LER-1979-016, /03L-0:on 791003,emergency Diesel Generator 3D Failed to Start for Monthly Tech Spec Test.Caused by Sticking of Woodward UG8 Dial Control Governor Load Limit Strap in Stop Position.Governor Replaced |
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| 2661979016R03 - NRC Website |
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N6;C FORM 366 U. S. NUCLEAR REGULATORY COMMISSION (7 77t LICENSEE EVENT REPORT CONTROL BLOCK: l l
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2 At 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br />, 10-3-79, the 3D emergency Diesel cenerator (one of two) l l failed to start fcr its montaly technical specification test.
The 4D l
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The 3D Diesel I
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ggenerator was restored to service at 1720 hours0.0199 days <br />0.478 hours <br />0.00284 weeks <br />6.5446e-4 months <br />, 10-3-79, after comple-l o
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- 3 34 35 36 3e 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i io lThe GM Electromotive Division 999-20 Diesel canerator failed to start i
It it Ilbecause the Woodward UG8 dial control governor (bulletin no. 03004G)
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] load limit strap stuck in the stop position.
The faulty governor was I
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- - 2 ATTACHMENT TO LICENSEE EVENT REPORT NO. 79-016/03T-0 Wisconsin Electric Power Company Point Beach Nuclear Plant Unit 1 Docket No. 50-266 At 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br />, October 3, 1979, the 3D emergency Diesel generator (one of two) failed to start for its monthly Technical Specification test. The 4D emergency Diesel gen-erator was immediately tested to verify its operability.
The GM Electromotive Division 999-20 Diesel generator failed to start because the Woodward UG8 dial control governor (bulletin or catalogue no. 03004G) load limit strap stuck in the stop or shutdown position.
This governor had been recently installed as a replace-ment for the identical original governor for preventive maintenance.
There were no known problems with the original governor, but it had been in service since the original installation of the Diesel generator and it was felt that it should be replaced as a precautionary measure.
The replacement governor had been ordered from the manufacturer and was a rebuilt unit.
When the replacement governor was initially installed, the load limit strap did stick in the shutdown position on one occasion.
The replacement governor was then removed, disassembled, inspected, reassembled, and installed.
The problem did not recur during ceveral pre-service retests and the Diesel was then placed into service.
When the replacement governor failed on October 3,
- 1979, the original governor was still on site and was reinstalled.
After the Diesel generator successfully completed the monthly Technica.; Specification test, it was returned to service at 1720 hours0.0199 days <br />0.478 hours <br />0.00284 weeks <br />6.5446e-4 months <br />, October 3, 1979.
The factory replacement governor has been returned to the manufacturer.
The event led to a degraded mode of operation (reduced degree of redundancy) permitted by the Technical Specifications.
The public health and safety was not affected due to the operability of the 4D emergency Diesel generator 1269 346
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| 05000301/LER-1979-001-01, /01T-0 on 790219:w/unit off-line & at 10% Steam Flow,A&B Main Steam Stop Valves Failed to Close.Caused by Deposits on Valve Shafts or Hardening of Gland Packing. Valves Were Exercised & Packing Adjusted | /01T-0 on 790219:w/unit off-line & at 10% Steam Flow,A&B Main Steam Stop Valves Failed to Close.Caused by Deposits on Valve Shafts or Hardening of Gland Packing. 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Forwards LER 79-011/01T-0 | Forwards LER 79-011/01T-0 | | | 05000266/LER-1979-011-01, /01T-0:on 790804,while Proceeding to Cold Shutdown Condition,Containment Integrity Was Briefly Violated.Caused by Faulty Interlock Allowing Inside Containment Door to Open When Outside Door Was Already Open | /01T-0:on 790804,while Proceeding to Cold Shutdown Condition,Containment Integrity Was Briefly Violated.Caused by Faulty Interlock Allowing Inside Containment Door to Open When Outside Door Was Already Open | | | 05000266/LER-1979-012-01, /01T-0 on 790805:primary to Secondary Leak Noted in Steam Generator A.Caused by Defective Tubes in Steam Generators a & B.Leaking & Defective Tubes Plugged | /01T-0 on 790805:primary to Secondary Leak Noted in Steam Generator A.Caused by Defective Tubes in Steam Generators a & B.Leaking & Defective Tubes Plugged | | | 05000266/LER-1979-012, Forwards LER 79-012/01T-0 | Forwards LER 79-012/01T-0 | | | 05000266/LER-1979-013-01, /01T-0:on 790830,Unit 1 Taken Off 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05000266/LER-1979-015, Forwards LER 79-015/01T-0 | Forwards LER 79-015/01T-0 | | | 05000266/LER-1979-015-01, /01T-0:on 791002,during Normal Power Operation, Loose Tube Fitting Discovered on Common Line from containment-to-containment Pressure Transmitters.Cause Undetermined.Fitting Tightened | /01T-0:on 791002,during Normal Power Operation, Loose Tube Fitting Discovered on Common Line from containment-to-containment Pressure Transmitters.Cause Undetermined.Fitting Tightened | | | 05000266/LER-1979-016-03, /03L-0:on 791003,emergency Diesel Generator 3D Failed to Start for Monthly Tech Spec Test.Caused by Sticking of Woodward UG8 Dial Control Governor Load Limit Strap in Stop Position.Governor Replaced | /03L-0:on 791003,emergency Diesel Generator 3D Failed to Start for Monthly Tech Spec Test.Caused by Sticking of Woodward UG8 Dial Control Governor Load Limit Strap in Stop Position.Governor Replaced | | | 05000266/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | | | 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