05000333/LER-1978-059-03, /03L-0 on 780805:primary Containment Pressure Suppression Pool Level Exceeded Tech Specs Limit by Two Inches.Caused by Operator Failure to Isolate RHR Sys from keep-full Subsys

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/03L-0 on 780805:primary Containment Pressure Suppression Pool Level Exceeded Tech Specs Limit by Two Inches.Caused by Operator Failure to Isolate RHR Sys from keep-full Subsys
ML19270G115
Person / Time
Site: FitzPatrick Constellation icon.png
Issue date: 08/30/1978
From: W. Verne Childs
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19270G110 List:
References
LER-78-059-03L, LER-78-59-3L, NUDOCS 7906040288
Download: ML19270G115 (1)


LER-1978-059, /03L-0 on 780805:primary Containment Pressure Suppression Pool Level Exceeded Tech Specs Limit by Two Inches.Caused by Operator Failure to Isolate RHR Sys from keep-full Subsys
Event date:
Report date:
3331978059R03 - NRC Website

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2 l During routine surveillance testing of the RHR system primary containment i

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o l Operator failed to isolate the RHR system from the " keep full" subsystem durine l

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