LER-1979-034, /01T-0 on 790530:diesel Generator Failed to Start During Operability Test.Caused by Failure to Engage of Lower Air Start Bendix Gear.Gear Aligment Will Be Checked After Diesel Generator Tests |
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1 77) 7 LICE.NSEE EVENT REPORT i
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8 bu 61 DOCKET NUMBER 66 6J EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROCABLE CONSEQUENCES O'o lon 5/24/79 with Units 2 and 3 in steady state operation, U 2/3 DG failed to start l
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g 48 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h lBoth events were failure to engage of lower air start bendix gear. After l
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ylower start motor replaced.
Failure to engage occurred several times in l
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Mod. in progress to install multiple air start attempt circuitry, y
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ATTACRMENT TO LICENSEE EVENT REPORT 79-034/0lT-0 COMMONUEALTH EDISON COMPANY (C'JE)
DRESDEN UNIT ILDRS2 DOCKET # 050-237 On 5/24/79 with both Units 2 and 3 in steady state operation, the U 2/3 D/G failed to start during a test to prove operability subs _quent to finding a LPCI injection valve inoperable.
It was observed that the lower bendix gear butted tooth to tooth with the ring gear le failed to engage. A second start immediately following the failure was suc-cessful. Tests performed by maintenance personnel could not repeat the gear abutment. However, on 5/30/79, a similar event occurred when U2/3 D/G failed to start during an opera 5111ty test follcwing a fail-ure of the U2 D/G to properly shutdown (R.O. #79-37/03L-0). U3 was immediately proven operable and an orderly shutdown of Unit 2 commenced.
The safety significance of this event was minimized since offsite power was available at all times.
Both events were caused by the failure to engage of the lower air start bendix gear.
Following the first failure on 5/24/79, 2/3 D/G was successfully started three times.
The failure could not be duplicated.
After the second failure, the lower air start motor was replaced.
It was taken apart and inspected, but no abnormality could be found.
Failures of these motors to engage has occurred in the past.
As a result of these earlier failures the station contacted the vendor to seek a corrective action to prevent recurrence of the air start motors failing to engage.
As a result of that investigation, a modification is pending to the air start circuitry to add a multiple start feature.
The modified system will function by making several attempts at air start motor engagement, before the starting sequence is locked out.
The present system only allows one attempt before the start cir-cuitry locks out on " Failure To Start".
Installation of the modifi-cation will be completed as soon as all parts are available. The frequency of operability testing for the 2/3 DG has been increased to weekly for one month to assure proper operation.
In addition, after each start of the diesel for surveillance testing and until the air start modification is complete, proper alignment of the air start pinions is being verified in accordance with an approved station procedure.
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| 05000237/LER-1979-001-03, /03L-0 on 790103:torus Level Increased to -1 Inch, Due to Repetitive Starts of HPCI Turbine.Increase in Torus Level Determined to Be Result of Inadequate Procedure.Hpci Surveillance Procedures to Be Amended | /03L-0 on 790103:torus Level Increased to -1 Inch, Due to Repetitive Starts of HPCI Turbine.Increase in Torus Level Determined to Be Result of Inadequate Procedure.Hpci Surveillance Procedures to Be Amended | | | 05000237/LER-1979-001, Forwards LER 79-001/03X-1 | Forwards LER 79-001/03X-1 | | | 05000010/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000010/LER-1979-001-03, /03L-0 on 790518:while Digging Ditch for New Pipe, Const Personnel Observed Water Running Into Trench from Proximity of Radwaste return-to-storage Line.Caused by Return Line to 1A Storage Leaking from Aluminum Line | /03L-0 on 790518:while Digging Ditch for New Pipe, Const Personnel Observed Water Running Into Trench from Proximity of Radwaste return-to-storage Line.Caused by Return Line to 1A Storage Leaking from Aluminum Line | | | 05000010/LER-1979-002-03, /03L-0 on 780825:during Monthly Surveillance DI5 5400-2,offgas Monitor 1 Tripped at Greater than 100%, Which Is Not within Setpoint Limit.Caused by Instrument Drift.Setpoint Recalibr | /03L-0 on 780825:during Monthly Surveillance DI5 5400-2,offgas Monitor 1 Tripped at Greater than 100%, Which Is Not within Setpoint Limit.Caused by Instrument Drift.Setpoint Recalibr | | | 05000010/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000237/LER-1979-002, Forwards LER 79-002/01X-1 | Forwards LER 79-002/01X-1 | | | 05000237/LER-1979-002-01, /01X-1 on 790103:during Normal Operation,Hpci Turbine Failed to Start During Quarterly Flow Test.Caused by Partial Engagement of Interlock Dump Valve Operating Lever. 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Under Investigation | | | 05000237/LER-1979-010, Forwards LER 79-010/01T-0 | Forwards LER 79-010/01T-0 | | | 05000237/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000237/LER-1979-013-03, /03L-0 on 790223:after Diesel Generator Was Manually Started Prior to Taking Transformer Out of Svc, Water Pump Breaker Thermally Tripped & Redundant Power Supply Also Tripped.Cause Unknown | /03L-0 on 790223:after Diesel Generator Was Manually Started Prior to Taking Transformer Out of Svc, Water Pump Breaker Thermally Tripped & Redundant Power Supply Also Tripped.Cause Unknown | | | 05000237/LER-1979-014-03, /03L-0 on 790305:U2 Diesel Generator Failed to Start on First & Fifth Attempts.Caused by Bendix Gear Failure to Engage & Failure of Air Start Solenoid to Energize.Solenoid Was Replaced | /03L-0 on 790305:U2 Diesel Generator Failed to Start on First & Fifth Attempts.Caused by Bendix Gear Failure to Engage & Failure of Air Start Solenoid to Energize.Solenoid Was Replaced | | | 05000237/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000237/LER-1979-015, Forwards LER 79-015/01T-0 | Forwards LER 79-015/01T-0 | | | 05000237/LER-1979-016, Forwards LER 79-016/01T-0 | Forwards LER 79-016/01T-0 | | | 05000237/LER-1979-017-01, X2 for Dresden, Units 2 and 3 Re Inadequacies Observed in Implementation of Administrative Procedural Controls Which Threaten to Cause Reduction of Degree of Redundancy Provided in Reactor Protection System or Engineered Saf | X2 for Dresden, Units 2 and 3 Re Inadequacies Observed in Implementation of Administrative Procedural Controls Which Threaten to Cause Reduction of Degree of Redundancy Provided in Reactor Protection System or Engineered Safety Feature Sys | | | 05000237/LER-1979-017, Forwards LER 79-017/01T-0 | Forwards LER 79-017/01T-0 | | | 05000237/LER-1979-019, Forwards LER 79-019/03L-0 | Forwards LER 79-019/03L-0 | | | 05000237/LER-1979-020-03, /03L-0 on 790413:measured Leakage for 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79-026/03L-0 | | | 05000249/LER-1979-027, Forwards LER 79-027/03L-0 | Forwards LER 79-027/03L-0 | | | 05000237/LER-1979-027-03, /03L-0 on 790502:during Startup,Main Turbine Tripped on High Water Level.Caused by Packing Leak on Isolation Valve for PS-263-60B.Packing Adjusted,Tested & Sys Lineup Returned to Normal | /03L-0 on 790502:during Startup,Main Turbine Tripped on High Water Level.Caused by Packing Leak on Isolation Valve for PS-263-60B.Packing Adjusted,Tested & Sys Lineup Returned to Normal | | | 05000237/LER-1979-027, Forwards LER 79-027/03L-0 | Forwards LER 79-027/03L-0 | | | 05000249/LER-1979-027-03, /03L-0:on 791003,half of Trip Sys Inoperable Due to Lifting of Flooding Magnetrol Switch Leads to Condenser Pit.Switch Leads Reattached.No Precise Cause Found | /03L-0:on 791003,half of Trip Sys Inoperable Due to Lifting of Flooding Magnetrol Switch Leads to Condenser Pit.Switch Leads Reattached.No Precise Cause Found | | | 05000237/LER-1979-028, Forwards LER 79-028/03L-0 | Forwards LER 79-028/03L-0 | | | 05000237/LER-1979-028-03, /03L-0 on 790508:N2 Line Low Temp Alarm Received & Frost Found on Inerting line.A0-2-1601 & Inerting Line Failed Leak Rate Test.Caused by Failure of Temp Recorder at N2 Vaporizer | /03L-0 on 790508:N2 Line Low Temp Alarm Received & Frost Found on Inerting line.A0-2-1601 & Inerting Line Failed Leak Rate Test.Caused by Failure of Temp Recorder at N2 Vaporizer | | | 05000237/LER-1979-029-03, /03L-0 on 790508:DIS 1400-3,pressure Switch 2-1430-1466D Failed to Trip.Caused by Sticky Plunger in Pressure Switch.Switch Removed,Cleaned & Reset to Trip at 94.5 Psig Increasing | /03L-0 on 790508:DIS 1400-3,pressure Switch 2-1430-1466D Failed to Trip.Caused by Sticky Plunger in Pressure Switch.Switch Removed,Cleaned & Reset to Trip at 94.5 Psig Increasing | | | 05000237/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | | | 05000249/LER-1979-030-03, During Scram Testing in Refuel Mode,Substantial Loss of Position Indication Noted for Control Rod Driveline H-9.Caused by Improperly Seated Socket,Suggesting Faulty Electrical pin-socket Alignment | During Scram Testing in Refuel Mode,Substantial Loss of Position Indication Noted for Control Rod Driveline H-9.Caused by Improperly Seated Socket,Suggesting Faulty Electrical pin-socket Alignment | | | 05000249/LER-1979-030, /03X-1 for Dresden Unit 3 Regarding a Supplement to LER 79-30/03L-0 Addressing the Cause and Corrective Actions for the Loss of Position Indication for CRD H-9 | /03X-1 for Dresden Unit 3 Regarding a Supplement to LER 79-30/03L-0 Addressing the Cause and Corrective Actions for the Loss of Position Indication for CRD H-9 | | | 05000237/LER-1979-031-03, /03L-0 on 790509:crack Found on 2D1 Feedwater Emergency Spill to Condenser Line & Crack Located on Pipe to Condenser Weld.Caused by Mechanical Failure.Cracked Portion Removed & Rewelded | /03L-0 on 790509:crack Found on 2D1 Feedwater Emergency Spill to Condenser Line & Crack Located on Pipe to Condenser Weld.Caused by Mechanical Failure.Cracked Portion Removed & Rewelded | | | 05000237/LER-1979-031, Forwards LER 79-031/03L-0 | Forwards LER 79-031/03L-0 | | | 05000237/LER-1979-032, Forwards LER 79-032/03L-0 | Forwards LER 79-032/03L-0 | |
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