LER-1979-104, /03L-0:on 791028,remote Shutdown Indicator for Decay Heat Cooler Outlet Temp DH-40-TI Was Inoperable.Caused by Loose Precision Resistor Assembly.Resistor Bridge Assembly Tightened & DH-40-TI Returned to Svc |
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reported that the rethote shutdown indicator for "B" decay heat cooler outlet
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No effect opon the plant or general.public.
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Reference LER 79-095.
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gThe cause of this event is attributed to a loose precision resistor assenbiv.
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DH-40-TI was returned to service at 0900 on 2 November 1979.
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REI 79-10-11 has been initiated to evaluate decav heat remote shutdown indicationi
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SUPPLEMENTARY INFORMATION Report No.:
50-302/79-104/03L-0 Facility:
Crystal River Unit #3 Report Date:
20 November 1979 Occurrence Date:
28 October 1979 Identification of Occurrence:
Remote shutdown indicator for "B" decay heat cooler outlet temperature DH-40-TI inoperable, contrary to Technical Speci-fication 3.3.3.5.
Conditions Prior to Occurrence:
Mode 1 power operation (100%).
Description of Occurrence:
At 0400 during the performance of Daily Operating Surveillance SP-300 it was reported that the remote shutdown indicator for "B"
acay heat cooler outlet temperature, DH-40-TI was inoperable.
It was discover 9d that DH-40-TI (103*F) was inconsistent with redundant Control Room indicator DH-2-TI-2 (95*F) and "B" decay heat pump suction indicator DH-6-TI-2 (80 F).
Maittenance restored operability and DH-40-TI was returned to service at 0900 on 2 November 1979.
Designation of Apparent Cause:
The cause of this event is attributed to a loose precision resistor bridge assembly. The resistor bridge assembly was tightened and DH-40-TI was returned to service.
Analysis of Occurrence:
No effect upon the plant or general public.
Corrective Action
REI 79-10-11 has been initiated to evaluate decay heat remote shutdown temperature indication. Further corrective action will be based upon the results of this evaluation and submitted as a supplement to this report.
Failure Data:
This is the second occurrence reported for DH-40-TI.
Reference LER 79-095.
/rc 1444078
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/03L-0 on 790214:during Safeguards Test, RB-3GP-2 Light Did Not Illuminate.Caused by Burr on Relay Shaft.Relay Cleaned & Burr Removed | /03L-0 on 790214:during Safeguards Test, RB-3GP-2 Light Did Not Illuminate.Caused by Burr on Relay Shaft.Relay Cleaned & Burr Removed | | | 05000302/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000302/LER-1979-014-03, /03L-0 on 790220:decay Heat Cooler 3A Outlet Remote Shutdown Temp Indicator Inaccurate & Rendered Inoperable.Caused by Failed Resistance Temp Detector (Rtd). 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