LER-1979-019, Forwards LER 79-019/01T-0 |
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'6 COOPER NUCLE AR STATION Nebraska Public Power District
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C:iSS790430 August 20, 1979 Mr. K. V. Seyfrit U.S. Nuclear Regulatory Commission Office of Inspection and Enforcement Region IV 611 Ryan Plaza Suite 1000 Arlington, Texas 76011
Dear Sir:
This report is submitted in accordance with Section 6.7.2.A.5 of the Technical Specifications for Cooper Nuclear Station and discusses a reportable occurrence that was discovered on August 9, 1979. Our in-itial notification was telecopied to your office on August 10, 1979. A licensee event report form is also enclosed.
Report No..
50-298-79-19 Report Date:
August 20, 1979 Occurrence Date: August 9, 1979 Facility:
Cooper Nuclear Station Brownville, Nebraska 68321 Identification of Occurrence:
Failure or malfunction of one or more components which prevents or could prevent, by itself, the fulfill =ent of the functional re-quirements of system (s) used to cope with accidents analyzed in the SAR.
Conditions Prior to Occurrence:
Reactor power was at 99% of rated thermal power.
This occurrence was initiated subsequent to a reactor scram.
Description of Occurrence:
Upon receipt of an auto start signal, the HPCI (High Pressure Coolant Injection) system did not initially start.
However, a short time after the initiation signal, the HPCI system did start and maintained reactor vessel water level.
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Mr. K. V. Seyfrit August 20, 1979 Page 2.
Designation of Apparent Cause of Occurrence:
It was found that the failure of the pump to start was caused by the failure of the seal rings on the hydraulic operator for the turoine stop valve.
The seal rings were allowing oil to leak by the piston of the operator and insufficient force was available to open the stop valve at full system steam pressure. When disas-sembled it was found that approximately 1/3 of the seating surface of one ring was missing. The valve actuator is a 12 inch hydraulic cylinder manufactured by Miller Fluid Power Company, Model J-53.
Analysis of Occurrence:
A review of this occurrence indicates that at its lowest point the reactor water level was approximately -70 inches.
This is about 35 inches above the top of the active fuel.
The RCIC (Reactor Core Isolation Cooling) pump automatically started and supplied water to the reactor vessel and would have restored vessel water level had HPCI not started. HPCI did not start until about 14 minutes after the scram when system pressure was reduced to about 600 psig.
Initially it was believed that the apparent cause of this occur-rence as stated in the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> notification was low lube oil pres-sure to.the operating piston on the stop valve actuator. The following sequence of events revealed the apparent cause currently stated in this response.
The lube oil pressure was adjusted and the HPCI stop valve was stroked in an acceptable time frame with no steam pressure when the reactor was shutdown. The HPCI was de-clared operable and was satisfactorily tested in the manual test mode at 150 psig main steam pressure during reactor startup.
The reactor was placed in RUN and the turbine generator was synchron-ized to the bus.
HPCI was again started manually satisfactorily.
However, during the subsequent automatic quick start test, HPCI did not start due to the stop valve not opening. At this point HPCI was declared inoperable and additional troubleshooting activities commenced.
The problem was diagnosed as failed piston rings.
During the ensuing two days while the piston rings were being procured from the vendor, the HPCI system could have been manually initiated if required. The HPCI system was in this manual mode for approximately 56 hours6.481481e-4 days <br />0.0156 hours <br />9.259259e-5 weeks <br />2.1308e-5 months <br /> and was inoperable for about 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> during troubleshooting and replacement of the piston rings.
3 The HPCI stop valve is a vertically mounted hydraulically operated piston type globe valve with the actuating cyclinder on the bottom and an internal balance chamber on top of the globe valve piston.
The purpose of the balance chamber is to insure smooth operation of the valve during the opening cycle. This function is provided by
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e Mr. K. V. Seyfrit August 20, 1979 Page 3.
an internal orificed steam passage which permits approximately 20%
of the main steam pressure to accumulate in the balance chamber during valve opening. When the valve is fully open, the internal steam pressure is equalized throughout the stop valve body. During this occurrence, the valve actuator piston did not have sufficient force to overcome the initial main steam pressure in the balance chamber. As the main steam pressure decreased after the reactor scram, the force on the valve actuator piston became sufficient to open the stop valve and start the RPCI pump and aid in restoring reactor water level to its normal range.
The failed piston ring was of a cup type configuration and fabri-cated from leather. It is believed that the ring failure was accelerated due to the operating temperature of the stop valve.
The failed ring had never been replaced and the estimated time in service of the subject ring is six (6) years.
All Low Pressure Coolant Injection systems were operable and could have been used to maintain level had they been required. This occurrence presented no adverse consequences from the standpoint of public health and safety.
Corrective Action
The leather cup rings in the valve actuator were replaced and a simulated Auto Actuation Test (S.P. 6.3.3.3) was satisfactorily performed at full system pressure to verify pump operability. All applicable surveillance procedures have been changed to insure that during testing the stop valve is opened under conditions approx-imating those found during an automatic system initiation.
The preventive maintenance program has been revised to include checking the subject valve actuating piston for excess oil leakage and the subject piston rings are scheduled for replacement every five years. The turbine control actuator for the RCIC is of a different design and the mode of failure identified in the occur-rence is not applicable to the RCIC.
Sincerely, i
L. C. Lessor Station Superintendent Cooper Nuclear Station LCL :c g Attach.
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| 05000298/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000298/LER-1979-001-03, /03L-0 on 790103:during Operation,Drywell Atmospheric Radiation Monitor Gas Channel (RMV-RM-4C) Failed Downscale.Caused by Detector Failure Caused by Moisture in Detector Chamber.Detector Replaced;Chamber & Lines Dried | /03L-0 on 790103:during Operation,Drywell Atmospheric Radiation Monitor Gas Channel (RMV-RM-4C) Failed Downscale.Caused by Detector Failure Caused by Moisture in Detector Chamber.Detector Replaced;Chamber & Lines Dried | | | 05000298/LER-1979-005-03, /03X-1 on 790216:reactor Recirculation Motor Generator Set a Tripped During Normal Operation.Caused by Failure of Level Switch NBI-LIS-58A Due to Corrosion. Corrosion Cleaned from Inside Switch Case & Switch Replaced | /03X-1 on 790216:reactor Recirculation Motor Generator Set a Tripped During Normal Operation.Caused by Failure of Level Switch NBI-LIS-58A Due to Corrosion. Corrosion Cleaned from Inside Switch Case & Switch Replaced | | | 05000298/LER-1979-005, Forwards LER 79-005/03X-1 | Forwards LER 79-005/03X-1 | | | 05000298/LER-1979-008-03, /03L-0 on 790420:breaker 1FA Failed to Trip When Control Switch Operated to Trip.Caused by Failure of Auxiliary Switch Contact Mounted Inside Breaker 1FA to Make Proper Electrical Contact.Breaker Inspected & Cleaned | /03L-0 on 790420:breaker 1FA Failed to Trip When Control Switch Operated to Trip.Caused by Failure of Auxiliary Switch Contact Mounted Inside Breaker 1FA to Make Proper Electrical Contact.Breaker Inspected & Cleaned | | | 05000298/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000298/LER-1979-009-03, /03L-0 on 790430:four Penetrations Found Leaking Excessively During Local Leak Rate Test.Caused by Defects in Limitorque Operator Torque Switch,Seal Rings & Check Valves. All Defects Repaired | /03L-0 on 790430:four Penetrations Found Leaking Excessively During Local Leak Rate Test.Caused by Defects in Limitorque Operator Torque Switch,Seal Rings & Check Valves. All Defects Repaired | | | 05000298/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000298/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000298/LER-1979-010-03, /03L-0 on 790424:surface Linear Indication Found in Weld RA5-CF-13,main Steam to a & B RHR Heat Exchangers & HPCI Turbine.Caused by Welding Error.Defect Removed | /03L-0 on 790424:surface Linear Indication Found in Weld RA5-CF-13,main Steam to a & B RHR Heat Exchangers & HPCI Turbine.Caused by Welding Error.Defect Removed | | | 05000298/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000298/LER-1979-011-03, /03L-0 on 790424:reactor Water Cleanup MO-18 Contactor Failed to Close Manually During Cold Shutdown. Caused by Failure of Auxiliary Contact Mechanism.Repairs Completed Per IE Bulletin 78-05 | /03L-0 on 790424:reactor Water Cleanup MO-18 Contactor Failed to Close Manually During Cold Shutdown. Caused by Failure of Auxiliary Contact Mechanism.Repairs Completed Per IE Bulletin 78-05 | | | 05000298/LER-1979-012-03, /03L-0 on 790503:vessel Water Temp Increased to 220 F W/Primary Containment Integrity Not Established.Caused by Omission in Operating Procedures.Setpoint of Interlock Verified & Procedures Revised | /03L-0 on 790503:vessel Water Temp Increased to 220 F W/Primary Containment Integrity Not Established.Caused by Omission in Operating Procedures.Setpoint of Interlock Verified & Procedures Revised | | | 05000298/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000298/LER-1979-013-03, /03L-0 on 790508:correct Drywell to Suppression Chamber Reading Not Established.Caused by Leaking Inlet Purge Valve.Valve Repaired & Leak Tested | /03L-0 on 790508:correct Drywell to Suppression Chamber Reading Not Established.Caused by Leaking Inlet Purge Valve.Valve Repaired & Leak Tested | | | 05000298/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000298/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000298/LER-1979-014-03, /03L-0 on 790509:chamber Vent Valve for Torus Level Transmitter Was Left Closed.Caused by Technician Error.Vent Valve Opened & PC-LT-12 Placed Back Into Svc | /03L-0 on 790509:chamber Vent Valve for Torus Level Transmitter Was Left Closed.Caused by Technician Error.Vent Valve Opened & PC-LT-12 Placed Back Into Svc | | | 05000298/LER-1979-015-03, /03X-1 on 790525:breaker 1AS Failed to Close Automatically After Reactor Scrammed.Caused by Improper Operations of Switch 52 in Breaker 1AN.Breaker 1FA Failed to Trip.Caused by Misaligned Trip Coil & Armature | /03X-1 on 790525:breaker 1AS Failed to Close Automatically After Reactor Scrammed.Caused by Improper Operations of Switch 52 in Breaker 1AN.Breaker 1FA Failed to Trip.Caused by Misaligned Trip Coil & Armature | | | 05000298/LER-1979-015, Forwards LER 79-015/03X-1 | Forwards LER 79-015/03X-1 | | | 05000298/LER-1979-016-03, /03L-0 on 790531:RHR Pump 1A Tripped During Start on Overcurrent in Phase C.Caused by Failure of GE Model 121AC66K8A Overcurrent Relay Operating Disc to Return to Normal Position.Relay Cleaned,Recalibr & Retested | /03L-0 on 790531:RHR Pump 1A Tripped During Start on Overcurrent in Phase C.Caused by Failure of GE Model 121AC66K8A Overcurrent Relay Operating Disc to Return to Normal Position.Relay Cleaned,Recalibr & Retested | | | 05000298/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | | | 05000298/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000298/LER-1979-017-03, /03L-0 on 790620:during Review,Observed That Surveillance Procedure 6.2.4.1 Did Not Include Daily Check of Undervoltage Relays or Monthly Functional Testing. Cause Unstated.Procedures Revised | /03L-0 on 790620:during Review,Observed That Surveillance Procedure 6.2.4.1 Did Not Include Daily Check of Undervoltage Relays or Monthly Functional Testing. Cause Unstated.Procedures Revised | | | 05000298/LER-1979-018-03, /03L-0 on 790706:during Routine Testing,Reactor Vessel Level Indicating Switch NBI-LIS-58A Was Found W/Trip Point Less than Allowed.Caused by Sediments of Dust & Moisture in Auxiliary Switch | /03L-0 on 790706:during Routine Testing,Reactor Vessel Level Indicating Switch NBI-LIS-58A Was Found W/Trip Point Less than Allowed.Caused by Sediments of Dust & Moisture in Auxiliary Switch | | | 05000298/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000298/LER-1979-019-01, /01T-0:on 790809,upon Auto Start Signal,High Pressure Coolant Injection Pump Did Not Initially Start. Caused by Deterioration of Piston Rings in Valve Actuator. Rings Replaced & Test Completed Satisfactorily | /01T-0:on 790809,upon Auto Start Signal,High Pressure Coolant Injection Pump Did Not Initially Start. Caused by Deterioration of Piston Rings in Valve Actuator. Rings Replaced & Test Completed Satisfactorily | | | 05000298/LER-1979-019, Forwards LER 79-019/01T-0 | Forwards LER 79-019/01T-0 | | | 05000298/LER-1979-020-03, /03L-0:on 790809,while Performing Surveillance Procedure on Relief Valve Bellows Monitoring Sys,Pressure Switch MS-PS-71G Failed to Actuate.Caused by Improper Assembly.Switch Was Replaced | /03L-0:on 790809,while Performing Surveillance Procedure on Relief Valve Bellows Monitoring Sys,Pressure Switch MS-PS-71G Failed to Actuate.Caused by Improper Assembly.Switch Was Replaced | | | 05000298/LER-1979-020, Forwards LER 79-020/03L-0 | Forwards LER 79-020/03L-0 | | | 05000298/LER-1979-021-03, /03L-0:on 790811,carbon Absorber in Standby Gas Treatment Sys B Was Wetted W/Water When Control Room Received Actuation Alarm for Deluge Sys.Caused by Improper Installation of Baseplate of Fire Detection Unit | /03L-0:on 790811,carbon Absorber in Standby Gas Treatment Sys B Was Wetted W/Water When Control Room Received Actuation Alarm for Deluge Sys.Caused by Improper Installation of Baseplate of Fire Detection Unit | | | 05000298/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000298/LER-1979-022-03, /03L-0:on 790812,water from Carbon Absorber Housing of Standby Gas Treatment Sys a Sprayed Carbon Absorber Trays,Rendering Trays Inoperable.Caused by Inadequate Seating Area Between Valve Clapper & Latch | /03L-0:on 790812,water from Carbon Absorber Housing of Standby Gas Treatment Sys a Sprayed Carbon Absorber Trays,Rendering Trays Inoperable.Caused by Inadequate Seating Area Between Valve Clapper & Latch | | | 05000298/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | | | 05000298/LER-1979-023, Forwards LER 79-023/03L-0 | Forwards LER 79-023/03L-0 | | | 05000298/LER-1979-023-03, /03L-0:on 790809,Barton Model 288 Differential Pressure Indicating Switch MS-DPIS-119B Was Found in Excess of Tech Specs Table 3.2.A.Caused by Faulty Switch. Microswitch Assembly Was Replaced | /03L-0:on 790809,Barton Model 288 Differential Pressure Indicating Switch MS-DPIS-119B Was Found in Excess of Tech Specs Table 3.2.A.Caused by Faulty Switch. Microswitch Assembly Was Replaced | | | 05000298/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000298/LER-1979-024-03, /03L-0:on 790831,surveillance Testing Pressure Switch NBI-PS-55D Found W/Trip Point Below Tech Specs.Cause Not Stated.Switch Readjusted to Proper Setpoint & Then Replaced After Unsatisfactory Performance | /03L-0:on 790831,surveillance Testing Pressure Switch NBI-PS-55D Found W/Trip Point Below Tech Specs.Cause Not Stated.Switch Readjusted to Proper Setpoint & Then Replaced After Unsatisfactory Performance | | | 05000298/LER-1979-025, Forwards LER 79-025/03L-0 | Forwards LER 79-025/03L-0 | | | 05000298/LER-1979-025-03, /03L-0:on 790912,HPCI Turbine Stop Valve Separated from Actuator at Split Coupling.Caused by Improperly Mfg Split Coupling.Split Coupling Replaced & Installation Procedures Revised | /03L-0:on 790912,HPCI Turbine Stop Valve Separated from Actuator at Split Coupling.Caused by Improperly Mfg Split Coupling.Split Coupling Replaced & Installation Procedures Revised | | | 05000298/LER-1979-026, Forwards LER 79-026/03L-0 | Forwards LER 79-026/03L-0 | | | 05000298/LER-1979-026-03, /03L-0:on 790912,investigation Found Unidentified Drywell Leak on Reactor Recirculation Pump B.Caused by Failure of Pump Seal at Natural End of Life.Seal Replaced.No Further Action Planned | /03L-0:on 790912,investigation Found Unidentified Drywell Leak on Reactor Recirculation Pump B.Caused by Failure of Pump Seal at Natural End of Life.Seal Replaced.No Further Action Planned | | | 05000298/LER-1979-027, Forwards LER 79-027/03L-0 | Forwards LER 79-027/03L-0 | | | 05000298/LER-1979-027-03, /03L-0:on 791001,during Routine Surveillance Procedure MS-DPIS-119B,switch Was Found W/Setpoints in Excess of Tech Specs.Caused by Setpoint Drift.Instrument Recalibr | /03L-0:on 791001,during Routine Surveillance Procedure MS-DPIS-119B,switch Was Found W/Setpoints in Excess of Tech Specs.Caused by Setpoint Drift.Instrument Recalibr | | | 05000298/LER-1979-028, Forwards LER 79-028/03L-0 | Forwards LER 79-028/03L-0 | | | 05000298/LER-1979-028-03, /03L-0:on 791008,during Insp of Cable Spreading Room,One 4-inch Pipe Sleeve Not Sealed.Caused by Inadequate Control of Fire Seals Installation During Microwave Communications Sys Installation.Sleeve Was Sealed | /03L-0:on 791008,during Insp of Cable Spreading Room,One 4-inch Pipe Sleeve Not Sealed.Caused by Inadequate Control of Fire Seals Installation During Microwave Communications Sys Installation.Sleeve Was Sealed | | | 05000298/LER-1979-029-03, /03L-0:on 791012,during Routine Plant Tour,Pinhole Leak Detected in Upstream Weld of Supply Isolation Valve. Cause Unknown.Weld Will Be Repaired During Next Shutdown | /03L-0:on 791012,during Routine Plant Tour,Pinhole Leak Detected in Upstream Weld of Supply Isolation Valve. Cause Unknown.Weld Will Be Repaired During Next Shutdown | | | 05000298/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | | | 05000298/LER-1979-030-03, /03L-0:on 791021,while Pumping Water from Torus to radwaste,drywell-to-torus Differential Pressure Dropped Below Tech Specs.Caused by Nitrogen Pressure Forcing Water from Downcomers to Flow to Torus | /03L-0:on 791021,while Pumping Water from Torus to radwaste,drywell-to-torus Differential Pressure Dropped Below Tech Specs.Caused by Nitrogen Pressure Forcing Water from Downcomers to Flow to Torus | | | 05000298/LER-1979-030, Forwards LER 79-030/03L-0 | Forwards LER 79-030/03L-0 | |
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