| | | Reporting criterion |
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| 05000296/LER-1986-001-01, :on 860105,during Cleaning,Reactor Protection Sys (RPS) Tripped on Low Voltage.Caused by Operator Bumping RPS Motor Generator Set B Voltage Control Knob.Knobs Will Be Fitted W/Protection Covers |
- on 860105,during Cleaning,Reactor Protection Sys (RPS) Tripped on Low Voltage.Caused by Operator Bumping RPS Motor Generator Set B Voltage Control Knob.Knobs Will Be Fitted W/Protection Covers
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000260/LER-1986-001, :on 851118,spent Fuel Pool Storage Gates Removed While Lead Shielding Blankets in Use.Caused by Inadequate Procedural Controls to Ensure Maint of Safety Evaluation Requirements.Procedures Revised |
- on 851118,spent Fuel Pool Storage Gates Removed While Lead Shielding Blankets in Use.Caused by Inadequate Procedural Controls to Ensure Maint of Safety Evaluation Requirements.Procedures Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000259/LER-1986-001-02, :on 860107,effluent Exhausted to Main Stack W/Monitoring Channel Partially Operable.Caused by Lack of Communication Between Unit Operators & Support Personnel. Personnel Counseled |
- on 860107,effluent Exhausted to Main Stack W/Monitoring Channel Partially Operable.Caused by Lack of Communication Between Unit Operators & Support Personnel. Personnel Counseled
| 10 CFR 50.73(a)(2)(1) |
| 05000260/LER-1986-002-02, :on 860205,discovered Momentary Loss of Secondary Containment Due to Personnel Airlock Failure. Caused by Normal Wear in Sticking Solenoid Plunger.Plunger Cleaned & Lubricated.Circuit Tested |
- on 860205,discovered Momentary Loss of Secondary Containment Due to Personnel Airlock Failure. Caused by Normal Wear in Sticking Solenoid Plunger.Plunger Cleaned & Lubricated.Circuit Tested
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000296/LER-1986-002-01, :on 860116,during Performance of Core Spray Logic Test Surveillance Instruction (SI 4.2.B.39A),diesel Generators 3EA,3EB & 3EC Inadvertently Started.Caused by Personnel Error.Individuals Counseled |
- on 860116,during Performance of Core Spray Logic Test Surveillance Instruction (SI 4.2.B.39A),diesel Generators 3EA,3EB & 3EC Inadvertently Started.Caused by Personnel Error.Individuals Counseled
| 10 CFR 50.73(a)(2) |
| 05000260/LER-1986-003-03, :on 860226,electricians Inadvertently Bumped Reactor Protection Sys a Bus Transfer Switch & Caused Half Scram,Partial Primary & Secondary Containment Isolation. Caused by Personnel Error.Isolations Reset |
- on 860226,electricians Inadvertently Bumped Reactor Protection Sys a Bus Transfer Switch & Caused Half Scram,Partial Primary & Secondary Containment Isolation. Caused by Personnel Error.Isolations Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000296/LER-1986-003-01, :on 860123,during Performance of Reactor Bldg Ventilation Radiation Monitor Calibr Surveillance Instruction,Inadvertent Containment Isolation Occurred. Caused by Personnel Error.Personnel Counseled |
- on 860123,during Performance of Reactor Bldg Ventilation Radiation Monitor Calibr Surveillance Instruction,Inadvertent Containment Isolation Occurred. Caused by Personnel Error.Personnel Counseled
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000260/LER-1986-003, Corrected Page 2 to LER 86-003-00:on 860226,energized Isolation Logic Tripped.Caused by Personnel Error.Temporary Cover for Protection Against Accidental Bumping of Bus Transfer Switch Provided | Corrected Page 2 to LER 86-003-00:on 860226,energized Isolation Logic Tripped.Caused by Personnel Error.Temporary Cover for Protection Against Accidental Bumping of Bus Transfer Switch Provided | |
| 05000259/LER-1986-004-03, :on 851128,water Sampling Revealed Excessively High Conductivity & Chloride,Nitrate & Sulfate Concentrations.Caused by Leakage from Inner Floating Head Gaskets.Gaskets Replaced |
- on 851128,water Sampling Revealed Excessively High Conductivity & Chloride,Nitrate & Sulfate Concentrations.Caused by Leakage from Inner Floating Head Gaskets.Gaskets Replaced
| |
| 05000260/LER-1986-004-02, :on 860421,ESF Actuation Occurred During Replacement of Relay Coil on Reactor motor-operated Valve Board 2B.Caused by Electrician Error.Power Restored to Board & Electrician Cautioned |
- on 860421,ESF Actuation Occurred During Replacement of Relay Coil on Reactor motor-operated Valve Board 2B.Caused by Electrician Error.Power Restored to Board & Electrician Cautioned
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000296/LER-1986-004, :on 860125,Tech Spec 3.5.C.7 Re Availability of Normal & Emergency Power Violated When RHR Loop II & Diesel Generators Removed from Svc.Personnel Counseled & Tech Spec Clarification Proposed |
- on 860125,Tech Spec 3.5.C.7 Re Availability of Normal & Emergency Power Violated When RHR Loop II & Diesel Generators Removed from Svc.Personnel Counseled & Tech Spec Clarification Proposed
| 10 CFR 50.73(a)(2)(1) |
| 05000260/LER-1986-005-02, :on 860403,primary Containment Isolation Occurred.Caused by Insecure Jumper Connections Across Relay & Hampered Relay Access During Surveillance Instruction. Interim Measure Eliminates Jumper Placement |
- on 860403,primary Containment Isolation Occurred.Caused by Insecure Jumper Connections Across Relay & Hampered Relay Access During Surveillance Instruction. Interim Measure Eliminates Jumper Placement
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000296/LER-1986-005-03, :on 860215,containment Isolation Occurred. Caused by Relay Failure in Refuel Zone Exhaust Radiation Monitor.Relay Replaced & Isolation Reset |
- on 860215,containment Isolation Occurred. Caused by Relay Failure in Refuel Zone Exhaust Radiation Monitor.Relay Replaced & Isolation Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000259/LER-1986-005, :on 860210,control Room Emergency Ventilation Sys Trains a & B Actuated on High Radiation Alarm from Detector RM-90-259A.Caused by Cracked Internal Calibr Source Motor Mounting Bracket.Bracket Repaired |
- on 860210,control Room Emergency Ventilation Sys Trains a & B Actuated on High Radiation Alarm from Detector RM-90-259A.Caused by Cracked Internal Calibr Source Motor Mounting Bracket.Bracket Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000296/LER-1986-006-03, :on 860714,fire Protection Water Main Water for Sprinklers Discovered Unavailable.Caused by Failure to Remove Welded Pipe Blank During Sys Testing.Blank Removed. Pipe Testing Planned |
- on 860714,fire Protection Water Main Water for Sprinklers Discovered Unavailable.Caused by Failure to Remove Welded Pipe Blank During Sys Testing.Blank Removed. Pipe Testing Planned
| 10 CFR 50.73(a)(2) |
| 05000260/LER-1986-007-02, :on 860519,Div II Primary Containment Isolation Sys Power Fuse Blew,Causing Inadvertent Secondary Isolation & Initiation of Control Room Emergency Ventilation Sys. Caused by Fuse Failure.Fuse Replaced |
- on 860519,Div II Primary Containment Isolation Sys Power Fuse Blew,Causing Inadvertent Secondary Isolation & Initiation of Control Room Emergency Ventilation Sys. Caused by Fuse Failure.Fuse Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000296/LER-1986-007-03, :on 860628,Loop I of RHR Sys Declared Inoperable After Two Damaged Hangers Discovered by Design Engineers Inspecting Torus Attached Piping.Caused by High Vibration.Mod to Injection Valve Underway |
- on 860628,Loop I of RHR Sys Declared Inoperable After Two Damaged Hangers Discovered by Design Engineers Inspecting Torus Attached Piping.Caused by High Vibration.Mod to Injection Valve Underway
| 10 CFR 50.73(a)(2)(1) |
| 05000259/LER-1986-007, :on 860219,discovered That Unistrut Space Frame Supports for CRD Insert & Withdraw Lines Not Adequately Supporting Drive Tubing During Dbe.Caused by Personnel Failure to Follow Design Typicals |
- on 860219,discovered That Unistrut Space Frame Supports for CRD Insert & Withdraw Lines Not Adequately Supporting Drive Tubing During Dbe.Caused by Personnel Failure to Follow Design Typicals
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000296/LER-1986-008-03, :on 860905,LPCI Motor Generator Set Tripped from Shorted Generator Coil,Reducing RHR Capability.Damaged Generator Removed & Sent to Mfg for Repairs |
- on 860905,LPCI Motor Generator Set Tripped from Shorted Generator Coil,Reducing RHR Capability.Damaged Generator Removed & Sent to Mfg for Repairs
| 10 CFR 50.73(a)(2)(1) |
| 05000259/LER-1986-008-01, :on 860212,two Events Experienced Re Failure of Air Solenoid Valves,Utilized in Diesel Air Start Sys,To Fully Close.Caused by Corrosion Products Entering Valves from Air Sys Piping.Air Sys Blown Down Daily |
- on 860212,two Events Experienced Re Failure of Air Solenoid Valves,Utilized in Diesel Air Start Sys,To Fully Close.Caused by Corrosion Products Entering Valves from Air Sys Piping.Air Sys Blown Down Daily
| |
| 05000260/LER-1986-008-02, :on 860606,secondary Containment Isolation & Initiation of Control Emergency Ventilation Sys Occurred When Isolation Sys Power Fuse Blew.Caused by Exposed Wire on Junction Box.Fuse & Wire Repaired |
- on 860606,secondary Containment Isolation & Initiation of Control Emergency Ventilation Sys Occurred When Isolation Sys Power Fuse Blew.Caused by Exposed Wire on Junction Box.Fuse & Wire Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000296/LER-1986-009-03, :on 860908,Loop I of RHR Sys Declared Inoperable After Damaged Hanger Discovered.Caused by High Vibration in Shutdown Cooling Mode.Hanger Repaired & Design Mod Will Be Performed |
- on 860908,Loop I of RHR Sys Declared Inoperable After Damaged Hanger Discovered.Caused by High Vibration in Shutdown Cooling Mode.Hanger Repaired & Design Mod Will Be Performed
| 10 CFR 50.73(a)(2)(1) |
| 05000260/LER-1986-009-02, :on 860530,local Leak Rate Test on RHR Sys Valve 2-FOV-74-48 Improperly Performed.Caused by Inadequate Review of Sept 1984 Rev to Procedure Which Allowed Improper Valve Lineup.Procedure Revised |
- on 860530,local Leak Rate Test on RHR Sys Valve 2-FOV-74-48 Improperly Performed.Caused by Inadequate Review of Sept 1984 Rev to Procedure Which Allowed Improper Valve Lineup.Procedure Revised
| 10 CFR 50.73(a)(2)(1) |
| 05000259/LER-1986-009, :on 860226,inadvertent Secondary Containment Occurred Due to Instrument Mechanics Placing Jumper Across Terminal Points CC-38 & CC-40 to Bypass Relay 16A-K61A. Caused by Personnel Error.Personnel Cautioned |
- on 860226,inadvertent Secondary Containment Occurred Due to Instrument Mechanics Placing Jumper Across Terminal Points CC-38 & CC-40 to Bypass Relay 16A-K61A. Caused by Personnel Error.Personnel Cautioned
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000259/LER-1986-010, :on 860226,engineers Discovered Seismically Unqualified Instrument Fill Lines Connected to Pressure Suppression Chamber narrow-range Water Level Monitor Ref Leg.Caused by Inadequate Design Change |
- on 860226,engineers Discovered Seismically Unqualified Instrument Fill Lines Connected to Pressure Suppression Chamber narrow-range Water Level Monitor Ref Leg.Caused by Inadequate Design Change
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000296/LER-1986-010-03, :on 860919,inadvertent Secondary Containment Isolations Occurred.Caused by Radiation Monitor Spiking High.Detector & Converter Unit Replaced |
- on 860919,inadvertent Secondary Containment Isolations Occurred.Caused by Radiation Monitor Spiking High.Detector & Converter Unit Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000260/LER-1986-010, :on 860702,crack Indications Found in 10 Recirculation Sys Reactor Vessel Inlet Nozzle Safe Ends Due to Sensitive Ultrasonic Exam.Caused by Crevice Region Design of Safe Ends.Ends Replaced |
- on 860702,crack Indications Found in 10 Recirculation Sys Reactor Vessel Inlet Nozzle Safe Ends Due to Sensitive Ultrasonic Exam.Caused by Crevice Region Design of Safe Ends.Ends Replaced
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000260/LER-1986-010-02, :on 860702,sensitive Ultrasonic Exam Revealed Crack Indications in Recirculation Sys Reactor Vessel Inlet Nozzle Safe Ends.Corrective Action Proposals Await Development of Acceptance Criteria |
- on 860702,sensitive Ultrasonic Exam Revealed Crack Indications in Recirculation Sys Reactor Vessel Inlet Nozzle Safe Ends.Corrective Action Proposals Await Development of Acceptance Criteria
| 10 CFR 50.73(a)(2) |
| 05000296/LER-1986-011-03, :on 861023,plant Electrician Discovered LPCI Motor Generator (MG) 3DA Uncoupled.Caused by Inadequate Procedural Detail & Acceptance Criteria in Plant Maint Instructions.Lpci MG Set Recoupled |
- on 861023,plant Electrician Discovered LPCI Motor Generator (MG) 3DA Uncoupled.Caused by Inadequate Procedural Detail & Acceptance Criteria in Plant Maint Instructions.Lpci MG Set Recoupled
| 10 CFR 50.73(a)(2)(1) |
| 05000259/LER-1986-011, :on 860325,emergency Equipment Cooling Water Pumps A3,B3,B1 & C1 Started Unexpectedly When Hand Control Valve Closed During Pipe Maint.Caused by Operator Error & Poor Quality Drawings.Drawings Examined |
- on 860325,emergency Equipment Cooling Water Pumps A3,B3,B1 & C1 Started Unexpectedly When Hand Control Valve Closed During Pipe Maint.Caused by Operator Error & Poor Quality Drawings.Drawings Examined
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000260/LER-1986-011-02, :on 860718,reactor Protection Sys Tripped Due to Motor Generator (MG) Set Problem.Caused by Excessive Dust Buildup on Motor Intake & Exhaust Vents Precluding Proper Cooling.Mg Set Cleaned |
- on 860718,reactor Protection Sys Tripped Due to Motor Generator (MG) Set Problem.Caused by Excessive Dust Buildup on Motor Intake & Exhaust Vents Precluding Proper Cooling.Mg Set Cleaned
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000259/LER-1986-012-01, :on 860416,personnel Access Doors from Turbine Bldg Into Reactor Bldg Momentarily Open at Same Time.Caused by Proximity Switch & Latch Plate Out of Adjustment. Interlocking Mechanisms Repaired |
- on 860416,personnel Access Doors from Turbine Bldg Into Reactor Bldg Momentarily Open at Same Time.Caused by Proximity Switch & Latch Plate Out of Adjustment. Interlocking Mechanisms Repaired
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000260/LER-1986-012-02, :on 860918,480-volt Shutdown Board Inadvertently Deenergized When Operator Attempted to Transfer Power from Normal to Alternate.Caused by Loose Wire |
- on 860918,480-volt Shutdown Board Inadvertently Deenergized When Operator Attempted to Transfer Power from Normal to Alternate.Caused by Loose Wire
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000260/LER-1986-013-02, :on 860927,unplanned ESF Actuations Occurred Due to Failed Relay in Refueling Zone Vent Exhaust Radiation Trip Logic.Caused by Burned Coil in GE Model CR120A Relay. Relay Replaced |
- on 860927,unplanned ESF Actuations Occurred Due to Failed Relay in Refueling Zone Vent Exhaust Radiation Trip Logic.Caused by Burned Coil in GE Model CR120A Relay. Relay Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000259/LER-1986-013-01, :on 860422,Tech Spec Requirements for Secondary Containment Integrity in Refuel Zone Not Fully Met.Caused by Personnel Error Resulting in Improper Tagging of Damper Air Isolation Valves.Personnel Counseled |
- on 860422,Tech Spec Requirements for Secondary Containment Integrity in Refuel Zone Not Fully Met.Caused by Personnel Error Resulting in Improper Tagging of Damper Air Isolation Valves.Personnel Counseled
| 10 CFR 50.73(a)(2)(1) |
| 05000260/LER-1986-014-01, :on 861003,crack Detected & Sized in Reactor Water Cleanup Sys Piping.Caused by Intergranular Stress Corrosion of Sensitized Type 304 Stainless Steel.Weld Will Be Repaired & Further Insp to Be Conducted |
- on 861003,crack Detected & Sized in Reactor Water Cleanup Sys Piping.Caused by Intergranular Stress Corrosion of Sensitized Type 304 Stainless Steel.Weld Will Be Repaired & Further Insp to Be Conducted
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000259/LER-1986-015-01, :on 860424 & 29,during Installation of Permanent Switch Protective Covers on Reactor Protection Sys (RPS) MG Panel Switches,Rps Trip Occurred.Caused by Accidental Bump of Control Switch |
- on 860424 & 29,during Installation of Permanent Switch Protective Covers on Reactor Protection Sys (RPS) MG Panel Switches,Rps Trip Occurred.Caused by Accidental Bump of Control Switch
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000260/LER-1986-015-02, :on 861209,Trains a & C of Standby Gas Treatment Sys & Train a of Control Room Emergency Ventilation Actuated.Caused by Failed Coil in Relay.Coil Replaced & Safety Sys Reset |
- on 861209,Trains a & C of Standby Gas Treatment Sys & Train a of Control Room Emergency Ventilation Actuated.Caused by Failed Coil in Relay.Coil Replaced & Safety Sys Reset
| 10 CFR 50.73(a)(2) |
| 05000259/LER-1986-016, :on 860418,persistent Hydraulic Fluid Leakage Problem Observed w/Bergen-Patterson Large Bore Torus Dynamic Restraint Snubbers.Study Underway by Vendor.Seal Design Suspected Problem |
- on 860418,persistent Hydraulic Fluid Leakage Problem Observed w/Bergen-Patterson Large Bore Torus Dynamic Restraint Snubbers.Study Underway by Vendor.Seal Design Suspected Problem
| |
| 05000259/LER-1986-016-01, :on 860401,hydraulic Fluid Leakage Problem Observed w/Bergen-Patterson Large Bore Torus Dynamic Restraint Snubbers.Cause Undetermined.Vendor Conducting Study & Personnel Documenting Monthly Insps |
- on 860401,hydraulic Fluid Leakage Problem Observed w/Bergen-Patterson Large Bore Torus Dynamic Restraint Snubbers.Cause Undetermined.Vendor Conducting Study & Personnel Documenting Monthly Insps
| |
| 05000259/LER-1986-017-01, :on 860228,discovered Failure to Properly Torque Enclosing Tube Assembly Nut.Caused by Failure to Identify Torquing Requirements on Mfg Drawings & Route Objects.Nuts Tightened on Installed Switches |
- on 860228,discovered Failure to Properly Torque Enclosing Tube Assembly Nut.Caused by Failure to Identify Torquing Requirements on Mfg Drawings & Route Objects.Nuts Tightened on Installed Switches
| |
| 05000259/LER-1986-018, :on 860418,test Deficiencies Discovered During Review of intermediate-range Monitor Surveillance Instruction.Surveillance Procedures Will Be Rewritten to Fulfill Functional Test Requirements |
- on 860418,test Deficiencies Discovered During Review of intermediate-range Monitor Surveillance Instruction.Surveillance Procedures Will Be Rewritten to Fulfill Functional Test Requirements
| 10 CFR 50.73(a)(2)(1) |
| 05000259/LER-1986-019-01, :on 860608,11 & 13 Radiation Monitor Tripped High Actuating Standby Gas Treatment Sys Trains A,B & C & Control Room Emergency Ventilation Sys Trains a & B.Caused by Faulty Connector.Connector Replaced |
- on 860608,11 & 13 Radiation Monitor Tripped High Actuating Standby Gas Treatment Sys Trains A,B & C & Control Room Emergency Ventilation Sys Trains a & B.Caused by Faulty Connector.Connector Replaced
| |
| 05000259/LER-1986-020-01, :on 860619,auto Start of Two Emergency Equipment Cooling Water Pumps Occurred.Caused by out-of- Calibr Raw Cooling Water Sys Pressure Switch.Monthly Calibrs Will Be Performed Until New Switch Installed |
- on 860619,auto Start of Two Emergency Equipment Cooling Water Pumps Occurred.Caused by out-of- Calibr Raw Cooling Water Sys Pressure Switch.Monthly Calibrs Will Be Performed Until New Switch Installed
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000259/LER-1986-021, :on 860620,discovered That Reactor Bldg Flood Level Switches Not Seismically Qualified.Caused by Design Deficiencies.Alarm Response Procedures Revised to Visually Inspect Reactor Bldg |
- on 860620,discovered That Reactor Bldg Flood Level Switches Not Seismically Qualified.Caused by Design Deficiencies.Alarm Response Procedures Revised to Visually Inspect Reactor Bldg
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) |
| 05000259/LER-1986-022-01, :on 860703,potential Safety Concern Identified During Design Review Re nonsafety-grade Air Solenoid Operators on Testable Check Valves That Could Fail.Air Supply to Solenoids Removed During Operation |
- on 860703,potential Safety Concern Identified During Design Review Re nonsafety-grade Air Solenoid Operators on Testable Check Valves That Could Fail.Air Supply to Solenoids Removed During Operation
| |
| 05000259/LER-1986-023-01, :on 860717,during Attempt to Put Switchyard Capacitor Bank in Svc,Reactor Scram Occurred.Caused by Incomplete Closing of Switchyard Disconnect & Mechanical Failure.Retraining Course Developed |
- on 860717,during Attempt to Put Switchyard Capacitor Bank in Svc,Reactor Scram Occurred.Caused by Incomplete Closing of Switchyard Disconnect & Mechanical Failure.Retraining Course Developed
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000259/LER-1986-024, :on 860822,determined That nonsafety-related Piping Sys Penetrating Reactor bldg-turbine Bldg Wall Not Seismically Qualified.Caused by Design Oversight.Util Will Demonstrate Plant Qualification |
- on 860822,determined That nonsafety-related Piping Sys Penetrating Reactor bldg-turbine Bldg Wall Not Seismically Qualified.Caused by Design Oversight.Util Will Demonstrate Plant Qualification
| 10 CFR 50.73(a)(2) |
| 05000259/LER-1986-025-01, :on 860720,during Performance of Approved Maint Activity,Battery Terminal Broke Resulting in Inoperable Smoke Detectors.Caused by Miscommunication Between Personnel.Personnel Briefed on Communication |
- on 860720,during Performance of Approved Maint Activity,Battery Terminal Broke Resulting in Inoperable Smoke Detectors.Caused by Miscommunication Between Personnel.Personnel Briefed on Communication
| 10 CFR 50.73(a)(2)(1) |
| 05000259/LER-1986-026-01, :on 860724,mechanical Overspeed Trip of Standby Diesel Generator D Occurred.Caused by Failure of Assistant Unit Operator to Fully Lower Governor Setting to Low Speed Stop Position Prior to Start |
- on 860724,mechanical Overspeed Trip of Standby Diesel Generator D Occurred.Caused by Failure of Assistant Unit Operator to Fully Lower Governor Setting to Low Speed Stop Position Prior to Start
| 10 CFR 50.73(a)(2)(1) |