05000254/LER-2018-004-01, Reactor Scram Due to Turbine-Generator Load Reject

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Reactor Scram Due to Turbine-Generator Load Reject
ML19059A037
Person / Time
Site: Quad Cities Constellation icon.png
Issue date: 02/28/2019
From: Ohr K
Exelon Generation Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
SVP-19-009 LER 2018-004-01
Download: ML19059A037 (5)


LER-2018-004, Reactor Scram Due to Turbine-Generator Load Reject
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(i)
2542018004R01 - NRC Website

text

Exelon Generation SVP-19-009 February 28, 2019 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555 Quad Cities Nuclear Power Station, Unit 1 Renewed Facility Operating License No. DPR-29 NRC Docket No. 50-254 10 CFR 50.73

Subject:

Licensee Event Report 254/2018-004-01 "Reactor Scram Due to Turbine-Generator Load Reject" Enclosed is Licensee Event Report (LER) 254/2018-004-01, "Reactor Scram Due to Turbine-Generator Load Reject", for Quad Cities Nuclear Power Station, Unit 1.

This report is submitted in accordance with 1 O CFR 50. 73(a)(2)(iv)(A) for an event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B).

There are no regulatory commitments contained in this letter.

Should you have any questions concerning this report, please contact Mark Humphrey at (309) 227-2800.

Re/>~

Kenneth S. Ohr Site Vice President Quad Cities Nuclear Power Station cc:

Regional Administrator-NRC Region Ill NRC Senior Resident Inspector-Quad Cities Nuclear Power Station

SVP-19-009 U. S. Nuclear Regulatory Commission Page 2 of 2 bee:

NRC Project Manager-NRR (electronic Ltr & LER) Kimberly.qreen@nrc.gov Illinois Emergency Management Agency - Department of Nuclear Safety (hard copy Ltr & LER)

Charlie Mathews, IEMA Resident (electronic Ltr & LER)

Senior Reactor Analyst - NRC Region Ill (hard copy Ltr & LER)

Dave Gullatt, Director, Licensing and Regulatory Affairs - Cantara (electronic Ltr & LER)

Patrick R. Simpson, Manager, Licensing, Dresden & Quad Cities Stations (electronic Ltr & LER)

Exelon Document Control Desk Licensing (Hard Copy Ltr & LER)

Exelon Document Control Desk Licensing (Included in LER Completed)

Spencer T. Moore-MidAmerican Energy Company (electronic Ltr & LER) STMoore@midamerican.com LER Completed (electronic Ltr & LER)

Bruce Franzen, RA Manager - Dresden Nuclear Power Station (electronic Ltr & LER)

Mark Humphrey, RA Manager - Quad Cities Nuclear Power Station (electronic Ltr & LER)

Tom Petersen, NRC Coordinator - Quad Cities Nuclear Power Station (electronic Ltr & LER)

Kara Koett, NSRB Site Coordinator & INPO Site Coordinator - Quad Cities (electronic Ltr & LER)

INPO Records Center (included in LER Completed)

SVP Letter File (Q:\\SVP\\20YY)

Reg Assurance Clerk (for record turnover in EDMS)

NRC FORM366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 03/31/2020 (04-2018)

Estmated, the NRC may not conduct or sponsor, and a person is not required to respond to, the infomnation collection.

3.Page Quad Cities Nuclear Power Station Unit 1 05000254 1

OF 3

4. Title Reactor Scram Due to Turbine-Generator Load Reject
5. Event Date
6. LER Number
7. Report Date
8. Other Facilities Involved Month I

Sequential I Rev Facility Name Docket Number Day Year Year Number No.

Month Day Year 05000 Facility Name Docket Number 09 26 2018 2018 -

004 01 02 08 2019 05000

9. Operating Mode
11. This Report is Submitted Pursuant to the Requirements of 10 CFR §: (Check all that apply)

D 20.2201(b)

D 20.2203(a)(3)(i)

D 50.73(a)(2)(ii)(A)

D 50.73(a)(2)(viii)(A)

D 20.2201(d)

D 20.2203(a)(3)(ii)

D 50.73(a)(2)(ii)(B)

D 50.73(a)(2)(viii)(B) 1 D

D D

D 20.2203(a)(1) 20.2203(a)(4) 50.73(a)(2)(iii) 50.73(a)(2)(ix)(A)

D 20.2203(a)(2)(i)

D 50.36( c)( 1 )(i)(A)

~ 50.73(a)(2)(iv)(A)

D 50.73(a)(2)(x) 1 o. Power Level D 20.2203(a)(2)(ii)

D 50.36( c)( 1 )(ii)(A)

D 50.73(a)(2)(v)(A)

D 73.71(a)(4)

D 20.2203(a)(2)(iii)

D 50.36(c)(2)

D 50.73(a)(2)(v)(B)

D 73.71 (a)(5)

D 20.2203(a)(2)(iv)

D 50.46(a)(3)(ii)

D 50.73(a)(2)(v)(C)

D 73.77(a)(1) 100 D 20.2203(a)(2)(v)

D 50.73(a)(2)(i)(A)

D 50.73(a)(2)(v)(D)

D 73.77(a)(2)(i)

D 20.2203(a)(2)(vi)

D 50.73(a)(2)(i)(B)

D 50.73(a)(2)(vii)

D 73.77(a)(2)(ii)

D 50.73(a)(2)(i)(C)

D Other (Specify in Abstract below or in

C. CAUSE OF EVENT

YEAR 2018 -

3. LER NUMBER SEQUENTIAL NUMBER 004 The Root Cause was ineffective procedural controls for ensuring both unit output breakers were closed prior to performing contact status verifications and for ensuring the status control checks were performed correctly.

D. SAFETY ANALYSIS

System Design

REV NO.

01 The Quad Cities' switchyard is configured in a ring bus to ensure that during full-power operation, when one of the 345 KV breakers or one of the 345 KV transmission lines is removed from service, at least one of the two ring bus unit output breakers remains closed. Having both ring bus unit output breakers open at the same time would result in both breakers' load reject contacts being made up, which by design causes a load-reject trip of the Turbine-Generator and a subsequent Automatic Reactor SCRAM.

Safety Impact The safety significance of this event was minimal. All systems responded as designed during the event. Operators performed required actions safely and in accordance with procedures and training.

Risk Insights A risk assessment of the turbine-generator trip was performed for this event. The resulting assessment concluded that the event was not risk significant since Conditional Core Damage Probability (CCDP) and Conditional Large Early Release Probability (CLERP) were below the threshold.

E. CORRECTIVE ACTIONS

Immediate Corrective Actions:

The governing procedures were revised to incorporate enhanced guidance for performing contact checks on unit output breakers to support Unit 1 startup.

Follow-up Corrective Actions:

1. Operations Dept. to develop plan to re-enforce Technical Human Performance use within operating crews.
2.

Maintenance Dept. to develop plan to re-enforce technical fundamentals within maintenance crews.

F. PREVIOUS OCCURRENCES

No previous similar events have occurred at the site based on a search of station LERs and I Rs.

G. COMPONENT FAILURE DATA

No component failures were associated with this event. An ICES entry was completed for the event. Page _3_ of _i