LER-1979-020, /03L-0 on 790228:following Reactor Trip,Chem/Rod Sampling Revealed Reactor Coolant Dose Equivalent I-131 Exceeded 1.0 Mci Per Gram,Contrary to Tech Specs.Caused by Spike Following Reactor Trip & Leaking Fuel Pins |
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| 3021979020R03 - NRC Website |
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I U. S. NUCLEAR RECULATORY COM9 TIS $10N NRC PORM 364 EXHIBIT A (7 77)
LICENSEE EVENT REPORT
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(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI
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EVENT DESCm*nON ANO *RCS A8LE CONSEQUENCES h it 2020, following a reactor trip, Chem / Rad sampling revealed that the 1
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contrarv to Technical Specification 3.4.8.
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l Coolant System Purification reduced DEI-131 to acceptable levels.
o g i edundancy N/A.
The DEI-131 was.8771 microcuries per cram at 0205 on I
R 2 March 1979. This is the eleventh occurrence reported under thfs I
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SUPPLEMENTARY INFORMATION Report No.:
50-302/79-020/03L-0 Facility:
Crystal River Unit #3 Report Date:
16 March 1979 Occurrence Date:
28 Febru 1979 Identification of Occurrence:
The Dose Equivalent I-131 was greater than 1.0 microcuries per gram of primary coolant contrary to Technical Specifi-cation 3.4.8.
Conditions Prior to Occurrence:
Mode 3 Operation (Hot Standby)
Description of Occurrence:
At 2020, following a reactor trip, Chem / Rad sampling revealed that the Dose Equivalent I-131 exceeded 1.0 microcuries per gram of primary coolant. Dose Equivalent I-131 was 1.915 microcuries per gram. Action statement of 3.4.8 was entered and the four hour sampling frequency was initiated.
The Dose Equivalent I-131 returned to within acceptable limits at 0205 on 2 March 1979.
Designation of Apparent Cause:
This event was due to an expect,ed transient spike following a reactor trip and known leaking fuel pins.
Analysis of Occurrence:
There was no safety hazard to the plant or general public as sampling demonstrated reducing levels of DEI-131.
The transient was within the capabilities of the plant purification system.
Corrective Action
No corrective action deemed necessary as reactor coolant purification returned the DEI-131 to within acceptable limits.
Failure Data:
This is the eleventh occurrence reported under this Technical Specification.
Reactor Power History of Prior Forty-eight Hours
(
Ites 1 Event Date: 28 February 1979 i
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2-18779,.Y L'
HOUR GMWE TURB G MUTH M
Rr)TIO PAT)D
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(E710)
(T856)
(P753)
(P723)
NI/MT ME/MT W
f. en 2nup
, /,s e r-
/,en
, /,, r n
,. e, r -
m 1
97.04 9906 98.41 99.40 1.010
.956 g
1 2
97.02 9908 98.41 99.30 1.009
.986 cf nnin
~, i ; 1 on 7n i nno eng 6;
7 o-1 4
97.01 9908 98.41 99.20 1.008
.986 1
5 96.97 9915 98.45 99.20 1.008
.985 ci A
c4 o-cosu og u7 oo 7o
- nao e g r-3 7
97.02 9912 98.45 99.50 1.011
.985
.li 8
97.10 9907 98.49 99.50 1.010
.986 1:
o 9_?_,02 on!2 o? ' r oo 7n
! 000 o g '-
(P 10 97.02 9942 98.78 99.40 1.006
.982 C'l 11 96.98 9964 98.94 99.60 1.007
.980 h s' a
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13 96.49 10045 99.27 100.2t' 1.009
.972
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14 96.37 10_057 99.27 100.10 1.008
.971 ha.
o.,77 199 7 00,74 3 ggg ego
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(" 'E 16 96.35 10060 99.27 100.30 1.008
.971 3
17 96.32 10060 99.23 100.00 1.008
.971 20 so er ne 4nnmo no ce i. n 4 nno e,r E
19 96.28 10024 o8.82 99.90 1.011
.974
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13 20 96.30 10019 98.02 100.20
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24 e.
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E 22 96.32 10019 98.82 100.30 3.015
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'3 96.27 10027 98.86 100.00 1.012 974 C W 6-1""'"
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29 ae ar p4 i!.0 AVERAGE DAILY GENERATOR GROS 5 826.26 MUH'E'
- 1 AVERAGE DAILY THERMAL POWER 2423.92 MUH(T)
.n Aurn.ang ria T t y Tttpr>To-nonce p r >
n a--e occa rJ' / e r.i u
.i AVERAGE DAILY MWTH POWER 9E 773 e / c P' l'
AVERAGE DAILY NUCLEAR INST. FOWER o9 725 =/aFF RATIO OF NI TO MUTH = 1.010 it.
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HOUR GMWE TURB G MWTH NI RATIO RATID
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96.29 10021 98.82 99.90 1.011 974 5'
96.34 10016 98.82 99.90 1.011
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4 95.34 10022 95.55 99.9b k.b1k
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5 96.30 10018 98.78 99.90 1.011
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7 96.37 10014 98.82 99.70 1.009
.975
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96.23 10027 98.82 99.70 1.009
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S 10 96.70 10017 99.18 100.30 1.011
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13 96.67 10021 99.18 100.20 1.010
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14 96.67 10028 99.27 100.50 1.012
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17 96.01 10023 98.53 100.20 1.017
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22 96.02 10027 98.57 99.90 1.013
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23 96.04 10024 98.57 99.90 1.013
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AVERAGE DAILY GENERATOR GROSS 798.75 MWH(E) i 2.E AVERAGE DAILY THERMAL POWER 2423.58 MWH(T)
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AVERAGE DAILY MWTH POWER 92.84:
>/*FP II.
AVERAGE DAILY NUCLEAR INST. POWER 100.054 e/ FP E..
RATIO OF NI TO MWTH = 1.012 n
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1 HOUR GMWE TURB G MWTH NI RATIO RAT!D 2'
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NI/MT ME/MT
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1 96.00 10022 98.53 99.90
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96.00 10022 98.53 99.80 1.013
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95.98 10030 98.57 99.50 1.009
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13 95.37 10037 98.53 99.50 1.010
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14 95.79 11122 90.53 99.50 1.010
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22 0.00 0
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I0 AVERAGE DAILY GENERATOR GROSS 572.81 MUH(E)
~, 2 AVERAGE DAILY THERMAL POWEP 1698.25 MUH(T) d
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AVERAGE DAILY MWTH POWEP 69.852 e/aCo 21 AVERAGE DAILY UUCLEAR INST. POUER 60. 'l % e/aCo n
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RATIO OF MI TO MUTH = 1.009 y
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1
Fuel Burnup by Core Region Item 2 Event Dace:
28 February 1979
Item 2 The burnup was calculated at 406.6 EFPD for the four (4) enrichment regions.
REGION NUMBER of FA BURNUP A
52 13,302 MWD /MTU B
60 14,136 MWD /MTU C
61 9,303 MWD /MTP Oconee 4
14,000 MWD /MTU Ave.
12,222 MWD /MTU
8 Clean-up Flow History Item 3 Event Date:
28 February 1979 e
=w
Item 3 Clean-up flow history starting forty-eight (48) hours prior to the first sample in which the limit was exceeded is as follows:
DATE TIME LET DOWN FLOW 2/26/79 0030 47 GPM 2/27/79 0105 47 GPM 2/28/79 0120 47 GPM
History of Degassing Operations For This Report Item 4 Event Date: 28 February 1979 I
se > w e
DEGAS OPERATIONS DATE TABLE TIME 2/27/79 Degassed MUT to WGDT 1345 2/28/79 Degassed Pressurizer 1516 2/28/79 Reactor Trip 1639
Time Duration When DEI-131 Exceeded 1.0 p C1/ gram and I-131 Analysis Results Item 5 Event Date:
28 February 1979 e
,s Item 5 As per Technical Specification 3.4.8 The four (4) hour sampling frequency was initiated at 1820 on 28 February 1979 and the Dose Equivalent I-131 was 1.915 microcuries per gram. The four (4) hour sampling frequency was terminated at 0600, 2 March 1979 when the DEI-131 was determined to be.6732 microcuries per gram. DEI-131 was < 1 u Ci/ gram at 0205, 2 March 1979 when the sample results were.8771 u Ci/ gram.
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| 05000302/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000302/LER-1979-001-03, /03L-0 on 790101:during Operating Daily Surveillance Log Survey (SP-300),noted That Pressure in B Core Flood Tank Was 630 Psi.Caused by Operator Error During Repressurization | /03L-0 on 790101:during Operating Daily Surveillance Log Survey (SP-300),noted That Pressure in B Core Flood Tank Was 630 Psi.Caused by Operator Error During Repressurization | | | 05000302/LER-1979-002-03, /03L-0 on 790102:33 Ft Wind Direction Monitor Was Inoperable.Caused by Wind Direction Sensor Bearing Being Contaminated W/Coal Dust.Sensor Renewed Thru Normal Maint | /03L-0 on 790102:33 Ft Wind Direction Monitor Was Inoperable.Caused by Wind Direction Sensor Bearing Being Contaminated W/Coal Dust.Sensor Renewed Thru Normal Maint | | | 05000302/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000302/LER-1979-003-03, /03L-0 on 790106:during Rx Runback Following Turbine Trip,Main Feedwater Block Valve FWV-30 Did Not Close.Caused by Valve Sticking on Its Back Seat.Corrective Action:Manual Cycling | /03L-0 on 790106:during Rx Runback Following Turbine Trip,Main Feedwater Block Valve FWV-30 Did Not Close.Caused by Valve Sticking on Its Back Seat.Corrective Action:Manual Cycling | | | 05000302/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000302/LER-1979-004-03, /03L-0 on 790115:cable Tunnel Sump Pump Failed to Start During Operability Verification.Maint Restored Sump Pump Operability.Caused Attributed to Failure of Pump | /03L-0 on 790115:cable Tunnel Sump Pump Failed to Start During Operability Verification.Maint Restored Sump Pump Operability.Caused Attributed to Failure of Pump | | | 05000302/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000302/LER-1979-005-01, Discusses Commitment Stated in LER 79-005-01T-1 Re MSIV Valves Not Closing within Design Time of Five Seconds During Double Ended Pipe Rupture.Util Has Determined That Upgrading Air Circuit to Seismic Class I Will Not Be Nec | Discusses Commitment Stated in LER 79-005-01T-1 Re MSIV Valves Not Closing within Design Time of Five Seconds During Double Ended Pipe Rupture.Util Has Determined That Upgrading Air Circuit to Seismic Class I Will Not Be Necessary | | | 05000302/LER-1979-006, Forwards LER 79-006/01T-0 | Forwards LER 79-006/01T-0 | | | 05000302/LER-1979-006-01, /01T-0 on 790201:figures for Transient Limits on Rapid Depressurizations & High Pressure Injection Tests in Disagreement W/Cycle 2 Reload Rept.Tech Specs Will Be Revised | /01T-0 on 790201:figures for Transient Limits on Rapid Depressurizations & High Pressure Injection Tests in Disagreement W/Cycle 2 Reload Rept.Tech Specs Will Be Revised | | | 05000302/LER-1979-007-03, /03L-0 on 790117:reactor Coolant Dose Equivalent I-131 Exceeded 1.0 Mci.Caused by Expected Transient Spikes Following Reactor Trip & Known Leaking Fuel Pins | /03L-0 on 790117:reactor Coolant Dose Equivalent I-131 Exceeded 1.0 Mci.Caused by Expected Transient Spikes Following Reactor Trip & Known Leaking Fuel Pins | | | 05000302/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000302/LER-1979-008-03, /03L-0 on 790119:RC3-GP3-BL4 Light Did Not Extinguish When Test Switch Returned to Off Position.Caused by Dirty Contacts in Relay | /03L-0 on 790119:RC3-GP3-BL4 Light Did Not Extinguish When Test Switch Returned to Off Position.Caused by Dirty Contacts in Relay | | | 05000302/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000302/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000302/LER-1979-009-03, /03L-0 on 790124:while Performing Reactor Protection Sys Functional Testing,Rod Group 6 Dropped Into Core,Rod Group Overlap Was Exceeded.Caused by a AC Power Breaker Being Left Open | /03L-0 on 790124:while Performing Reactor Protection Sys Functional Testing,Rod Group 6 Dropped Into Core,Rod Group Overlap Was Exceeded.Caused by a AC Power Breaker Being Left Open | | | 05000302/LER-1979-010-03, /03L-0 on 790125:during Routine Operations,Air Handling Fan Failed to Start.Caused by Faulty Overcurrent Timing Relay | /03L-0 on 790125:during Routine Operations,Air Handling Fan Failed to Start.Caused by Faulty Overcurrent Timing Relay | | | 05000302/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000302/LER-1979-011-03, /03L-0 on 790210:reactor Coolant Dose Equivalent I-131 Exceeded Tech Spec Limits.Caused by Expected Spike Following Reactor Trip & Known Leaking Fuel Pins.Reactor Coolant Sys Cleanup Returned to Acceptable Limits | /03L-0 on 790210:reactor Coolant Dose Equivalent I-131 Exceeded Tech Spec Limits.Caused by Expected Spike Following Reactor Trip & Known Leaking Fuel Pins.Reactor Coolant Sys Cleanup Returned to Acceptable Limits | | | 05000302/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000302/LER-1979-012-03, /03L-0 on 790214:during Safeguards Test, RB-3GP-2 Light Did Not Illuminate.Caused by Burr on Relay Shaft.Relay Cleaned & Burr Removed | /03L-0 on 790214:during Safeguards Test, RB-3GP-2 Light Did Not Illuminate.Caused by Burr on Relay Shaft.Relay Cleaned & Burr Removed | | | 05000302/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000302/LER-1979-014-03, /03L-0 on 790220:decay Heat Cooler 3A Outlet Remote Shutdown Temp Indicator Inaccurate & Rendered Inoperable.Caused by Failed Resistance Temp Detector (Rtd). RTD Replaced & Sys Recalibr | /03L-0 on 790220:decay Heat Cooler 3A Outlet Remote Shutdown Temp Indicator Inaccurate & Rendered Inoperable.Caused by Failed Resistance Temp Detector (Rtd). RTD Replaced & Sys Recalibr | | | 05000302/LER-1979-015-03, /03L-0 on 790221:fire Svc Tanks 1-B & 1-A Contained Less than Min Volume Required by Tech Specs. Caused by Improper Design.Engineering Evaluation Initiated | /03L-0 on 790221:fire Svc Tanks 1-B & 1-A Contained Less than Min Volume Required by Tech Specs. Caused by Improper Design.Engineering Evaluation Initiated | | | 05000302/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000302/LER-1979-016, Forwards Supplementary Info Re LER 79-016/04X-0 | Forwards Supplementary Info Re LER 79-016/04X-0 | | | 05000302/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000302/LER-1979-017-03, /03L-0 on 790223:heat Trace Recorder for Concentrated Boric Acid Flowpath Was Malfunctioning & Rendered Inoperable.Caused by Failed Recorder Drive Wheel. Drive Wheel Replaced & Heat Trace Recorder Returned to Svc | /03L-0 on 790223:heat Trace Recorder for Concentrated Boric Acid Flowpath Was Malfunctioning & Rendered Inoperable.Caused by Failed Recorder Drive Wheel. Drive Wheel Replaced & Heat Trace Recorder Returned to Svc | | | 05000302/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000302/LER-1979-018-03, /03L-0 on 790301:inner Airlock Door Found Unlatched.Caused by Inadequate Latching Design.Corrective Action Will Be Determined Upon Results of Engineering Info Request | /03L-0 on 790301:inner Airlock Door Found Unlatched.Caused by Inadequate Latching Design.Corrective Action Will Be Determined Upon Results of Engineering Info Request | | | 05000302/LER-1979-019, Forwards LER 79-019/03L-0 | Forwards LER 79-019/03L-0 | | | 05000302/LER-1979-019-03, /03L-0 on 790223:motor Driven Emergency Feedwater Pump Discharge Pressure Gauge EF-2-PI Was Out of Calibr. Caused by Inoperable Dampening Snubber Located in Sensing Line.Snubber Was Replaced | /03L-0 on 790223:motor Driven Emergency Feedwater Pump Discharge Pressure Gauge EF-2-PI Was Out of Calibr. Caused by Inoperable Dampening Snubber Located in Sensing Line.Snubber Was Replaced | | | 05000302/LER-1979-020, Forwards LER 79-020/03L-0 | Forwards LER 79-020/03L-0 | | | 05000302/LER-1979-020-03, /03L-0 on 790228:following Reactor Trip,Chem/Rod Sampling Revealed Reactor Coolant Dose Equivalent I-131 Exceeded 1.0 Mci Per Gram,Contrary to Tech Specs.Caused by Spike Following Reactor Trip & Leaking Fuel Pins | /03L-0 on 790228:following Reactor Trip,Chem/Rod Sampling Revealed Reactor Coolant Dose Equivalent I-131 Exceeded 1.0 Mci Per Gram,Contrary to Tech Specs.Caused by Spike Following Reactor Trip & Leaking Fuel Pins | | | 05000302/LER-1979-021-04, /04L-0 During 1978:difference of More than Two Std Deviations Existed Between Preoperational Study & Operational Study in Metabolic Functions of Discharge Salt Marshes Adjacent to Facility.Cause Natural or Seasonal | /04L-0 During 1978:difference of More than Two Std Deviations Existed Between Preoperational Study & Operational Study in Metabolic Functions of Discharge Salt Marshes Adjacent to Facility.Cause Natural or Seasonal | | | 05000302/LER-1979-021, Forwards LER 79-021/04L-0 | Forwards LER 79-021/04L-0 | | | 05000302/LER-1979-023, Forwards LER 79-023/03L-0 | Forwards LER 79-023/03L-0 | | | 05000302/LER-1979-023-03, /03L-0 on 790308:discovered RCS C1 Concentration Was .17ppm,contrary to Tech Specs.Caused by Appearance of Suspended Solids During Cooldown When Boron Concentration Increased.Purification Sys Reduced Concentration | /03L-0 on 790308:discovered RCS C1 Concentration Was .17ppm,contrary to Tech Specs.Caused by Appearance of Suspended Solids During Cooldown When Boron Concentration Increased.Purification Sys Reduced Concentration | | | 05000302/LER-1979-024-03, /03L-0 on 790315:during Plant Heatup,Discovered That Temp Device at 175 Ft Elevation of Meteorological Monitoring Tower Was Inoperable.Cause Unknown.Temp Device Tested Satisfactorily & Returned to Svc | /03L-0 on 790315:during Plant Heatup,Discovered That Temp Device at 175 Ft Elevation of Meteorological Monitoring Tower Was Inoperable.Cause Unknown.Temp Device Tested Satisfactorily & Returned to Svc | | | 05000302/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000302/LER-1979-026, Forwards LER 79-026/03L-0 | Forwards LER 79-026/03L-0 | | | 05000302/LER-1979-026-03, /03L-0 on 790318:during Reactor Startup,Discovered Absolute Position Indication for Rod 8 Was Inoperable.Caused by Sticking Reed Switch.Variable Ac Frequency,Applied to Reed Switch Circuit,Eliminated Sticking | /03L-0 on 790318:during Reactor Startup,Discovered Absolute Position Indication for Rod 8 Was Inoperable.Caused by Sticking Reed Switch.Variable Ac Frequency,Applied to Reed Switch Circuit,Eliminated Sticking | | | 05000302/LER-1979-027, Forwards Supplemental Info for LER 79-027/04X-0 | Forwards Supplemental Info for LER 79-027/04X-0 | | | 05000302/LER-1979-028, Forwards LER 79-028/03L-0 | Forwards LER 79-028/03L-0 | | | 05000302/LER-1979-028-03, /03L-0 on 790321:while Performing Emergency Feedwater Sys Demonstration,Discovered Pump Discharge Pressure Gauge EF-2-PI Inoperable.Caused by Failed Pressure Gauge.Gauge Replaced | /03L-0 on 790321:while Performing Emergency Feedwater Sys Demonstration,Discovered Pump Discharge Pressure Gauge EF-2-PI Inoperable.Caused by Failed Pressure Gauge.Gauge Replaced | | | 05000302/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | | | 05000302/LER-1979-029-03, /03L-0 on 790321:discovered Makeup Pump 3-C Discharge Stopcheck Valve MUV-2 Was Improperly Positioned. Cause unknown.MUV-2 Reset to Proper Throttle Setting & Returned to Svc | /03L-0 on 790321:discovered Makeup Pump 3-C Discharge Stopcheck Valve MUV-2 Was Improperly Positioned. Cause unknown.MUV-2 Reset to Proper Throttle Setting & Returned to Svc | | | 05000302/LER-1979-031-01, /01T-0 on 790412:during Routine Radwaste Release, Release Monitor Went Into High Alarm Because Radwaste Isolation Valves WDV-320 & 321 Failed to Close.Caused by Sticking Contacts in Monitor Bypass Switch | /01T-0 on 790412:during Routine Radwaste Release, Release Monitor Went Into High Alarm Because Radwaste Isolation Valves WDV-320 & 321 Failed to Close.Caused by Sticking Contacts in Monitor Bypass Switch | | | 05000302/LER-1979-031, Forwards LER 79-031/01T-0 | Forwards LER 79-031/01T-0 | |
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