ML19253B660
| ML19253B660 | |
| Person / Time | |
|---|---|
| Site: | Crane |
| Issue date: | 06/20/1974 |
| From: | Davis A, Spessard R, Sternberg D NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML19253B649 | List: |
| References | |
| 50-289-74-25, NUDOCS 7910160746 | |
| Download: ML19253B660 (20) | |
See also: IR 05000289/1974025
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U.S. ATO !IC ENERGY COM:!ISSION
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DIRECTORATE OF REGUL\\ TORY OPERATIONS
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REGION I
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fic Inspection Report No:
50-289/74-25
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Docket No:
50-289
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Licensee:
Metropolitan' Edison Company
License No:
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Three lille Island Unit l'
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Priority:
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Category:
B-2
Location:
Middletown, Pennsylvania
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Typa of Licensee:
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Type of Inspection:
Routine, Announced
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Dates of Inspect ~ ion:
June 3 through June 6, 1974
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Dates of Previous Inspection:
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Reporting Inspector
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R. L.,Spessard,' Reactor I.nspector
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Accompanying Ir.spectors:
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D. M. Sternberg, Reactor Inspector
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W. A. Ruhlman, Reactor Inspector
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Date
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Other Accompanying Personnel:
A. B. Davis, Senior Reactor Inspector
(June 4&5,
Date
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Reviewed By:
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A. B. Davis, Senior Reactor Inspector
D'a t e
q9101607y[
Reactor Operations Branch
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SUFSIARY OF FINDIMCS
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Fnforcement Action
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Violations
1.
Contrary to the requirements of the FSAR Section lA, Operating
Quality Assurance Plan Section VI, the Makeup and Purification
System and the Decay Heat Removal System were lined up with
superseded operating procedures.
(Details 13.e. (1) and (2))
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2. Contrary to the requirements of the FS AR Section lA, Operating
Quality Assurance Plan,Section VI, the Waste Gas Disposal
System was lined up with a procedure-containing unauthorized
changes.
(Detail 13.e.(3))
Safety
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None Identified
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Licensee Action on Previously identified Enforcement Items
Not Inspected
Unusual Occurrences
A.
Superseded valve checklists and startup checklists were used during
the course of plant startup.
(A0 74-7, lht Ed Telegram dated June
,
6, 1974 to Director, DRO, RO:I).
(Detail 13.e)
B.
A socket weld leak was discovered on the discharge header of the
reactor coolant system makeup pumps.
(A0 74-6, lht Ed Telegram
dated June 4, 1974 to Director, DRO, RO:1).
(Detail 5)
C.
A pinhole sized leak was discovered in the "B" Makeup Pump recircu-
lation flow orifice (A0 74-5, Fht Ed Telegram dated June 3,1974 to.
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Director, DRO, RO:I).
(Detail 4)
D.
The "C" tbkeup Pump sustained severe damage during operation.
(Detail 6)
E.
The Sodium Thiosulfate Tank was diluted with Sodium Hydroxide during
recirculation of the Sodium Hydroxide Tank.
(Detail 7)
F.
A burned terminal was discovered on one of the control rod drive
power transformers.
(Detail 12)
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Other Sinnificant Findings
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A.
Current
1.
Initial Criticality
a
The inspectors witnessed the initial criticality event which
was accomplished in an orderly and controlled manner in
accordance with the procedure.
Criticality was achieved at
10:36 pm on June 5,1974, and the actual critical conditions
were in close agreement with the predicted values.
(Detail
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13.u)
2.
The Sodium Thiosulfata Tank is now operable.
(Detail 7)
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3.
Repairs and testing of the control rod drive system have been
completed.
(Detail 8)
"14.
Design changes to both Diesel Generators have been completed
using approved maintenance procedures.
(Detail 9)
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5.
The reactor . building sump and feeder drains were observed to be
clean and free of debris.
(Detail 10)
B.
Status of Previousiv Reported Unresolved Items
1.
The following items are resolved:
A procedure has been implemented which describes the
a.
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actions to be taken to indicate the status of out of
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servicc/ calibration gauges, meters and instruments.
(Detail 11)
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b.
The discrepancies noted in the implementation of the
surveillance t - program have been corrected.
(Detail 13.e)
The licensee's review and evaluation of the Diesel
c.
Generator circuitry design changes has been completed.
(Detail 9)
C.
New Unresolved Items
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None Identified
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Management Interview
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An exit interview was held onsite on June 6, 1974, at the conclusion of
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the inspection with the following attendecs:
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Metropolitan Edison Company
Mr. J. G. Herbein, Station Superintendent
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Mr. J. R. Floyd, Supervisor of Operations
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Mr. W. E. Potts, Supervisor of Quality Control
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Mr. J. J. Colitz, Station Engineer
Mr. J. P. O'Hanlon, Nuclear Engineer
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Mr. C. E. Hartman, Electrical Engineer
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Mrr R. L. Summers, Junior Engineer
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General Public Utilities Service Corporation
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Mr. R. J. Toole, Assistant Test Superintendent
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The following summarizes items discussed.
A.
Preoperational Test Program (Detail 2)
B.
Initial Startup Test Program (Detail 3)
C.
Followup Action - A0 74-6 (Detail 5)
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D.
Followup Action - A0 74-5 (Detail 4)
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E.
Follovup Action - A0 74-4 (Detail 8)
F.
Followup Action - A0 74-3 (Detail 9)
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G.
Sodium Thiosulfate Tank Status (Detail 7)
H.
Reactor Building Sump (Detail 10)
I.
Instrument Status Indication (Detail 11)
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Inspectors' Witness of Initial Criticality and the observed
violations (Detail 13)
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Loss of the "C" Makeup Pump (Detail 6)
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Burned terminal on control rod drive power transformer (Detail 12)
In each area listed above, the licensee representatives acknculedged the
inform. tion presented by the inspectors.
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DETAILS
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1.
Persons Contacted On Site
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Metropolitan Edison Company (Met Ed)
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Mr. T. H. Acker, Control Room Operator
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Dr. T. S. Baer, Station Engineer
Mr. J. C. Banks, Control Room Operator
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Mr. M. L. Beers, Shift Foreman
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$2?? Mr. D. J. Boltz, Control Room Operator
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Mr. R. R. Booher, Auxiliary Operator
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Mr. T. L. Book, Control Room Operator
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Mr. N. D. Brown, Control Room Operator
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Mr. K. P. Bryan, Control Room Operator
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Mr. E. E. Bulmer, Mechanical Engineer
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Mr. H. L. Carr, Jr. , Auxiliary Operator
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Mr. J. J. Colitz, Station Engineer
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Mr. W. W. Cotter, Mechanical Engineer
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Mr. T. L. Crouse, Control Room Operator
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Mr. J. H. Deman, Radiation Chemistry Technician
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Mr. J. R. Floyd, Supervisor of Operations - Unit 1
Mr. A. C. Fredlund, Control Room Operator
Mr. B. C. Getty, Mechanical Engineer - Unit 2
Mr. C. F. Gilbert, Supervisor of Operations - Unit 2
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Mr. K. L. Harner, Radiation Chemistry Technician
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Mr. R. R. Harper, Instrumen't Foreman
Mr. C. E. Hartman, Electrical Engineer
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Mr. R. A. Heilman, Control Roca Operator
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Mr. J. G. Herbein, St.ation Superintendent
Mr. J. F. Hilbish, Project Engineer - Nuclear
Mr. G. R. Hitz, Control Room Operator
Mr. R. S. Hutchison, Auxiliary Operator
Mr. I. P. Hydrick, Shift Foreman
Mr. C. W. Keyser, Control Room 6perator
Mr. B. A. Mehler, C]ntrol Room Operator
Mr. R. P. }Eller, Test Coordinator
Mr. L. G. Noll. Control Room Operator
Mr. J. P. O'Hanlon, Nuclear Engineer
Mr. W. E. Perks, Shift Foreman - Unit 2
Mr. J. F. Peters, Administrator
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4 A 5 '.101
Mr. E. L. Pilsitz, Control Room Operator
Mr. R. H. Porter, Shift Supervisor
Mr. C. E. Randolf, Engineering Assistant
Mr. R. A. Rice, Security Specialist
Mr. M. J. Ross, Shif t Supervisor
Mr. D. M. Shovlin, Supervisor of Mait:t*7ance
Mr. B. G. Smith, Shift Foreman
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Mr. J. R. Smith, Shif t- Supervisor
Mr. R. L. Summers, Junior Engineer
tk. J. H. Thomas, Coordinator of Services
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Mr. R. P. Velez, Radiation Chemistry Technician
Mr. G.i C. Wallace, Shif t Supervisor
}k. D. E. Weaver, Instrument Foreman
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Mr. H. L. Wilson, Instrument Foreman
Mr. W. H. Zewe, Shift Foreman
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Ceneral Public Utilities Service Corporation (CPUSC)
5[N1- Mr. J. J. Barton, Startup and Test
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..ac i Mr. W. H. Behrle, Shif t Test Director
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Mr. L. E. Eriggs, Startup Engineer
Mr. H. C. Eisnaugle, Project Administrator
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Mr. C. E. Gatto, Shif t Test Engineer
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Mr. T. M. Hawkins, Shift Test Engineer
Mr. G. P. Miller, Test Superintendent
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- p=, Mr. M. A. Nelson, Technical Engineer
- Mr. S. G. Poje, Shift Test Engineer
Mr. I. D. Porter, Shif t Test Engineer
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Mr. J. J. Stromberg, Site Auditor
Mr. R. J. Toole, Assistant Test Superintendent
Mr. J. E. Wright, Site QA Manager
Mr. L. M. Zubey, Mechanical Engineer
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Babcock and Wilcox Nuclear Services
Mr. J. H. Flint , Shift Data Analyst
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Mr. R. A. Govers, Engineer
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Mr. E. R. Kane, Engineer
Mr. J. A. Middleton, Engineer
Mr. M. B. Owen, Engineer
Mr. W. E. Schaid, Shift Data Analyst
NUS Comoany
Mr. J. D. Trotter, Consultant
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2.
Preoperational Test Program
The inspector reviewed TWG bbeting minutes for the period iby 29 -
June 4, 1974 (Meetings 110-115), completed test results (of ficial
Field Copy), and the approved Prerequisite List for Initial
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Criticality.
Additionally, the licensce's written safety evalua-
tions made pursuant to 10 CFR 50.59 for not completing certain
preoperational tests as described in the FSAR were reviewed on a
sampling basis (included TP 120/1, 2 and 3, TP 360/lA, TP 230/8, SP
102.6 and F1104/6).
The following information was obtained:
a.
Prooperational Testing Status
Tests Completed and Accepted
88%
Tests Partially Completed and Accepted
8%
Tests Not Completed
4%
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The licensee evaluated the overall results of the preopera-
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tional test program and concluded that the program was suf-
ficiently complete to support (relative to safety) initial
criticality.
Tests not to be completed prior to initial
criticality were previously reported in Report 50-289/74-23,
Detail 7.a.
Additionally, the following tests were not
completed:
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(1) TP 600/25, Hydrogen Addition Test
(2) TP 600/26, Degasification Test
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Tests (1) and (2)' above are to be deleted from the MTX
on the baeis that the test objectives were accomplished
by Met Ed Operating Procedures.
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(3)
TP 271/4, l'ain and Auxiliary System Functional Test
(4)
TP 600/11, Emergency Feed System and OTSC Level Control
Test
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Tests (3-) and (4) above have been partially ccmpleted and
accepted by the licensec.
The outstanding items relate
to the turbine driven cmcrgency feedwater pump which was
inoperable (needed new shaft).
Testing to be completed
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prior to reaching 5% of full power (Tech Specs require
this pump prior to reaching 5% of Full Power).
(5) TP 600/30, Hot Functional Test Checkpoints
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This test had been partially completed and ecepted by the
licensee.
The outstanding item related to the Ibin Steam
Isolation Valve Support System which did not have contact
on every valve because design temperature had not been
reached.
Testin6 to be completed prior to reaching 5% of
full power.
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The inspector has no further questions relative to the pre-
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operational test program at this time.
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b.
Test Results
The inspector verified that the test results for the proce-
dures listed below had been accepced by the licensee unless
otherwise indicated.
Included in the inspector's review (on
a sampling basis) was the licensee's disposition of identi-
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fied test exceptions and deficiencies and comparison of test
data with acceptance criteria.
No deficiencies were identi-
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fied.
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(1) TP 151/1, Reactor Building Isolation Valve Leak Tests
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(2)
TP 600/4, Makeup and Purification System Operational Test
The inspector observed that the letdown isolation valve
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(MU-V3) had been successfully retested.
This item is
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closed.
(Report 50-289/74-08, Detail 6.a)
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(3)
F1104/15A, Auxiliary Building and' Fuel Handling Building
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Ventillation Functional Verification
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(4)
TP 360/2, Area Radiation Monitors Calibration and
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Functional Test
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(5)
TP 310/3, E.S. Detection and Actuation Test
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(6)
TP 305/2, Reactor Protection System Response Time Test
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(7)
SP 320/4, ICS - Turbine Interface Test
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(8)
TP 301/2, N.I. Detector Cabling and Response Tests
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(9)
TP 301/3D, N.I. Determination and Setting of Detector
Voltages
(10) SP-2, Filter Efficiency Tests
(11) TP 360/lB, Process Radiation Monitors Calibration and
Functional Tests - Atmospheric
(12) TP 360/1C, Procc as Radiation Monitors Calibration and
Functional Tests - Liquid
(13) TP 600/5, Nuclear Chemical Addition and Sampling System
Operational Test
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(14) TP 600/28, Controlling Procedure for Hot Functional
Testing
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(15) TP 600/13, Pressurizer Operation and Spray Flow Test
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Results cf this test had been partially accepted *.iith one
open item relative to setting the pressurizer spray bypass
valve.
This item was accomplished prior to approach to
initial criticality.
The inspector observed that the above tests had been cerducted
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and accepted in accordance with the licensee's commitments to
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RO:1.
(Met Ed letter dated April 19, 1974 to the Director,
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DRO, RO:I and Reports 50-289/74-17, Detail 5.b and 50-289/74-18,
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Details 2 and 3).
3.
Initial Startuo Test Program
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Procedures
The inspector reviewed the following procedures and verified
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that previous RO:I comments had been included in accordance
with the licensee's commitments.
(Report 50-289/74-18,
Detail 7.b. Items (5), (9) and (10))
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(1)
TP 800/5, Reactivity Coefficients at Power
(2)
TP 800/32, Loss of Offsite Power Test
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(3) TP 800/34, Generator Trip Test
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b.
Test Results
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(1)
Detailed Review by RO:I
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The. inspector conducted a detailed review of the completed
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procedures (Official Field Copy) listed below.
The
licensee had accepted the results of these tests.
Test
results met the acceptance criteria, and all test require-
ments were satisfactorily performed.
(a)
TP 200/11D, Reactor Coolant Pump Flow Test - Hot,
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With Core
The inspector observed that final balancing of the
reactor coolant pumps had been completed and that
data indicated frame and shaft vibrations met the
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accept.7nce criteria'.
This item is closed.
(Report
50-2S9/.74-08, Detail 6.f)
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(b) TP 200/12D, Reactor Coolant Flow Coastdcwn Test -
Hot, With Core
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The inspector observed that TCN-2 to this procedure
was approved by the TWG on >by 29, 1974, in accor-
dance with the requirements of Test Instruction
No. 9.
This TCN, which permitted tripping the
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fastest and slowest rods at the same time by re-
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patching (Hot, No Flow Trip Test), was made to
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provide easier control of reactor coolant system
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temperature by minimizing reactor coolant pump
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starts and steps.
These tests and the Hot, Full
Flow Trip Tests were conducted following repairs
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to the damaged CRD system equipment (A0 74-4).
(2) Verification by RO:I
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The inspector verified by review of the completed pro-
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cedure (Official Field Copy) that the results of TP 302/
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2C In-Core Detector Post - Installation Electrical Test
had been accepted by the licensee.
c.
SP 710/2 - Controlling Procedure for Post Core Load Precritical
Testing
The inspectors reviewed this procedure (Official Field Copy)
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which was being conducted and which was a prerequisite for
beginning the approach to initial criticality (TP 710/1).
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The TWG reviewed the status of this procedure prior to sign-
off of the Prerequisite List for Initial Criticality, and the
inspectors' verified that the outstanding items frca this pro-
cedure, as identified in the Prerequisite List, were completed
prior to starting TP 710/1.
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The results of heat loss test for the pressurizer were discussed
with licensee representatives who provided the following infor-
mation:
Modifications to the insulation showed no f mprovements
over previously observed conditions.
The excessive heat loss
was not considered an operating problem; however, for econcay
reasons the matter was still being reviewed.
Valve RC-V2 was
operating satisfactorily; however, a larger motor crerator is
to be installed.
The inspector has no further questions on
this matter at this time.
(Report 50-289/74-08, Detail 6.c).
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4.
Followuo Action A0 74-5
During a previc-
RO inspection (Report 50-289/74-23, Detail 2), the
inspector veri: 2d that the licensee had established a program for
inspecting bbkeup and Purification System Orifices.
The licensee
reported by telephone on May 31, 1974, and by telegram on June 3,
1974, that a pinhole sized leak had developed in the "B" Fbkeup
pump recirculation flow orifice.
This pump was in service and the
reactor coolant system was in a heat-up mode (utilizing Reactor
Coolant Pump heat) at the time the leak was discovered.
The "A"
- - Makeup Pump was put in service, the "B" Makeup Pump was secured,
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During this RO inspection the inspector reviewed the actions taken
by the licensee relative to this occurrence.
Included in the in-
spector's review were the following:
written maintenance procedure
(WA 563) including the retest requirements (operational hydro per
.,
USAS B31.1.0), weld history records, welder qualification records,
~^".NDT examination records, X-rays of other orifices in the system,
~ visual inspection of the repairs with the system in operation, and
the licensee's plans relative to the other orifices in the system.
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No deficiencies were identified.
The following actions had been
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taken or were planned:
A replacement orifice (from Unit 2) was installed and the "B"
a.
Makeup Pump returned to service.
b.
X-rays were taken of the recirculation orifices for the "A" and
"C" Makeup Pumps and the letdown block orifice.
X-rays indicated
severe hydraulic erosion had occurred to the orifice for the "A"
Makeup pump; no evidence of erosion to the orifice for the "C"
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, Makeup pump, and slight erosion to the letdown block orifice.
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Run times for the Makeup pumps (from electrical switchgear in-
c.
stalled instrumentation) were as follows:
"A" - 1684 hours0.0195 days <br />0.468 hours <br />0.00278 weeks <br />6.40762e-4 months <br />,
"B" - 1141 hours0.0132 days <br />0.317 hours <br />0.00189 weeks <br />4.341505e-4 months <br />, and "C" - 120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br />.
d.
As a result of Items b and c above, the "A" Fbkeup pump was
valved out, the "C" tbkeup pump was running, and the "B" Make-
up was lined up but not running.
The "C" and "B" Makeup
pumps were selected for E.S. mode per Technical Specification 3.3.1.1.b.
However, during this R0 inspection the "C" Makeup
pump had to be removed from service (refer to Detail 6), and
"A" and "B" }bkeup pumps were put in the E.S. mode with the
"B" Makeup pump operating.
Additionally, operating instruc-
tions containing appropriate precautions relative to the
"A"
pump were issued.
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The UT inspection program which was being implemented per B&W's
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recommendations did not detect the leak (actually discovered
by an operator) because the leak occurred in an area -(thru the
wall at tie last orifice plate) not being examined.
The area
bedng examined was upstream of the orifice assembly rather
than on ene downstream side which was the location of'the
a
leak previously discovered at A50-1.
The licensee intends to
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institute a weekly radiography examination of the recircula-
tion orifices for the
"A",
"B", and "C" Makeup pumps and the
letdown block orifice.
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Orifices of a new design had been ordered, and two of these
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(for the Makeup pumps) were expected to arrive on site by
June 10, 1974.
klans were to install these orifices on a
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priority basis on the "A" and "C" Makeup pumps.
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5.
Followup Action AO 74-6
The licensee reported on June 3,1974, during this RO Inspection
1^
and by telegram on June 4, 1974, that a leak was discovered in a
socket weld on the discharge header of the reactor coolant system
makeup pumps.
The leaking weld joint was located in a 1" 304
stainless steel l'ine which supplies makeup water to the core flood
tanks.
The reactor coolant system was at 350cF and 1000 psig when
the Icak was discovered.
The secondary system was bottled up,
the reactor coolant pumps and the operating makeup pump stopped,
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and the leaking weld isolated to make repairs that were completed
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on June 4, 1974.
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The inspector reviewed the written maintenance procedure (WA 570)
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including the retest requirements (operational hydro per USAS
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B31.1.0) and Welder Qualification Records.
The repair consisted of
grinding out the defect, laying a fillet weld in the ground out
area until the area was filled up, and making a cover pass over the
entire weld to provide additional strength.
The inspector made a
visual inspection of the weld following repairs and while the
system was in operation.
Additionally, the inspector had dis-
cussions with GPUSC - QA representatives concerning this f ailure,
the repairs and PT examination.
The following information was
obtained:
This was the first socket weld failure in a stainless
,
steci joint.
The weld records for the original weld were reviewed
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and no abnormalities were identified.
The makeup and purification
system had been successfully hydroed to 4575 psig per USAS B31.1.0
(1.5 times design pressure).
The cause of the failure was unknown,
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but was surmised to be possibly insufficient weld metal.
Following
repairs the PT cxamination revealed no indications, as determined
by a Level III inspector.
6.
Loss of t'ne "C" lbkeuo Pump
At approximately 1:29 AM on June 5,1974, the "C" Makeup Pump which
was operating, was manually stopped and the "B" Makeup Pump was
started.
The plant was being maintained at 5320F + 20F with re-
actor coolant pump heat.
Control rod groups 1 thru 4 (Safety Rods)
were fully withdrawn with the remaining control rods (groups 5 thru
....
- .- M S-8) fully inserted, and reactor coolant system boron concentration
"2E~was about 2070 ppm.
Preparations were underway for the initial
critical approach with systems / components being aligned in accor-
dance with an approved prerequisite checkoff list.
The control
room operator received a " Low Lube Oil Pressure" alarm on the "C"
Makeup Pump.
The same pump was " punched up" on the computer con-
sole and a high bearing temperature was indicated by the computer.
The operator manually started the "B" Makeup Pump and secured the
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"C" pump.
Subsequent checkout of the computer memory indicated
that the total clapsed time from oil pressure alarm to securing the
pump was nineteen (19) seconds.
Flow to the reactor coolant pump
seals was maintained at all times.
In order to maintain the elec-
.
trical separation criteria.and the.needs of the emergency makeup
capabilities, the "B" pump was later switched to the alternate
power supply and valves were aligned.
The elapsed time frca oil
- pressure alarm until all electrical / valve ~ lineups were completed
was three (3) hours.
The inspector accompanied the operator out-
side the control room and followed most of the valve lineups and
electrical switching.
In all cases, the operator appeared to
-
follow all applicable safety regulations and approved valve lineup /
+
electrical switching procedures.
Severe damage occurred to the "C"
pump, and the pump was being replaced with an identical pump from
Unit 2 when this L3 inspection ended.
In the Unit 1 design there
are 3 Makeup Pumps; however, only 2 of these pumps are required to
be' operable in the E.S. mode powered from independent separate
busses to make the reactor critical.
This condition was satisfied.
7.
Sodium Thiosulfate Tank Ooerational Status
During a previous RO inspection (Report 50-289/74-23, Detail 3),
this matter was reviewed.
During this RO inspc ction, the inspector
observed that the installatten of the tank insulation was essentially
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complete.
The inspector also determined that installation and test-
ing of the heat tracing (lower section) had been completed.
The
upper section of the heat tracing has been installed; however, cir-
cuitry design changes are to be made to this section to permit its
actuation as determined by tank temperature.
According to licensee
representatives, the lower section is sufficient to maintain a tank
temperature of >75 F, and the upper section would be actuated on, as
required during severe cold weather conditiens.
'
.,_ At the time of this inspection the tank contents were out of specs
Prf as a result of dilution by Sodium Hydroxide.
This occurred as a
'
biEiresult of leakage thru a normally closed valve (BS-VS1) during re-
circulation of the Sodium Hydroxide Tank.
This condition was identi-
fied as a result of sampling both tanks.
As an interim measure,
operating procedures have been revised to require removal of the
spool piece (between the normally closed valve and associated tank)
in the supply lino to the tank not being circulated.
The licensee
-- is evaluating a sy stem modification, that consists of installing
-
a second isolation valve in the supply line to each tank, to correct
this apparent desige deficiency.
The licensee plans to drain the
tank, and add a new batch of Sodium Ti.losulfate to bring the tank
contents back into specs; a licenser representative stated that
RO:I would be notified when this m olution was completed.
RO:I was notified by the licensee by telephone on June 14, 1974,
that the contents of the Sodium Thiosulf ate Tank met the require-
ments of Technical Specification 3. 3.1. 3 (e. g. , 35,800 pounds of
sodium thiosulf ate at 29.5 weight percent solution with 1.5 weight
percent boric acid - sodium hydroxide buffer at a pH of 9.2).
The
--
licensee was informed that R0:I had no further questions on the
operability of this tank and that R0:I would reconmend to DL that
License Condition 2.c. (1) be cleared.
-
8.
Followup Action - A0 74-04
The licensee's ten day letter for this occurrence had not been re-
ceived at the time of this inspection; however, the corrective
action to restore the Control Rod Drive System to operational
status following the fire in a CRD cabiaet was reviewed.
This
consisted of a review of selected maintenance procedures used to
!
repair the damage and a review of rod scram time test dat- obtained
after the repairs.
R0:1 has no f ttrther questions in this area at
this time.
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9.
Followup Action - A0 74-03
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The licensee stated in a letter dated May 30, 1974, that tha
followup action to correct the condition of the 13 Emergency Diesel
'
Generat' r failure to run was to generate an approved procedure to
o
repair, test and restore to service and brief personnel inv'olved in
the need to use procedures.
The inspector reviewed the approved
' procedure used to restore the 1B Diesel and also the procedure used
to modify the 1A Diesel Generator.
The inspector also discussed
with a licensee representative the briefing of the maintenance
- 3;gpersonnel and verified such training was conducted.
RO:I has no
'
this-time.
(9g: further questions in this area at
'
The design change evaluation (GPU Startup Problem Report 975 com-
,
pleted on June 3, 1974) was reviewed by the inspector.
This report
-
reevaluated the design adequacy of the circuit changes based on
quescions raised during a previous RO inspection.
The inspector
has no further questions on this matter, and the item is resolved.
~
(Report 50-289/74-18, Detail 13.m)
10.
Reactor Building Sumo
_
The inspector physically inspected the Reactor Building sump and
several feeder drains.
These appeared to be clean and free of
debris.
This item.is closed.
(Report 50-289/74-18, Detail 12)
11.
Instrument Status Indication
'
A deficiency in the licensee's program used to indicate the opera-
-
1<:. bility and/or calibration status of meters, gauges and instrunents
~
was identified in Report 50-289/74-21, Detail 3.
The licensee has
written and implemented a procedure and tagging system whereby out
of calibration meters, gauges and instruments are identified and
marked.
The inspector revieced two (2) different instrucents which
had been marked in accordance with this procedure.
Temporary tags
are being used, but permanent black and white stickers have been
ordered according to a licensee representative.
RO:I has no further
questions in this area at this time.
12.
Burned Terminal on Control Rod Drive Power Transformer
on June 3, 1974, the licensee reported an observed imbalance ia
the phase currents of the CRD system.
The problem was traced
to a burned terminal on the primary of one of two main transfor-
mers for the system.
,
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The inspector observed the work in progress and observed that a pro-
cedure was being used and Q.C. coverage existed.
The licensee's
representative stated all similar terminals were checked and found
to be tight.
Additionally, he stated no safety issue was involved
in this occurrence.
The inspector observed the return to service
of this equipment prior to initial criticality and has no furtner
questions on this matter.
13.
Inspectors' Witness of Initial Criticality
Certain activities, procedures, and documents of the licensee were
-
EjyLireviewedbytheinspectorstoverifycompletenessofrequirements
u.qrfor initial cciticality.
The following is a list of specific topics
reviewed and the inspector's comments relating to. these items:
a.
Criticality Procedure: Official copy was current and had all
revisions incorporated.
.
.b.
Primary Chemistry: Most recent samples indicated chemistry
,
within Technical Specification limits.
.
c.
Gaseous and Liquid Effluents Monitoring:
The installed effluent
monitoring system was observed to be operating and within the
current calibration cycle.
d.
Chemical Factor Analysis:
The inspector witnessed a Met Ed
Radiation Chemistry Technician perform the determination of
the primary coolant boron concentration.
This activity was
accomplished using the correct procedure.
A one time sample,
.
specially diluted by the Unit 2 Station Engineer was passed
~I-
to the Radiation Chemistry Technician as a normal sample.
It was correctly analyzed and its off-nominal concentration
. correctly identified.
.
e.
Procedure Prerequisites: A sample of Surveillance Test Pro-
cedures and system Operating Procedures, which were required
to be completed by the Initial Criticality Procedure (TP 710/
1), were reviewed.
No deficiencies in the results of the
Surveillance Tests were noted.* The following deficiencies
were observed during the review of the operating procedures:
- Deficiencies in the licensee's Surveillanca Test Program were pre-
viously identified in Report 50-289/74-23, Detail 21.
The licensee
had conducted a comprehensive review 3 and the inspectors noted the
identified deficiencies had been corrected.
RO:1 het no further
questions in this area at this time.
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(1)
The Makeup and Purification System was being lined during
preparations for initial criticality in accordance with
OP 1104-2.
The Control Room Working Copy used to acccm-
plish this activity was observed to be Revision 1 dated
February 1, 1974.
The Control Room File Copy was ob-
served to be Ravision 2 dated April '- 1974.
Subsequent
review of the Procedure Index indicated that Revision 3
to this procedure had been distributed on Fby 24, 1974.
(2)
The Decay Heat Removal System was lined up during pre-
parations for initial criticality in accordance with OP
r,m_.
~{'(.} ~
1104-4.
The valves in this system wers positioned per
Enclosure 1 to OP 1104-4 Revision 0 on May 30,1974.
It
~ " -
was observed that the Control Room Working and File
copies of this procedure, including Enclosure 1 were
Revision 2 approved April 27, 1974 and placed in the
Control Room files on May 16, 1974.
The above are in violation of the FSAR 'Section lA, Opera-
~ ~ " ~ -
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ting Quality Assurance Plan,Section VI, Document Control,
which states in part:
". . .The Generation Division docu-
ment control procedure further requires that each >bnager
---
and Station Superintendent provide in their procedures
measurec: ... to ensure that approved changes be pronptly
transmitted for incorporation into documents; and to
ensure that obsolete or superseded documents are elimin-
ated from the system and not used..."
(3)
The Waste Gas Disposal System was lined up during pre-
>
-
parations for initial criticality in accordance with
OP 1140-27.
It was observed that the Control Room Werk-
~
ing Copy which had been used to accomplish this setup
had pen and ink changes to certain valve, level indicator
and electrical panel designators on pages 5 and 6.
There
was no indication that.these changes were approved by any-
one.
It was also noted that these changes did not appear
in the Control Room File Copy of OP 1104-27.
This copy
was also observed to be missing pages 22, 23, 24, 25, 26
and 29.
The above is in violation of the FSAR Section lA, Opera-
ting Quality Assurance Plan,Section VI, Document Control,
which states in part:
"The Superintendent of the TMI
Station Unit 1 will ensure that no changes are made to
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site instructions, procedures, and drawings unless such
changes are approved by the appropriate approving organi-
zation ..."
8
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These items were brought to the attention of the Plant Superinten-
'
dent who directed a review of the revisions of the procedures used
to align all safety related systems during preparations for initial
criticality.
As a result of this review the licensee stated all
j
valves affected by differences in the current and superseded check-
lists were correctly positioned prior to beginning the approach to
,
._,;,, initial criticality.
The Plant Operations Review Committee (PORC)
,
!
'0, , s evaluated this occurrence as an abnormal occurrence, and it was
.
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reported as A0 74-7.
.
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f.
Required Plant Systems in Service:
The systems required by
the prerequisite lists were reviewed on a sampling basis and
were found to bc operational or noted exceptions had been
3
reviewed and determined to have no impact on criticality.
, _ , ,
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g.
Calibration Checks of Instrumentation:
A sample of safety
related system surveillance tests were reviewed and found
_.
to be current and complete.
h.
Source Checks c f the Source Range Instrumentation:
The
response of the S.R. Channels to the installed neutron
sources was observed.
i.
Signal to Noise Checks:
The licensee took an exception to
-
'--
the requirement in TP 710/1 to verify the source range signal
to noise ratio greater than 2.
This exception was based on
a preoperational test accomplished prior to fuel loading.
j.
Minimum Count Rate on Each Channel:
The inspector observed
an indicated count rate in excess of the minimum required
(>2 ' CPS) at the tite Control Rod withdrawal ccamenced.
k.
Reactor Trip Settings Lowered: The inspector reviewed the
most current surveillance test of Channel C of the Power
Range Instrumentation and observed that the trip setting
was lowered in accordance with the Test Change Notice to
the Power Range Surveillance Test.
1.
Increased Channel Sensitivity of Instrumentation:
The
inspector reviewed the most current Surveillance Test of
Channel C Power Range Instrumentation and observed that
the gain had been increased in accordance with the Test
Cha'nge Notice to the Power Range Surveillance Test.
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Special Instrumentation In Service:
The inspector observed
f
m.
the counter-scalers and stop watches required by the pro-
}
cedure appeared operabic.
j
n.
Data Properly Recorded:
The inspector observed that data
required by the procedure being entered into the data
i
sheets,
Data Properly Presented for Analysis:
The inspector observed
o.
boron concentration data and count rate data being presented
to the data takers and analysts for evaluation.
~c~..
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<p.
Analysis Performed:
The inspector observed the generation
of the 1/M plots and verified several points independently.
Additionally, the dilution rate was checked using stop
watch and the installed flow meter.
q.
Adequate Staff: The inspector reviewed a Test Manning memo
prepared by the Plant Superintendent and found it met the
'~"
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requiremants of the Technical Specifications for this test.
-
r.
SRO's and R0 at the Required Location: The inspector observed
-
the number of licensed operators required by the Test Manning
Memo were on watch during the procedure.
s.
Maximum Crew Working Time:
A representative of the licensee
informed the inspector that the maximum shif t being worked
j
by the personnel directly involved with the initial criticality
.
was twelve (12) hours.
i
.
I
t.
Shift Turnover Performed in an Orderly Manner:
The inspector
attended several crew turnovers and test briefings.
These
were conducted in an orderly mann;r.
Orderly and Systematic Use of Procedure: The insp.: tor wit-
u.
nessed the initial criticality evolution and observed that
the evolution was conducted in accordance with the procedure
in an orderly manner.
The following is a brief summary of the sequence of events observed
during the actual evolution.
All times listed were on June 5, 1974.
The procedure commended at 2:30 pm.
Plant conditions were as
follows.
Temperature 532 120F, primary pressure 2155 1 25
psi, Control Rod Assemblics (CRA) Croups 1-4 fully withdrawn,
1445 215
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4 Reactor Coolant Pumps running, primary Boron Concentration
was 2070 ppm.
At this time Groups 5, 6, 8 were fully with-
drawn and Group 7 pulled to 75%.
Rod withdrawal was com-
pleted at 3:35 pm and boron dilution of the primary commenced
at 4:56 pm at a rate of 50 1 10 GPM.
Dilution was secured at
10:27 pm, and the letdown flow was increased to about 140 GPM.
The reactor was declared critical at 10:36 pm with a boron
concentration of 1623 ppm compared to the acceptance "alue
of 1626 150 ppm.
The power level was stabilized with rod
motion and necessary data was collected.
_Eh.fy.
Procedural Signoff Completed:
The inspector observed the sign-
[
off of the prerequisites for the procedure and the appropriate
r
checklists.
w.
Data Analysis Performed in a Timely Manner:
The maintenance
of the 1/M Plots and estimated critical condition updates were
observed to be performed in accordance with the procedure which
provided adequate time to ensure control of the evolution.
'- -
' x.
Criticality Achieved Near Predicted Value: The licensee's data
-
indicated the critical concentration of boron was 1623 ppm com-
--
-
pared to a prediction of 1626 150 ppm, with all other specified
reactivity sources as required by the procedure.
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1445 216
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