LER-1979-009, Forwards LER 79-009/03L-0 |
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.. Commonwe-Edison Dresden Nuclear Power Station R.f3. #1 Morris, Illinois 6~50
'felephone 815/942-2920 February 20, 1979 BBS LTR 1179-168 James G. Keppler, Regional Director Directorate of Regulatory Operations U.S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL. 60137' -=~*'.*'**':":.':-:'.'"--
- - Region III Reportable Occurrence Report /f79-09/03L-0, Docket 11050-237 is hereby submitted to your office in accorda_nce with Dresden Nuclear Power Station Technical Specification 6.6.B.2. (b), conditions leading to operation in a degraded mode permitted by a limiting condition for operation or plant shutdown required by a limiting condition for operation.
BBS:lcg
Director of Inspection & Enforcement Director of Management Information & Program.Control File/NRC
17-77) l LICENSEE EVENT REPORT l
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. ~~~~~! ~01 o I s I o I o f o I 2 I 3 11 101 o I 11 2 I 11 7 I 9 101 o I 2 I 2 I o I 7 I 9 I CV 60 61 DOCKET NUMBER 68 69 EVENT OATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PAOBABLE CONSEQUENCES@
I While Unit 2 was in steady. state operation and Unit. 3 was in cold shut down, it was found that the plant chimney sampling system was operating:incorrectly. Since the steam jet air ejector monitors were operable the safety significance of this event is*
minimal.
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from the turbine. building :into the *system.
The replaced valve was inadyertently in-IIIIJ stalled backwards, still allowing building air to be drawn in.
Following repair system flow still low due to plugged filter.
Installation of condensate drain to I DJ)) ~I ~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~----1
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ATTACHMENT TO LICENSEE EVENT REPORT 79-09/031-0
. COMMONWEALTH EDISON COMPANY (CWE)
DRESDEN UNIT -2 * (ILDRS-2)
DOCKET If 050-237 While Unit 2 was in steady state operation and Unit 3.was in cold shutdown, it was determined the plant chimney sampling system was not operating correctly.
Since the steam jet air ejector monitors.
- were operable, the safety significance of this event was minimal.
On 1/21/79, a work request was.initia~ed.. t~ investigate the problem.
It was found that the purge valve V2 was stuck open, allowing turbine build.:ing air to be.corttinuously'.drawri:.ii1to the. system.~'*'J'he:yalye.. ~~~as replaced and the valve which was removed was disassembled. **h\\ias: :>.
foµnd that. the valve stem was bent.. on 1/24/79, another in_;es't..igat.i~ri of a low flow problem revealed that. the valve which had just been re-placed had been installed backwards, and once again*was allowing
~ir from the Turbine Building to be drawn into the system.
Despite the repair of the purge valve, a low flow problem persisted.
Further investigation showed that the particulate filter became plugged very frequently.
water stains could be found on the filters and the filter holder... Apparently* the.moisture of the warm air. from.
the chimney condensed in the sampling pipe due to the extreme cold weather.. It was found that in the original design of the system.
there was a loop drain.
Apparently in a later modification, the.
drain was replaced by a heater.
It is believed that this heater cannot handle the excessive condensation caused by the re.cent ex-cessively cold weather.
An.investigation is under way to. determine if there is a need to reinstall the loop drain..Until the low flow problem is corrected, the filter will be changed more frequently, to avoid moisture saturation.
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| 05000237/LER-1979-001-03, /03L-0 on 790103:torus Level Increased to -1 Inch, Due to Repetitive Starts of HPCI Turbine.Increase in Torus Level Determined to Be Result of Inadequate Procedure.Hpci Surveillance Procedures to Be Amended | /03L-0 on 790103:torus Level Increased to -1 Inch, Due to Repetitive Starts of HPCI Turbine.Increase in Torus Level Determined to Be Result of Inadequate Procedure.Hpci Surveillance Procedures to Be Amended | | | 05000237/LER-1979-001, Forwards LER 79-001/03X-1 | Forwards LER 79-001/03X-1 | | | 05000010/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000010/LER-1979-001-03, /03L-0 on 790518:while Digging Ditch for New Pipe, Const Personnel Observed Water Running Into Trench from Proximity of Radwaste return-to-storage Line.Caused by Return Line to 1A Storage Leaking from Aluminum Line | /03L-0 on 790518:while Digging Ditch for New Pipe, Const Personnel Observed Water Running Into Trench from Proximity of Radwaste return-to-storage Line.Caused by Return Line to 1A Storage Leaking from Aluminum Line | | | 05000010/LER-1979-002-03, /03L-0 on 780825:during Monthly Surveillance DI5 5400-2,offgas Monitor 1 Tripped at Greater than 100%, Which Is Not within Setpoint Limit.Caused by Instrument Drift.Setpoint Recalibr | /03L-0 on 780825:during Monthly Surveillance DI5 5400-2,offgas Monitor 1 Tripped at Greater than 100%, Which Is Not within Setpoint Limit.Caused by Instrument Drift.Setpoint Recalibr | | | 05000010/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000237/LER-1979-002, Forwards LER 79-002/01X-1 | Forwards LER 79-002/01X-1 | | | 05000237/LER-1979-002-01, /01X-1 on 790103:during Normal Operation,Hpci Turbine Failed to Start During Quarterly Flow Test.Caused by Partial Engagement of Interlock Dump Valve Operating Lever. Lever Adjusted.Hpci Started to Verify Operability | /01X-1 on 790103:during Normal Operation,Hpci Turbine Failed to Start During Quarterly Flow Test.Caused by Partial Engagement of Interlock Dump Valve Operating Lever. Lever Adjusted.Hpci Started to Verify Operability | | | 05000237/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000237/LER-1979-003-03, /03L-0 on 790105:PS 2-1430-1466D Tripped at 105 Psi.Caused by Instrument Drift | /03L-0 on 790105:PS 2-1430-1466D Tripped at 105 Psi.Caused by Instrument Drift | | | 05000237/LER-1979-004-03, /03L-0 on 790111:LPCI Sys Full Flow Test Valve MO-2-1501-38B Failed While Securing D LPCI Pump.Caused by Broken Pinion Gear on Valve Operator Motor Shaft | /03L-0 on 790111:LPCI Sys Full Flow Test Valve MO-2-1501-38B Failed While Securing D LPCI Pump.Caused by Broken Pinion Gear on Valve Operator Motor Shaft | | | 05000237/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000237/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000237/LER-1979-005-03, /03L-0 on 790119: During Normal Operation, Mass Spectometer Leak Detector Downscale Condition Annunciated & High Rad Alarm & Half Scram Occurred Twice on Same Day. Log Rad Monitor Replaced | /03L-0 on 790119: During Normal Operation, Mass Spectometer Leak Detector Downscale Condition Annunciated & High Rad Alarm & Half Scram Occurred Twice on Same Day. Log Rad Monitor Replaced | | | 05000237/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000237/LER-1979-008-03, /03L-0 on 790126: LPCI Min Flow Value MO-2-1501-13A Failed to Close Completely During LPCI Pump Operability Surveillance.Cause of Failure Unknown | /03L-0 on 790126: LPCI Min Flow Value MO-2-1501-13A Failed to Close Completely During LPCI Pump Operability Surveillance.Cause of Failure Unknown | | | 05000237/LER-1979-009-03, /03L-0 on 790121:plant Chimney Sampling Sys Operating Incorrectly.Caused by Purge Valve V2 Being Stuck Open | /03L-0 on 790121:plant Chimney Sampling Sys Operating Incorrectly.Caused by Purge Valve V2 Being Stuck Open | | | 05000237/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000237/LER-1979-010-01, /01T-0 on 790202:section of Blowout Panel Blown Out,Breaching Secondary Containment.Cause Under Investigation | /01T-0 on 790202:section of Blowout Panel Blown Out,Breaching Secondary Containment.Cause Under Investigation | | | 05000237/LER-1979-010, Forwards LER 79-010/01T-0 | Forwards LER 79-010/01T-0 | | | 05000237/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000237/LER-1979-013-03, /03L-0 on 790223:after Diesel Generator Was Manually Started Prior to Taking Transformer Out of Svc, Water Pump Breaker Thermally Tripped & Redundant Power Supply Also Tripped.Cause Unknown | /03L-0 on 790223:after Diesel Generator Was Manually Started Prior to Taking Transformer Out of Svc, Water Pump Breaker Thermally Tripped & Redundant Power Supply Also Tripped.Cause Unknown | | | 05000237/LER-1979-014-03, /03L-0 on 790305:U2 Diesel Generator Failed to Start on First & Fifth Attempts.Caused by Bendix Gear Failure to Engage & Failure of Air Start Solenoid to Energize.Solenoid Was Replaced | /03L-0 on 790305:U2 Diesel Generator Failed to Start on First & Fifth Attempts.Caused by Bendix Gear Failure to Engage & Failure of Air Start Solenoid to Energize.Solenoid Was Replaced | | | 05000237/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000237/LER-1979-015, Forwards LER 79-015/01T-0 | Forwards LER 79-015/01T-0 | | | 05000237/LER-1979-016, Forwards LER 79-016/01T-0 | Forwards LER 79-016/01T-0 | | | 05000237/LER-1979-017-01, X2 for Dresden, Units 2 and 3 Re Inadequacies Observed in Implementation of Administrative Procedural Controls Which Threaten to Cause Reduction of Degree of Redundancy Provided in Reactor Protection System or Engineered Saf | X2 for Dresden, Units 2 and 3 Re Inadequacies Observed in Implementation of Administrative Procedural Controls Which Threaten to Cause Reduction of Degree of Redundancy Provided in Reactor Protection System or Engineered Safety Feature Sys | | | 05000237/LER-1979-017, Forwards LER 79-017/01T-0 | Forwards LER 79-017/01T-0 | | | 05000237/LER-1979-019, Forwards LER 79-019/03L-0 | Forwards LER 79-019/03L-0 | | | 05000237/LER-1979-020-03, /03L-0 on 790413:measured Leakage for Personnel Air Lock Was 54.63 Std Cubic Ft/H.Leakage Identified Through Outer Lower Handwell.Shaft Packing Was Replaced & Air Lock Retested | /03L-0 on 790413:measured Leakage for Personnel Air Lock Was 54.63 Std Cubic Ft/H.Leakage Identified Through Outer Lower Handwell.Shaft Packing Was Replaced & Air Lock Retested | | | 05000249/LER-1979-021-03, /03L-0:on 790821,during Normal Operation,Offgas Monitor 3A Took Step Increase W/No Power Change & hi-hi Trip Light Was On.Caused by Faulty V1 Electrometer Tube,Which Was Replaced.Monitors Will Be Tested Monthly | /03L-0:on 790821,during Normal Operation,Offgas Monitor 3A Took Step Increase W/No Power Change & hi-hi Trip Light Was On.Caused by Faulty V1 Electrometer Tube,Which Was Replaced.Monitors Will Be Tested Monthly | | | 05000237/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000237/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | | | 05000237/LER-1979-023-03, /03L-0 on 790406:during Radioactive Insp,Lack of Fusion Noted in Weld 4-4 on 4-inch Reactor Head Vent Line 2-0215-4.Weld Cut Out & Rewelded Per ASME Boiler & Pressure Vessel Code.Asme Hydrostatic Test Completed | /03L-0 on 790406:during Radioactive Insp,Lack of Fusion Noted in Weld 4-4 on 4-inch Reactor Head Vent Line 2-0215-4.Weld Cut Out & Rewelded Per ASME Boiler & Pressure Vessel Code.Asme Hydrostatic Test Completed | | | 05000249/LER-1979-023-03, /03L-0:on 790823,source Range Monitor Calibr Supplied Rod Block Trip at 1.03E5,exceeding Tech Specs Limit.Caused by Drift & Temp Dependency in Source Range Monitor.Defective Component Not Yet Identified | /03L-0:on 790823,source Range Monitor Calibr Supplied Rod Block Trip at 1.03E5,exceeding Tech Specs Limit.Caused by Drift & Temp Dependency in Source Range Monitor.Defective Component Not Yet Identified | | | 05000237/LER-1979-025, Forwards LER 79-025/03L-0 | Forwards LER 79-025/03L-0 | | | 05000237/LER-1979-026, Forwards LER 79-026/03L-0 | Forwards LER 79-026/03L-0 | | | 05000249/LER-1979-027, Forwards LER 79-027/03L-0 | Forwards LER 79-027/03L-0 | | | 05000237/LER-1979-027-03, /03L-0 on 790502:during Startup,Main Turbine Tripped on High Water Level.Caused by Packing Leak on Isolation Valve for PS-263-60B.Packing Adjusted,Tested & Sys Lineup Returned to Normal | /03L-0 on 790502:during Startup,Main Turbine Tripped on High Water Level.Caused by Packing Leak on Isolation Valve for PS-263-60B.Packing Adjusted,Tested & Sys Lineup Returned to Normal | | | 05000237/LER-1979-027, Forwards LER 79-027/03L-0 | Forwards LER 79-027/03L-0 | | | 05000249/LER-1979-027-03, /03L-0:on 791003,half of Trip Sys Inoperable Due to Lifting of Flooding Magnetrol Switch Leads to Condenser Pit.Switch Leads Reattached.No Precise Cause Found | /03L-0:on 791003,half of Trip Sys Inoperable Due to Lifting of Flooding Magnetrol Switch Leads to Condenser Pit.Switch Leads Reattached.No Precise Cause Found | | | 05000237/LER-1979-028, Forwards LER 79-028/03L-0 | Forwards LER 79-028/03L-0 | | | 05000237/LER-1979-028-03, /03L-0 on 790508:N2 Line Low Temp Alarm Received & Frost Found on Inerting line.A0-2-1601 & Inerting Line Failed Leak Rate Test.Caused by Failure of Temp Recorder at N2 Vaporizer | /03L-0 on 790508:N2 Line Low Temp Alarm Received & Frost Found on Inerting line.A0-2-1601 & Inerting Line Failed Leak Rate Test.Caused by Failure of Temp Recorder at N2 Vaporizer | | | 05000237/LER-1979-029-03, /03L-0 on 790508:DIS 1400-3,pressure Switch 2-1430-1466D Failed to Trip.Caused by Sticky Plunger in Pressure Switch.Switch Removed,Cleaned & Reset to Trip at 94.5 Psig Increasing | /03L-0 on 790508:DIS 1400-3,pressure Switch 2-1430-1466D Failed to Trip.Caused by Sticky Plunger in Pressure Switch.Switch Removed,Cleaned & Reset to Trip at 94.5 Psig Increasing | | | 05000237/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | | | 05000249/LER-1979-030-03, During Scram Testing in Refuel Mode,Substantial Loss of Position Indication Noted for Control Rod Driveline H-9.Caused by Improperly Seated Socket,Suggesting Faulty Electrical pin-socket Alignment | During Scram Testing in Refuel Mode,Substantial Loss of Position Indication Noted for Control Rod Driveline H-9.Caused by Improperly Seated Socket,Suggesting Faulty Electrical pin-socket Alignment | | | 05000249/LER-1979-030, /03X-1 for Dresden Unit 3 Regarding a Supplement to LER 79-30/03L-0 Addressing the Cause and Corrective Actions for the Loss of Position Indication for CRD H-9 | /03X-1 for Dresden Unit 3 Regarding a Supplement to LER 79-30/03L-0 Addressing the Cause and Corrective Actions for the Loss of Position Indication for CRD H-9 | | | 05000237/LER-1979-031-03, /03L-0 on 790509:crack Found on 2D1 Feedwater Emergency Spill to Condenser Line & Crack Located on Pipe to Condenser Weld.Caused by Mechanical Failure.Cracked Portion Removed & Rewelded | /03L-0 on 790509:crack Found on 2D1 Feedwater Emergency Spill to Condenser Line & Crack Located on Pipe to Condenser Weld.Caused by Mechanical Failure.Cracked Portion Removed & Rewelded | | | 05000237/LER-1979-031, Forwards LER 79-031/03L-0 | Forwards LER 79-031/03L-0 | | | 05000237/LER-1979-032, Forwards LER 79-032/03L-0 | Forwards LER 79-032/03L-0 | |
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