/4/79 at 1100 the HPCI turbine was operated with the General Electric Technical representative present.
He noted that the pin on the motor speed changer linkage which actuates the interlock dump valve when the motor speed changer is on the low speed stop was not fully depressing the interlock dump valve operating lever.
The purpose of the interlock dump valve is to prevent the control valves from opening during system startup with the turbine reset and the motor speed changer not on the low speed stop.
The interlock dump valve actuating lever was adjusted to provide full engagement and HPCI pump and valve operability surveillance DOS 2300-1 successfully performed at 1400.
During the Unit 2 refueling outage on 4/79, the General Electric Technical representative made an inspection of the HPCI turbine control system.
This included checking linkage measurements and piston travel during control system operation.
He found that the electric positioner piston did not fully re-tract to the required position when the motor speed changer is run to the low speed stop.
The pin discussed above is connected to the electric po-sitioner piston rod.
This accounts for the adjustment required previously to effect proper interlock dump valve operation.
Further investigation revealed that an oil restriction existed in the motor speed changer pilot valve resulting in incomplete venting of the.control _QiLfrom~_the.electric positioner piston.
When the restriction problem was rectified, the control system was verified to operate properly.
It is planned to perform a similar control system inspection on the Unit 3 HPCI turbine during the next Unit 3 refueling outage.
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| 05000237/LER-1979-001-03, /03L-0 on 790103:torus Level Increased to -1 Inch, Due to Repetitive Starts of HPCI Turbine.Increase in Torus Level Determined to Be Result of Inadequate Procedure.Hpci Surveillance Procedures to Be Amended | /03L-0 on 790103:torus Level Increased to -1 Inch, Due to Repetitive Starts of HPCI Turbine.Increase in Torus Level Determined to Be Result of Inadequate Procedure.Hpci Surveillance Procedures to Be Amended | | | 05000237/LER-1979-001, Forwards LER 79-001/03X-1 | Forwards LER 79-001/03X-1 | | | 05000010/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000010/LER-1979-001-03, /03L-0 on 790518:while Digging Ditch for New Pipe, Const Personnel Observed Water Running Into Trench from Proximity of Radwaste return-to-storage Line.Caused by Return Line to 1A Storage Leaking from Aluminum Line | /03L-0 on 790518:while Digging Ditch for New Pipe, Const Personnel Observed Water Running Into Trench from Proximity of Radwaste return-to-storage Line.Caused by Return Line to 1A Storage Leaking from Aluminum Line | | | 05000010/LER-1979-002-03, /03L-0 on 780825:during Monthly Surveillance DI5 5400-2,offgas Monitor 1 Tripped at Greater than 100%, Which Is Not within Setpoint Limit.Caused by Instrument Drift.Setpoint Recalibr | /03L-0 on 780825:during Monthly Surveillance DI5 5400-2,offgas Monitor 1 Tripped at Greater than 100%, Which Is Not within Setpoint Limit.Caused by Instrument Drift.Setpoint Recalibr | | | 05000010/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000237/LER-1979-002, Forwards LER 79-002/01X-1 | Forwards LER 79-002/01X-1 | | | 05000237/LER-1979-002-01, /01X-1 on 790103:during Normal Operation,Hpci Turbine Failed to Start During Quarterly Flow Test.Caused by Partial Engagement of Interlock Dump Valve Operating Lever. Lever Adjusted.Hpci Started to Verify Operability | /01X-1 on 790103:during Normal Operation,Hpci Turbine Failed to Start During Quarterly Flow Test.Caused by Partial Engagement of Interlock Dump Valve Operating Lever. Lever Adjusted.Hpci Started to Verify Operability | | | 05000237/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000237/LER-1979-003-03, /03L-0 on 790105:PS 2-1430-1466D Tripped at 105 Psi.Caused by Instrument Drift | /03L-0 on 790105:PS 2-1430-1466D Tripped at 105 Psi.Caused by Instrument Drift | | | 05000237/LER-1979-004-03, /03L-0 on 790111:LPCI Sys Full Flow Test Valve MO-2-1501-38B Failed While Securing D LPCI Pump.Caused by Broken Pinion Gear on Valve Operator Motor Shaft | /03L-0 on 790111:LPCI Sys Full Flow Test Valve MO-2-1501-38B Failed While Securing D LPCI Pump.Caused by Broken Pinion Gear on Valve Operator Motor Shaft | | | 05000237/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000237/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000237/LER-1979-005-03, /03L-0 on 790119: During Normal Operation, Mass Spectometer Leak Detector Downscale Condition Annunciated & High Rad Alarm & Half Scram Occurred Twice on Same Day. Log Rad Monitor Replaced | /03L-0 on 790119: During Normal Operation, Mass Spectometer Leak Detector Downscale Condition Annunciated & High Rad Alarm & Half Scram Occurred Twice on Same Day. Log Rad Monitor Replaced | | | 05000237/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000237/LER-1979-008-03, /03L-0 on 790126: LPCI Min Flow Value MO-2-1501-13A Failed to Close Completely During LPCI Pump Operability Surveillance.Cause of Failure Unknown | /03L-0 on 790126: LPCI Min Flow Value MO-2-1501-13A Failed to Close Completely During LPCI Pump Operability Surveillance.Cause of Failure Unknown | | | 05000237/LER-1979-009-03, /03L-0 on 790121:plant Chimney Sampling Sys Operating Incorrectly.Caused by Purge Valve V2 Being Stuck Open | /03L-0 on 790121:plant Chimney Sampling Sys Operating Incorrectly.Caused by Purge Valve V2 Being Stuck Open | | | 05000237/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000237/LER-1979-010-01, /01T-0 on 790202:section of Blowout Panel Blown Out,Breaching Secondary Containment.Cause Under Investigation | /01T-0 on 790202:section of Blowout Panel Blown Out,Breaching Secondary Containment.Cause Under Investigation | | | 05000237/LER-1979-010, Forwards LER 79-010/01T-0 | Forwards LER 79-010/01T-0 | | | 05000237/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000237/LER-1979-013-03, /03L-0 on 790223:after Diesel Generator Was Manually Started Prior to Taking Transformer Out of Svc, Water Pump Breaker Thermally Tripped & Redundant Power Supply Also Tripped.Cause Unknown | /03L-0 on 790223:after Diesel Generator Was Manually Started Prior to Taking Transformer Out of Svc, Water Pump Breaker Thermally Tripped & Redundant Power Supply Also Tripped.Cause Unknown | | | 05000237/LER-1979-014-03, /03L-0 on 790305:U2 Diesel Generator Failed to Start on First & Fifth Attempts.Caused by Bendix Gear Failure to Engage & Failure of Air Start Solenoid to Energize.Solenoid Was Replaced | /03L-0 on 790305:U2 Diesel Generator Failed to Start on First & Fifth Attempts.Caused by Bendix Gear Failure to Engage & Failure of Air Start Solenoid to Energize.Solenoid Was Replaced | | | 05000237/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000237/LER-1979-015, Forwards LER 79-015/01T-0 | Forwards LER 79-015/01T-0 | | | 05000237/LER-1979-016, Forwards LER 79-016/01T-0 | Forwards LER 79-016/01T-0 | | | 05000237/LER-1979-017-01, X2 for Dresden, Units 2 and 3 Re Inadequacies Observed in Implementation of Administrative Procedural Controls Which Threaten to Cause Reduction of Degree of Redundancy Provided in Reactor Protection System or Engineered Saf | X2 for Dresden, Units 2 and 3 Re Inadequacies Observed in Implementation of Administrative Procedural Controls Which Threaten to Cause Reduction of Degree of Redundancy Provided in Reactor Protection System or Engineered Safety Feature Sys | | | 05000237/LER-1979-017, Forwards LER 79-017/01T-0 | Forwards LER 79-017/01T-0 | | | 05000237/LER-1979-019, Forwards LER 79-019/03L-0 | Forwards LER 79-019/03L-0 | | | 05000237/LER-1979-020-03, /03L-0 on 790413:measured Leakage for Personnel Air Lock Was 54.63 Std Cubic Ft/H.Leakage Identified Through Outer Lower Handwell.Shaft Packing Was Replaced & Air Lock Retested | /03L-0 on 790413:measured Leakage for Personnel Air Lock Was 54.63 Std Cubic Ft/H.Leakage Identified Through Outer Lower Handwell.Shaft Packing Was Replaced & Air Lock Retested | | | 05000249/LER-1979-021-03, /03L-0:on 790821,during Normal Operation,Offgas Monitor 3A Took Step Increase W/No Power Change & hi-hi Trip Light Was On.Caused by Faulty V1 Electrometer Tube,Which Was Replaced.Monitors Will Be Tested Monthly | /03L-0:on 790821,during Normal Operation,Offgas Monitor 3A Took Step Increase W/No Power Change & hi-hi Trip Light Was On.Caused by Faulty V1 Electrometer Tube,Which Was Replaced.Monitors Will Be Tested Monthly | | | 05000237/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000237/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | | | 05000237/LER-1979-023-03, /03L-0 on 790406:during Radioactive Insp,Lack of Fusion Noted in Weld 4-4 on 4-inch Reactor Head Vent Line 2-0215-4.Weld Cut Out & Rewelded Per ASME Boiler & Pressure Vessel Code.Asme Hydrostatic Test Completed | /03L-0 on 790406:during Radioactive Insp,Lack of Fusion Noted in Weld 4-4 on 4-inch Reactor Head Vent Line 2-0215-4.Weld Cut Out & Rewelded Per ASME Boiler & Pressure Vessel Code.Asme Hydrostatic Test Completed | | | 05000249/LER-1979-023-03, /03L-0:on 790823,source Range Monitor Calibr Supplied Rod Block Trip at 1.03E5,exceeding Tech Specs Limit.Caused by Drift & Temp Dependency in Source Range Monitor.Defective Component Not Yet Identified | /03L-0:on 790823,source Range Monitor Calibr Supplied Rod Block Trip at 1.03E5,exceeding Tech Specs Limit.Caused by Drift & Temp Dependency in Source Range Monitor.Defective Component Not Yet Identified | | | 05000237/LER-1979-025, Forwards LER 79-025/03L-0 | Forwards LER 79-025/03L-0 | | | 05000237/LER-1979-026, Forwards LER 79-026/03L-0 | Forwards LER 79-026/03L-0 | | | 05000249/LER-1979-027, Forwards LER 79-027/03L-0 | Forwards LER 79-027/03L-0 | | | 05000237/LER-1979-027-03, /03L-0 on 790502:during Startup,Main Turbine Tripped on High Water Level.Caused by Packing Leak on Isolation Valve for PS-263-60B.Packing Adjusted,Tested & Sys Lineup Returned to Normal | /03L-0 on 790502:during Startup,Main Turbine Tripped on High Water Level.Caused by Packing Leak on Isolation Valve for PS-263-60B.Packing Adjusted,Tested & Sys Lineup Returned to Normal | | | 05000237/LER-1979-027, Forwards LER 79-027/03L-0 | Forwards LER 79-027/03L-0 | | | 05000249/LER-1979-027-03, /03L-0:on 791003,half of Trip Sys Inoperable Due to Lifting of Flooding Magnetrol Switch Leads to Condenser Pit.Switch Leads Reattached.No Precise Cause Found | /03L-0:on 791003,half of Trip Sys Inoperable Due to Lifting of Flooding Magnetrol Switch Leads to Condenser Pit.Switch Leads Reattached.No Precise Cause Found | | | 05000237/LER-1979-028, Forwards LER 79-028/03L-0 | Forwards LER 79-028/03L-0 | | | 05000237/LER-1979-028-03, /03L-0 on 790508:N2 Line Low Temp Alarm Received & Frost Found on Inerting line.A0-2-1601 & Inerting Line Failed Leak Rate Test.Caused by Failure of Temp Recorder at N2 Vaporizer | /03L-0 on 790508:N2 Line Low Temp Alarm Received & Frost Found on Inerting line.A0-2-1601 & Inerting Line Failed Leak Rate Test.Caused by Failure of Temp Recorder at N2 Vaporizer | | | 05000237/LER-1979-029-03, /03L-0 on 790508:DIS 1400-3,pressure Switch 2-1430-1466D Failed to Trip.Caused by Sticky Plunger in Pressure Switch.Switch Removed,Cleaned & Reset to Trip at 94.5 Psig Increasing | /03L-0 on 790508:DIS 1400-3,pressure Switch 2-1430-1466D Failed to Trip.Caused by Sticky Plunger in Pressure Switch.Switch Removed,Cleaned & Reset to Trip at 94.5 Psig Increasing | | | 05000237/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | | | 05000249/LER-1979-030-03, During Scram Testing in Refuel Mode,Substantial Loss of Position Indication Noted for Control Rod Driveline H-9.Caused by Improperly Seated Socket,Suggesting Faulty Electrical pin-socket Alignment | During Scram Testing in Refuel Mode,Substantial Loss of Position Indication Noted for Control Rod Driveline H-9.Caused by Improperly Seated Socket,Suggesting Faulty Electrical pin-socket Alignment | | | 05000249/LER-1979-030, /03X-1 for Dresden Unit 3 Regarding a Supplement to LER 79-30/03L-0 Addressing the Cause and Corrective Actions for the Loss of Position Indication for CRD H-9 | /03X-1 for Dresden Unit 3 Regarding a Supplement to LER 79-30/03L-0 Addressing the Cause and Corrective Actions for the Loss of Position Indication for CRD H-9 | | | 05000237/LER-1979-031-03, /03L-0 on 790509:crack Found on 2D1 Feedwater Emergency Spill to Condenser Line & Crack Located on Pipe to Condenser Weld.Caused by Mechanical Failure.Cracked Portion Removed & Rewelded | /03L-0 on 790509:crack Found on 2D1 Feedwater Emergency Spill to Condenser Line & Crack Located on Pipe to Condenser Weld.Caused by Mechanical Failure.Cracked Portion Removed & Rewelded | | | 05000237/LER-1979-031, Forwards LER 79-031/03L-0 | Forwards LER 79-031/03L-0 | | | 05000237/LER-1979-032, Forwards LER 79-032/03L-0 | Forwards LER 79-032/03L-0 | |
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