05000348/LER-1979-057-03, /03L-0:on 791122,steam Generator B Level Channel 486 Declared Inoperable Due to High Reading.Caused by Instruments Equalizing Valve Leaking.Valve Tightened,Tested & Returned to Operation

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/03L-0:on 791122,steam Generator B Level Channel 486 Declared Inoperable Due to High Reading.Caused by Instruments Equalizing Valve Leaking.Valve Tightened,Tested & Returned to Operation
ML19256G016
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 12/19/1979
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19256G012 List:
References
LER-79-057-03L, LER-79-57-3L, NUDOCS 7912270228
Download: ML19256G016 (1)


LER-1979-057, /03L-0:on 791122,steam Generator B Level Channel 486 Declared Inoperable Due to High Reading.Caused by Instruments Equalizing Valve Leaking.Valve Tightened,Tested & Returned to Operation
Event date:
Report date:
3481979057R03 - NRC Website

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g,J ya Up TNUV;lEH C.1 GJ LVtNT DATE 74 73 HEPo'tT DATE 00 EVENT Of SCnlPTION AND FROSASLE cONSEC',.;ENCES h [oTT]lAt 1130 on 11/22/79, Steam Generator B level channel 486.was declared inoperable due l

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Tech. Spsc. 3.3.1.1,in part, requires S.G. B level channel 486 to be l

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Tech. Spec. 3. 3.1.1 action statement requirements were met.

The health andg c,, c l safety of the public were not affected by this event.

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lii: !lThis event uas caused bv the instruments emializine valve lenin 2: subsaouentiv the i

ti i i I valve was tichtened and the channel was returned to operation at 0200 on 11/23/70 1

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