ML18153B281

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Insp Repts 50-280/93-15 & 50-281/93-15 on 930606-0703.Two non-cited Violations Identified.Major Areas Inspected:Plant Status,Operational Safety Verification,Maint Insps,Safety Assessment & Quality Verification
ML18153B281
Person / Time
Site: Surry  Dominion icon.png
Issue date: 07/30/1993
From: Belisle G, Branch M, Tingen S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18153B280 List:
References
50-280-93-15, 50-281-93-15, NUDOCS 9308100037
Download: ML18153B281 (21)


See also: IR 05000280/1993015

Text

Report Nos. :

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

50-280/93-15 and 50-281/93-15

Licensee: Virginia Electric and Power Company

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR~32 and DPR-37

Facility Name:

Surry 1 and 2

In~pection Conducted:* June 6 through July 3, 1993

Inspectors:

Approved by:

Scope:

. W. ~ibrResident

Inspect r

a.-~&

_S. G~ Ting~ e dent Inspector

G. ~c..:;:chief

Division of Reactor Projects

SUMMARY

7/w.3

Da't~gned

This routine resident inspection was conducted on site in the areas of plant

status, operational safety verification, maintenance inspections, safety

assessment and quality verification, Technical Specification review program,

Updated Final Safety Analysis Report improvement program, Level I project

tracking, and licensee event review. During the performance of this

inspection, the resident inspectors conducted reviews of the licensee's

backshifts, holiday or weekend operations on June 20 and 25.

Results:

In the operations area, the following items were noted:

URI 50-280,281/93-15-0l, Use of probalistic risk assessment (PRA) for

Unreviewed Safety Question Determination, pending further review by the

NRC (paragraph 3.c).

9308100037 930730

PDR

ADOCK 05000280

G

PDR~

2

Failure.to test the low pressure carbon dioxide fire protection system

per Technical Specification 4.18.D.l.b.2 was identified as part 1 to

Non-Cited Violation 50-280,281/93-15-04 (paragraph 9). Failure to

establish a continuous fire watch in accordance with Technical

Specification 3.21.B.4 was identified as part 2 to Non-Cited Violation

50-280,281/93-15-04 (paragraph 9).

In the maintenance/surveillance functional area, the following items were

noted:

Non-Cited Violation 50-281/93-15-02, was identified- for failure to

perform minor maintenance in accordance with VPAP-2002 (paragraph 4.a).

Non-Cited Violation 50-280,281/93-15-03 was identified for failure of

personnel to sequence tie-in cleanliness and fit.up/tack inspections in

accordance with VPAP~0903 (paragraph 4.b).

In the safety assessment/quality verification area, the following items were

noted:

The licensee's multi-tiered self-assessment programs collectively

incorporate various levels of corporate and station management in

ensuring safe operation. These programs are effective in contributing

to problem prevention by monitoring and evaluating plant performance and

following up with corrective action recommendations (paragraph 5).

The Corporate Nuclear Safety Independent Review Group provided effective

safety evaluaiton independent review (paragraph 5.d)!

The Integrated Trend Report identified recurring problems through

adverse trends, provided various problem/event in-depth reviews and

provided valid recommendations for corrective action (paragraph* 5.d).

The Station Nuclear Safety Operating Committee was effective in

evaluating proper substitution of manual operating action for automatic

actions and consequently ensuring that corrective actions prevented

recurrence of specific problems (paragraph 5.g).

Station Nuclear Safety's station deviation*and trending review have

improved identifying and correcting recurring problems (paragraph 5.h).

Although the Updated Final Safety Analysis Report improvement program is

progressing, a date has not be determined for completing the program

  • (paragraph 7).

The Level I Corporate and Station Project Tracking programs demonstrated

management's involvement in activities critical to station performance*

and also provided an additional method for ensuring that adequate

corrective actions are implemented (paragraph 8).

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • J. Artigas, Supervisor Quality Assurance
  • R. Bilyeu, Licensing Engineer

R. Blount, Superintendent of Engineering

  • D. Christian, Assistant Station Manager
  • D. Erickson, Superintendent of Radiation Protection

R. Gwaltney, Superintendent of Maintenance

  • R. Gardner, Outage and Planning Department
  • H. Hay, Supervisor, Quality Assur~nce
  • R. Hayes, Supervisor, Corporate Quality Assurance
  • M. Kansler, Station Manager
  • A. Keagy, Supervisor, Nuclear Materials
  • C. Luffman, Superintendent, Security
  • R. MacManus, Acting Superintendent, Engineering
  • J. McCarthy, Superintendent of Operations
  • A. Price, Assistant Station Manager
  • R. Saunders, Assistant Vice President, Operations
  • E. Smith, Site Quality Assurance Manager
  • D. Sommers, Supervisor, Corporate Licensing
  • J. Swientoniewski, Supervisor, Station Nuclear Safety

NRC Personnel

  • M. Branch, Senior Resident Inspector
  • S. Tingen, Resident Inspector
  • Attended Exit Interview

Other licensee employees contacted included control room operators,

shift technical advisors, shift supervisors and other plant personnel.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Plant Status

Unit 1 began the reporting period in power operation. The Unit was at

power at the end of the inspection period, day 143 of continuous

operations.

Unit 2 began the reporting period in power operation.

On June 20, the

unit tripped during a manual turbine runback from 100% power that was

initiated due to the A MFWP failure. This transient is discussed in

detail in section 3.b. The unit was restarted the same day and since

only one MFWP was available, the unit operated at reduced power

(i.e., 65%} for the remainder of the inspection period.

2

3.

Operational Safety Verification (71707, 42700}

The inspectors conducted frequent tours of the-control room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operations *safety and

compliance with TSs and to maintain awareness of the overall operation

of the facility.

Instrumentation and ECCS lineups were periodically

reviewed from control room indication to assess operability. Frequent

plant tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping.

Deviation reports were reviewed to assure that potential

safety concerns were properly addressed and reported.

a.

June 20, Unit 2 Reactor Trip on Loss of the A MFWP

At 4:14 a.m., on June 20, Unit 2 tripped during a manual turbine

runback initiated from 100% power as required by procedures when

the A MFWP tripped. The MFWP tripped when one of the 2 electric

driving motors shorted to ground causing the feeder breaker to

trip. The reactor tripped on feed/steam flow mismatch consistent

with a low SG level initiated from the A SG channels. A

combination of steam dump actuation, SG shrink and swell from

pressure swings, the loss of the MFWP, and the cold AFW injection

caused the SG level instability. The licensee notified the NRC as,

required on this event.

The inspectors monitored the licensee's recovery actions

subsequent to the trip and performed an independent review of

plant transient and recorder charts. Based on this review, the

inspectors determined that the plant responded as expected and

that the ECCS and reactor protective systems actuated as designed.

There were some plant equipment problems that required

investigation and repairs ~ri-0r to unit restart. The equipment

problems and licensee's corrective actions included the following:

The !RPI for rod M-10 indicated approximately 25 steps off

of the bottom and the rod bottom light was not lit after the

reactor trip. Approximately 40 minutes later after the RCS

temperature stabilized the rod bottom light illuminated and

the !RPI indication drifted toward 0.

DR S-93-0799 was

submitted and the licensee's research indicated that the

!RPI for this rod had previously experienced sluggishness

and this condition had been evaluated by engineering.

The

licensee performed a calibration of this IRPI prior to unit

restart. All rods fully inserted into the core on the

reactor trip.

The B RCP high/low oil alarm annunciated.

DR S-93-0804 was

submitted and was resolved by draining a small amount of oil

from the reservoir.

b *

3

Following the reactor trip the intermediate range Nls

decreased off-scale low.

DR S-93-0798 was submitted and the

detectors were calibrated.

Several additional BOP equipment problems were experienced

during the transient and they were evaluated and resolved

prior to unit restart.

The inspectors attended the MRB and SNSOC post trip*review prior

to unit restart. The inspectors also attended the operating crew

debriefing after the trip and prior to their leaving the site.

The licensee's post trip process appeared to be effective in

evaluating and resolving important plant equipment issues prior to

unit restart.

The unit was restarted at 6:47 p.m., on June 20 and was back

on-line at 10:33 p.m., that same day.

The unit operated at

reduced power (approximately 65%) for the remainder of the

inspection period.

Plants Readiness to Cope With Adverse Weather Conditions

The inspectors reviewed the licensee's procedures and programs to

cope with adverse weather conditions if they should arise. The

inspection considered the design basis of equipment and structures

that would be exposed to wind forces from either a tornado or a

hurricane to include emergency response and event assessment

equipment.

The inspectors held meetings with both site and

corporate personnel knowledgeable in wind loading design.

The

inspectors used Surry drawing 11448-FY-lD Revision 17, Plot Plan

Surry Power Station, as the basis for discussing the wind loading

design for the major structures and equipment.

Equipment and structure design is described in sections 2.2.2 and

15.2 of the UFSAR.

Table 15.2-1 list structures and equipment and

their design basis. A tornado wind speed of approximately 300 mph

and a hurricane wind speed of 137 mph were assumed in the UFSAR

analysis. However, the design wind loading basis for all

equipment and structures located at the plant are not described.

New buildings such as the administration building and the new

radwaste facility are also not included.

From the UFSAR review and discussions noted above, the inspectors

determined that many structures and equipment exposed to the

maximum winds from a hurricane or tornado could be damaged and may

not survive.

For example, non-safety related structures and

equipment are generally designed to the BOCA code, which for the

location and function of Surry as a power station would be

designed to withstand a wind force of approximately 100 mph .

4

Examples of BOCA designed structures and equipment include but are

not limited to the following:

LEOF

TSC

New Security and Administrative Building

DSC

CAS/SAS

New Radwaste Building

Switchyard and Transformers

Fire Tanks

Above Ground EDG Fuel Oil Tank

Meteorological Towers and Emergency Sirens

Environmental Monitoring Stations

In addition to the above, the roofs and siding of several other

buildings are also only designed for BOCA code winds.

For

example, the Auxiliary Building roof and some above ground siding

are designed for 100 mph winds.

There is also semi-permanent installed equipment such as hydrogen

tanks, water processing trailers and Sea-Vans that may not survive

design basis wind forces.

In addition, loose low level rad waste

is stored in a metal storage shed within the protected area. This

shed is designed for BOCA code winds.

The inspectors also reviewed abnormal operating instruction

ADI O-AP-37.01 revision 1, Abnormal Environmental Conditions,

which provides guidance for operations to ensure safe plant

conditions in the event of impending adverse weather conditions.

This procedure established the licensee's philosophy for unit

conditions based on weather forecast, time before land fall,

emergency plan implementation, and management's heightened

awareness or degrading conditions. The licensee's emergency

declaration is described in EPIP-1.01 Attachment 1, Emergency

Action Level Table (TAB L) Natural Events.

The inspectors also held meetings with the corporate EP manager

and an OER person to discuss the status of the licensee's review

of lessons learned from Hurricane Andrew and any corrective

actions being implemented.

The licensee's lesson learned review

is being conducted through their normal OER process.

The licensee

indicated that the OER report will be finalized and issued to

management in the mid-summer timeframe.

The inspectors also

reviewed an informal checklist that contained, in bullet form,

many significant "What-To-Dos" but there was little or no "How-To-

Dos".

The licensee indicated that the checklist could be used if

needed in the event of adverse weather.

The inspectors concluded

that although the licensee's program has not been completely

formalized, the modifications that have been made represent

improvement over their previous program.

c.

5

Feedwater Isolation System Review

During a station deviation review, the inspectors became aware of

DR S-93-0774 which described a possible unreviewed safety question

associated with isolating the feedwater system.

Feedwater

isolation is needed to protect against the consequences of a steam

line failure that could cause a pressurization of the containment

or a RCS cooldown with a loss of reactor shutdown margin.

The feedwater isolation function. is described in the UFSAR,

section 14.3.2. A detailed description is not provided but the

system consists of a safety related protective system that is

actuated by an SI signal which causes automatic closure of all

three pairs of air operated FWRVs and bypass FWRVs and the

tripping of the MFWPs.

Additionally, the tripping of the MFWPs

through non-safety related breakers causes the non-safety related

discharge valves (1 or 2-FW-MOV-150 or 250A&8) which are powered

from non-safety electrical busses to close.

In the past, Surry has disabled (jacked) a FWRV in the open

position to a specific SG; therefore, it would not automatically

close on -an SI signal. The licensee performed SEs (i-.e.,

10 CFR 50.59) reviews for this evolution since 1989. Recent SEs

determined that jacking the valve open to perform maintenance on

the control or feedback circuitry was an acceptable practice as

long as the redundant tripping of the MFWPs was operable and

compensatory actions were in place to close another non-safety

feedwater isolation MOV (1 or 2-FW-MOV-154 or 254A, 8, C) just up

stream of the FWRV, from the control room if necessary.

DR S-93-0774 was issued because of the licensee's independent

review group's assessment of the SE 92-173, dated September 24,

1992, which addressed placing a FWRV on its jack. The package

reviewed included administrative control form (AC S2-92-807) and

TS interpretation (TSI-014), including safety evaluation

(SE 92-1738):

The independent review group's report to the

station, attached to the DR, indicated that for certain postulated

cases, termination of feedwater flow during a steam line break

accident may not be achievable with current compensatory actions

and within the time frame assumed in the steam break accident

analysis. The following information was taken from that report:

  • The safety evaluation (SE 92-1738) assumes that the feedwater

isolation will occur within 30 seconds through closure of the

feedwater isolation MOVs.

For a total LOOSP, the MFWP and

condensate pumps will shutdown due to a loss of electrical power

thereby terminating feedwater within the required time.

However,

the SE did not address the impact of a partial loss of station

service electric power. A potential scenario is that a loss of a

4160V station service bus with one FWRV jacked open could result

in continuous feedwater flow to the SG that has experienced a

MSL8.

The combination of a feedwater isolation MOV and MFWP

6

discharge MOV loosing power, MFWPs tripped on the SI signal, and

the condensate pump continuing to run (from the unaffected station

service busses), results in continued feedwater flow.

This

scenario assumes a MSLB upstream of the MSTVs and the single

failure being a loss of a 4J60V station service bus.

Feedwater

flow would continue until the operators locally closes the

feedwater isolation MOV or trips the condensate pump.

The time

required to perform these compensatory actions would be greater

than the 30 seconds assumed in the safety analysis.

After being informed of the above potential unreviewed safety

question item, the plant initiated actions to~evaluate the

condition and determine reportability. The station's review

resulted in generating another SE.(93-14i) and a TS interpretation

that allows plant operations to continue with an administrated

8-.hour AOT for an inoperable FWRV (i.e., jacked open).

The new SE

was based on reliability and probability considerations which the

licensee considered acceptable by NSAC-125, Guidelines for

10 CFR 50.59 Safety Evaluations.

The licensee also considered

that manual operator action to trip the FWRV off the jack and

allow it to close within the 30 second time limit would be

achievable and acceptable.

The inspectors questioned the use of probability assessment in

making the decision that the modification (i.e., loss of automatic

isolation of main feedwater) does not constitute an unreviewed

safety question.

It is clear that the inability to automatically

terminate feedwater flow was not considered in the safety ~nalysis

describ~d in the UFSAR.

Therefore, the probability of occurrence

or consequences of an accident or.malfunction of equipment

important to safety previously evaluated in the safety analysis

report may be increased.

The licensee's calculation (S-896)

reviewed by the inspectors indicated that the combined increase in*

probability for the event described was insignificant if an AOT Of

8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> is used.

The licensee, therefore, considered it

acceptable to operate with the FWRV on the jack if an AOT did not

result in an increase in probability of occurrence.

The licensee's recent SE (93-142) also indicated that the

operators could close the jacked open FWRV within the 30 seconds

needed to terminate feedwater flow-for the steam break accident.

However, the SE contained statements that the basis was limited

risk associated with operating on the jack and not dependent on

strict operator performance to close the FWRV within the 30

seconds assumed.

If it could be demonstrated that manual action

was addressed by a procedure and could be reliably performed

within the values bounded by the accident analysis, it appears

that the guidance of GL 91-18 could apply for future occasions~

The inspectors held discussions with NRC staff and were informed

that the use of NSAC-125 has not been endorsed by the NRC.

Therefore, the use of a probability assessment is in question.

4.

7

This item is identified as URI 50-280, 281/93-15-01, Use of PRA

for Unreviewed Safety Question Determination, pending further

review by the NRC.

d.

Housekeeping

In an effort to upgrade station housekeeping, the Assistant

Station Manager is walking down areas of the station with the

supervisors responsible for housekeeping in the area.

On June 9,

the inspectors accompanied the Assistant Station Manager and l&C

Supervisor on a housekeeping tour of the auxiliary building 45

foot level. _During this tour, general materi-al condition and

cleanliness were monitored and out of the way places such as under

. and behind equipment were inspected.

Examples of items noted

during the tour were red tape on cable tray covers, coat hanger

wire dangling from conduit, damaged label plates, loose junction

box covers, and loose fasteners on ventilation equipment.

The

inspectors noted that during the inspection period, the Vice

President of Nuclear Operations conducted a similar walkdown of

the auxiliary building basement.

The inspectors concluded that

housekeeping has improved and management walkdowns have

contributed to the improvement .

Within the area inspected, one URI was identified.

Maintenance Inspections (62703) (42700)

During the reporting period, the inspectors reviewed the following

maintenance activities to assure compliance with the appropriate

procedures.

a.

Leak Repair at Mechanical Joint

On June 14, the inspectors witnessed the licensee repa1r1ng

a leaking mechanical joint in the piping/tubing to charging pump

2-CH-P-lB suction pressure gage 2-CH-399.

The mechanical joint

was disassembled, inspected and reassembled. This maintenance was

considered minor maintenance and accomplished in accordance with

deficiency card IC-93-0175.

The maintenance was isolated

utilizing operator standby and the joint was leak tested when

placed back into service.

The inspectors reviewed Attachment 13

of VPAP-2002, Work Request and Work Order Tasks, dated

January 1, 1993.

The attachment describes criteria for

determining which tasks are considered minor maintenance and can

be performed with deficiency cards. Maintenance accomplished per

deficiency cards is generally simple in nature and does not

require a WO or written instructions.

Item (d) of Attachment 13

states that minor maintenance shall not effect the integrity of

safety related components and disassembly of a safety-related

component is not a minor maintenance activity. The inspectors

concluded that disassembling the mechanical joint in the

b.

8

piping/tubing to pressure gage 2-CH-399, a safety related system,

per a deficiency card IC-93-0175 was not in accordance with

Item {d) of Attachment 13. This was ide~tified as

NCV 50-281/93-15-02~ Failure to Perform Minor Maintenance in

Accordance With Administrative Procedure VPAP-2002.

This NRC

identified violation is not being cited because criteria specified

in Section VII.B of the NRC Enforcement Policy were satisfied.

As

corrective action, a change to VPAP-2002 was initiated to allow

disassembly of components in safety related systems in some

instances.

Welding a Service Radiation Monitor

The inspectors reviewed part of a modification for the Unit 2

radiation monitor for the RS heat exchanger SW cooling lines.

This radiation monito'r's function is to detect any tube leak in

the RS heat exchanger. The review was conducted on the

documentation for welding on the line going to the C radiation

monitor, mark numb'er 2-SW-P-5C.

There are approximately 16 welds

in this piping section.

During the inspector's welding and inspection documentation

review, the licensee stated that a contractor employee had

questioned whether a hold point was being bypassed when the tie-in

cleanliness inspection and the fit up/tack inspections were both

performed at the same time.

The licensee concluded that this was

an acceptable practice. The inspectors performed an independent

assessment of this conclusion.

The inspectors reviewed the weld data sheet and the appropriate_

procedures that were associated with welding and QC hold points.

A typical data sheet review shows that the first QC hold point is

the tie-in cleanliness and the second QC hold point is the one for

fit up/tack.

The inspectors reviewed administrative procedure

VPAP-0504, Technical Procedure Writers Guide, revision 1.

In the

definition part of this procedure {paragraph 4.5), a required QC

hold point is defined as a pre-selected location written in a

procedure that identifies a portion or portions-of the procedure

which requires witnessing by the QC department personnel or the

maintenance QMT personnel.

The procedure also states that work

shall not progress beyond the established hold point until the

required inspection is performed.

Attachment number 14 of this procedure gives the criteria for QC

hold points in procedures.

Paragraph 6 of this attachment gives

the required QC hold points for welding procedures pertaining to

safety-related and seismic items.

Part 6.d states in part that

cleanliness inspection of piping and piping components may be a

part of the fit up/tack inspection. This would allow the QC

inspectors to perform both of these inspections at the same time.

However, the statement that the cleanliness inspection may be a

part of the fit up/tack inspection was not part of the procedure

-*-

5.

g-

VPAP-0903, Control of Welding, revision 0, which was being used

for the weld inspection.

Administrative procedure VPAP-0903 was reviewed for a description

of the attributes to be inspected for the welding process.

_ -

Attachment 2 to that procedure states that the tie-in cleanliness

inspection is intended to insure that nothing is left in the pipe

before fit up.

The cleanliness inspection as part of the fit

up/tack inspection was not included in the procedure. Discussions

with some of the licensee's QC inspectors revealed that they

perform both inspections at the same time on occasions when no

adverse affects are possible. The decision a~ to when to perform

both of these inspections at the same time is made by the

_individual QC inspector.

The insp~ctors discussed this decision with the QC inspector that

made the decision relating to the contract employee's fit up.

The

QC inspector stated that there would be no problem inspecting the

attributes reql,lired by the cleanliness hold point since the length

of the two inch diameter pipe was two inches with an open end.

The inspectors agree that technically the inspection for

cleanliness could have b_een performed at the time of the fit

up/tack inspection, but VPAP-0903 did not have the words that

would authorize the performance of both inspections at the same

time.

The inspectors disagreed with the licensee's original

conclusion that it was acceptable to perform the tie-in

cleanliness and fit up/tack inspections simultaneously when

performi.ng these inspections in accordance with VPAP-0903.

Failure of personnel to sequence tie-in cleanliness and fit*

up/tack inspections in accordance with VPAP-0903 was identified as

NCV 50-280, 281/93-15-03. This NRC identified violation is not

being cited because criteria specified in Section VII.B of the NRC

Enforcement Policy were satisfied.

The licensee is currentiy changing VPAP-0903 to include the option*

.for performance of both the cleanliness and tie in/tack

inspections at the same time as it is authorized in the VPAP-0504.

Within the areas inspected, two NCVs were identified.

Safety Assessment and Quality Verification (40500)

The inspectors reviewed the licensee's activities associated with

safety policy implementation, station performance, safety review

committees, and feedback from self assessment programs and QA

activities. A multi-tiered program utilizing corporate and station

resources are utilized to accomplish these activities; The specific

areas reviewed were the Nuclear Business Plan, NOB, MSRC, CNS, Nuclear

Quality Assurance, MRB, SNSOC, and Station Nuclear Safety.

Some of

-these functions.are specifically required by TS and other areas are

performed in addition to TS requirements.

. I

a.

b.

c.

10

Nuclear-Business Plan

The inspectors reviewed the Virginia Power Nuclear Business Plan

. Goal Performance for May 1993.

The purpose of this report is to

assess the performance of Surry and North Anna in meeting their

established goals. The report assesses plant performance,

nuclear/industrial safety, cost management and regulatory

compliance.

Items assessed in the report were categorized as

significant strengths, satisfactory, improvement needed or

significant weakness.

Non-outage corrective maintenance back log

and EOG reliability were examples of significant strengths. *

Several areas were considered needing improvement.

Reactor trips

was an area needing improvement.

The goal for Surry-is to have

two or less unplanned reactor trips per year and, as of May 1993,

the units have already had two reactor trips with over half a year

in the assessment period remaining.

The report did not identify

any areas as significant weaknesses.

Nuclear Oversight Board

The purpose of the NOB is to provide an independent review and

oversight role of nuclear activities at the senior managem~nt

level. The Board advises the Senior Vice President, Nuclear and

the eight members consist of senior nuclear utility executives and

consultants.

Board review and recommendation results are

presented to the Virginia Power Pre~ident and Chief Executive

Officer.

Management Safety Review Conunittee

The MSRC function and activities are specified in TSs.

The

inspectors reviewed MSRC member qualifications and MSRC meeting

minutes for 1992 and 1993.

The inspectors concluded that MSRC

committee members were well qualified and experienced and that

meeting frequencies met TS requirements.

IPE flooding and the

increase in number of precursors to *significant events in 1992

were examples of MSRC concerns.

The inspectors verified that MSRC

issues were being tracked and properly closed.

d.

Corporate Nuclear Safety

CNS is divided into three groups, independent safety, review, OER,

and independent review.

CNS also has general responsibilities

that are shared between the three groups. These responsibilities

include coordinating involvement with WOG, integrated performance

trending, root cause evaluation, and DR/COE data base.

The primary responsibilities of the CNS independent safety review

group are to review events that occur at the station which

includes identifying root causes and corrective actions, perform

assessments of various station activities, and independently

monitor station performance. The inspectors reviewed CNS event

11

reviews or assessments*associated with tagging events, contractor

events, shutdown ~anagement, and administrative controls of

. radioactive materials and radiation exposure.

The inspectors

concluded that these reports were comprehensive in that root

causes and corrective .act i ans were i dent i fi ed.

In addition, to

reviewing the actions associated with a single event, similar

types of events are also reviewed in order to identify common or

repetitive causes.

The primary responsibility of the CNS OER group is to evaluate

industry events for significance and applicability to Virginia

Power and recommend action to avoid similar o~currences.

Examples

of sources of industry events monitored by the CNS OER group are

INPO SOERs and Nuclear Network, NRC Information Notices and

Generic Letters, and Vendor 10 CFR 21 Notifications. The group

  • also monitors Virginia Power LERs and NRC violations for common

applicability and recommends corrective actions.

In 1993, the

group began to monitor NRC violations issued to other utilities

.

for applicability at Virginia Power stations. During the previous

SAlP assessment period, a weakness was identified in the area of

CNS follow up on corrective action for recommendations from older

event reviews.* This issue was reviewed during this inspection

period and the inspectors concluded that this wea~ness was

corrected in that CNS verified that these corrective actions were

completed.

During a previous inspection, a weakness was

identified in that CNS closure summaries were not being completed

with the suggested 90 day program guidelines. This issue was also

reviewed during this inspection period and considered corrected in

  • . that there were no l anger any overdue closure surnmari es.

The primary responsibility of the CNS independent review group is

review SNSOC activities and to manage the Virginia Power

10 CFR 50.59 SE Program which includes reviewing all SEs prepared

by the Surry site engineering group.

The group has reviewed

approximately 450 Surry SEs throughout the current SALP assessment

period.

Of the 450 SEs the group had written comments on 20 SEs,

and 5 SE's were considered inadequate.

Four of these five SEs

were considered inadequate because they did not properly address

  • contaminated systems and had minor safety significance. The fifth

SE identified a potential unreviewed safety question associated

with placing a FWRV on its jack. This issue was previously

discussed in paragraph 3.c and was identified as a URI.

The

inspectors noted that SEs associated with placing FWRVs on their

jacks were reviewed on four other occasions since. 1989 prior to

the recent review and did not identify any problems. * The

inspectors questioned why the potential unreviewed safety question

was not identified on the previous reviews and were informed that

in the past reviews the most severe events and most bounding

analyses in determining the acceptability of this activity were

considered *. In this case, the most severe event considered, total

loss of off site power, did not have the most sever consequences.

The inspectors concluded that overall, the CNS independent review

-'

12

group provided effective independent review of SEs.

As a result

of the comments generated during the CNS independent review of

SEs, the station is in the process of developing a task team to

develop methods for improving SEs. _

One of the general responsibilities of CNS is to develop quarterly

Integrated Trend Reports.

The purpose of _this report is to assess

station issues and events at Surry and North Anna to determine if

adverse trends exist and identify any adverse trends to senior

management.

If adverse trends are identified the report provides

recommendations for corrective actions. The inspectors reviewed

the Integrated Trend Report dated June 1, 1993.

The report

identified areas with sustained improving trends and areas with

adverse trends.

Examples of areas of improved trends were

reactivity control, radiation releases, and overall human

performance.

Example of areas with adverse trends were radiation

monitor failures, relay failures, and work practices. The report

also identified and trended significant and precursor events.

The

report indicated that in the first quarter of 1992 the number of

significant events associated with plant transients was abnormally_

high due to two reactor trips that occurred during that period.

The inspectors verified that recommendations were tracked until

completed. The inspectors concluded that the Integrated Trend

Report identified recurring problems through adverse trends,

provided in-depth reviews of various problems/events, and provided

valid recommendations for corrective action.

e.

Nuclear Quality Assurance

TS 6.2.h specifies audits and frequencies that are required to be

routinely performed.

In 1992, 20 audits were performed and 15

audits are scheduled to be performed in 1993.

The inspectors

verified that audit open items were being tracked and pursued.

The QA audit tracking report listed four open 1991 audit items, 27

open 1992 audit items, and 11 1993 open items. The inspectors

reviewed the 1991 items and concluded that audit items corrective

actions were effectively implemented.

The QA department routinely performs assessments that are beyond

TS requirements. The purpose of these assessments are to evaluate

performance in specific areas. Approximately thirty assessments

were performed in 1992 and twenty-one assessments have been

performed or are in the process of being performed in 1993.

Assessments are performed in areas where performance problems or

need of enhancement have been identified on recently implemented

programs, on followup on previous assessement findings, or on

concerns in areas expressed by corporate or station management.

Assessment findings are reviewed with station management and are

tracked as open items until closed. The QA department also

routinely observes maintenance activities at the station.

Findings from these observations are documented and discussed with

the Superintendent of Maintenance. These observations are also

f.

g.

h.

13

utilized to trend station performance in the CNS integrated trend

report.

Station QA personnel are encouraged to visit counterparts at other

nuclear plants to compare programs and identify possible

improvements.

Corporate and North Anna personnel are utilized to

perform Surry audits. Also, Surry personnel are used to perform

North Anna audits. Assessments also utilize North Anna and

corporate personnel.

The department participates in an auditor

exchange program with other utilities, participates in a utilities

group that independently audit QA programs, and supervisors are

required to visit INPO 1 or SALP 1 rated site~ on a yearly bases.

Management Review Board

The MRB members are the Station Manager, two Assistant Station

Managers, and Station QA Manager. The overall function of the

- board is to overview and coordinate station activities. The

inspectors reviewed the 1992 and 1993 MRB meeting minutes.

Typical items reviewed at the weekly MRB meetings were temporary

modifications, JCOs, and compensatory actions. Other areas

reviewed were deferred maintenance items, RCEs, plant equipment

problems, plant events, Nuclear Safety Assessments Reports,

station assessments, and DR Trend Reports.

The MRB also

determines the ratings of the quarterly Performance Annunciator

Program windows.

The MRB has been effective in reviewing station

activities.

Station Nuclear Safety Operating Committee

TS 6.1.C.l specifies the requirements for the SNSOC composition,

meeting frequency, responsibilities, and authority. Throughout the

current SALP assessment period the inspectors have monitored SNSOC

performance.

The inspectors concluded that TS were met with

respect to SNSOC composition, duties, and meeting frequencies.

The inspectors observed SNSOC meetings and concluded that the

overall, in-depth review of areas important to safety were being

performed and that the members were qualified and experienced in

diverse disciplines. The SNSOC was especially effective in

evaluating proper substitution of manual operating action for

automatic actions and ensuring corrective actions prevented

specific problem recurrence~

Station Nuclear Safety

Tracking and trending DRs is the SNS department's responsibility.

The inspectors reviewed the results of the Station Deviation Trend

Report for the first quarter of 1993. This report trended the

failure mode/mechanism associated with DRs processed from January

through March 1993.

SNS issues a DR trend reports quarterly. The

four major trend categories were human performance, system

14

performance, component performance and specific equipment

performance.

The DR trend report identified five recommendations

based on the trend results. For example, one recommendation was

associated with recurring spiking problems on the ventilation

system Kamen radiation monitors. This recommendation included

corrective action. Recommendations are assigned CTS numbers that

are tracked until closure.

SNS also reviews DRs daily for recurring problems, and if the DR

is associated with a recurring problem it is discussed during the

morning supervisor meeting.

During the previous SALP assessment

period, examples were identified where the licensee indicated a

willingness to live with several recurring problems.

The SNS's

review of DRs and DR trending has improved identifying and

correcting recurring problems.

During this SALP assessement

period, recurring problems have been identified, components

declared inoperable if applicable, and corrective action

initiated. However, in some cases such as control room chillers

and station radiation monitors, corrective actions are long term

and problems will continue to occur until these long term

corrective actions are fully implemented.

Preparing the quarterly Nuclear Safety Assessement Report is

another responsibility of the SNS department.

The inspectors

reviewed the Surry Nuclear Safety- Assessment Report for the first

quarter of 1993.

The report assesses plant performance in the

following areas: past and current performance in key safety areas,

events that challenge the operator and the plant, significant

events and precursors, RCS and SG integrity, and material

condition.

Key INPO performance indicators are utilized to

compare the performance of Surry performance to the industry. The

report indicated that the state of nuclear safety in Unit 1 was

considered degraded when compared to previous reports.

Two

reactor trips, safety injections, and forced power reductions

contributed to the degraded performance.

The state of nuclear

safety in Unit 2 was considered high for the period. Three events

that occurred in the first quarter of 1993 were considered

reductions in the margin of safety.

Two events were associated

with turbine driven AFW pumps tripping due to degraded steam traps

which was previously discussed in NRC Inspection Report Nos.

50-280, 281/93-07.

The third event was associated with two main

control room chillers being inoperable which was discussed in LER

50-280, 281/93-05.

The inspectors concluded that the multi-tiered programs discussed above

collectively incorporate various levels of corporate and station

management in ensuring safe operation. The licensee's self-assessment

programs are effective in contributing to preventing problems by

monitoring and evaluating plant performance and following up on

corrective action recommendations.

Within the areas inspected no violations were identified.

15

6.

TS Review Program (40500)

7 *

The inspectors assessed the licensee's TS review program results. The

licensee implemented this program in September 1992, and the program is

scheduled for completion in October 1993.

This program reviews TS

surveillances and verify that the surveillances were being properly

performed.

This review identified examples where components important to safety

were not being tested.

In most cases TSs did not require testing. It

was identified that the circuitry that prevents the--RHR inlet MOVs from

opening at a high RCS pressure as not being functionally tested. It was

also identified that the manual SI actuation logic was not being fully

tested. These findings are being tracked by the licensee and will

remain open until resolved.

The inspectors reviewed the applicable TSs

and concluded that these components were not specifically addressed by

TSs to require routine testing.

This review has identified the following components that were not being

tested as required by TSs:

-

TS Table 4.1-1, Item 28 requires that turbine trip inputs to

reactor protection be tested prior to each startup. The review

identified that the turbine trip signals were tested prior to

startup but that the turbine trip signal to the reactor protection

system was not being tested prior to startup. The input to

reactor protection was being tested on a monthly basis after the

units were at power.

LER 50-280/93-07 was issued as a result of

this finding.

TS Table 4.1-1, Item 32 a, requires a refueling calibration of the

steam generator lo-lo level AFW auto start signal. This

calibration includes functional testing of the motor and turbine _

driven AFW pumps.

The review tdentified that the turbine driven

auto-start circuit was not being fully tested in Unit 2.

When

this was identified, a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> LCO was entered in accordance with

TS 4.0.3. The testing was completed satisfactorily within the

24-hour period.

Addendum I to LER 50-280/93-07 is scheduled to be

issued as a result of this finding. This testing had been

satisfactorily accomplished in Unit I.

Other less significant procedural errors have been identified and are

also being tracked as open items until resolved.

The inspectors will

continue to monitor this review.

Within the areas inspected no violations were identified.

UFSAR Improvement Program (40500)

During the previous SALP assessment period, a weakness was identified in

that the UFSAR was not accurate.

The inspectors discussed the UFSAR

l

,,

8.

16

Improvement Program status with the corporate UFSAR coordinator for

Surry. According to the coordinator, review of plant operation

described in the UFSAR has been completed and appropriate revisions

made, the UFSAR was reviewed and verified that there were no unresolved

safety questions, and UFSAR changes have been incorporated such that

there is no longer a backlog.

The licensee has identified chapter 2,

Site Description, as the current priority for review and is in the

process of revising the chapter. Chapter 2 is currently scheduled to be

completed by April 1994~ The licensee currently plans to assign the

remaining UFSAR chapters to various Virginia Power organizations for

review and revision. Although the program is progressing, a date has

not been determined for completing the UFSAR Improvement Program.

Within the areas inspected, no violations were identified.

Level I Project Tracking (40500)

The Level I Project Tracking Program establishes process for management

to track activities critical or essential to the success of the nuclear

program.

Corrective actions for INPO and NRC SALP deficiencies are

examples of items tracked under Level I. The inspectors reviewed the

open projects on the Corporate Level I Report dated June 21,1993.

The

CNS Integrated Trend Report, Maintenance Backlog Monitoring Data,

Station Staff Visits to other plants to observe Industry Good Practices,

and developing a Leadership Program for first and second line

supervisors-were examples of corporate Level Is. The inspectors also

reviewed the open projects on the Station Level I Report dated

June 29, 1993.

TS review project, TPUP completion, 1993 INPO

preparation, ground water intrusion program, and Post Trip review

process were examples of station Level Is. The inspectors concluded

that the Level I Corporate and Station Project Tracking Programs

demonstrated management's involvement in activities critical to station

perf9rmance and also provided an additional method for ensuring adequate

corrective actions are implemented.

Within the areas inspected, no violations were identified.

9.

Licensee Event Review (92700)

The inspectors reviewed the LER listed below .and evaluated the adequacy

of the corrective action. The inspectors' review also included followup

of the licensee's corrective action implementation:

(Closed) LER 280/92-11, Incomplete Low Pressure Carbon Dioxide Fire

Protection System Nozzle Testing Due to Procedure Deficiency and Lack of

Continuous Fire Watch.

TS 4.18.D.l.b.2 requires that operability of the

low pressure carbon dioxide fire protection system be demonstrated every

18 months by verifying flow from each nozzle during a puff test. During

the performance of a QA Fire Protection audit, it was identified that

flow was not being verified at all discharge nozzles.

As immediate

corrective action, the low pressure carbon dioxide fire protection

system was declared inoperable and a continuous fire watch was

established in accordance with TS 3.21.B.4. Failure to test the low

'

'

17

pressure carbon dioxide fire protection system per TS 4.18.D.l.b.2 was-

identified as part 1 to NCV 50-280, 281/93-15-04. This violation will

not be subject to enforcement action because the licensee's efforts in

identifying and correcting the violation met the criteria specified in

Section VII.B of the Enforcement Policy.

As corrective action, the

licensee revised l-PT-24.3b, Fire Protection Low Pressure Carbon Dioxide

System Puff Test, on September 22, 1992, to require that flow from each

nozzle be verified. The inspectors reviewed the procedure and verified

that the corrective action was implemented. Also as corrective action,

the licensee was in the process of performing a TS surveillance review

to ensure that they are being properly performed. This review is

discussed in paragraph 6.b.

-

When this condition was identified, a continuous fire watch was

stationed per TS 3.21.B.4. During a subsequent fir~ watch turnover, the

fire watch was inadvertently changed from continuous to hourly due to

erroneous communication between shifts. When this was identified, a

continuous fire watch was reestablished. Failure to establish a

continuous fire watch in accordance with TS 3.21.B.4 was identified as

part 2 to NCV 50-280, 281/93-15-04. This violation will not be subject

to enforcement action because the licensee's efforts in identifying and

correcting the violation meet the criteria specified in Section VII.B of

the Enforcement Policy.

As corrective action, the licensee revised the

fire watch assignment sheet to clearly specify continuous or_ hourly fire

watch inspection requirements.

The inspectors reviewed the fire watch

assignment sheet and verified the corrective action was implemented.

Within the areas inspected, one NCV was identified.

10.

Exit Interview

The results were summarized on July 12,- 1993, with those individuals

identified by an asterisk in Paragraph I.

The following summary of

inspection activity was discussed by the inspectors during this exit:*

Item Number

Status

URI 50-280, 281/93-15-01

OPEN

NCV 50-280/93-15-02

CLOSED

NCV 50-280, 281/93-15-03

CLOSED

Description

(Paragraph No.)

Use pf PRA for Unreviewed

Safety Question Determination

(paragraph 3.c).

Failure to Perform Minor

Maintenance in Accordance

With VPAP-2002 (paragraph

4.a).

Failure of Personnel to

Sequence Tie-in Cleanliness

and Fit Up/Tack Inspections in

Accordance With VPAP-0903

(paragraph 4.b).

,I

. '

NCV 50-280, 281/93-15-04

18

CLOSED

Failure to Test Fire

Protection System and Failure

to Establish a Continuous Fire

Watch in Accordance with TSs

(paragraph 9) ..

LER 50~280/92-11

CLOSED

Incomplete Low Pressure Carbon

Dioxide Fire Protection System

Nozzle Testing Due to

Procedure Deficiency and Lack

of Continuous Fire Watch

(paragraph 9).

Proprietary information is not contained in this report. Dissenting comments

  • were not received from the licensee.

11.

Index of Acronyms and Initialisms

AFW

AOI

AOT

BOCA -

BOP

CAS

CDE

CFR

CNS

CTS

DR

ECCS -

EDG

EP

EPIP -

FWRV

-

l&C

INPO -

IPE

IRPI -

JCO

LCO

LEOF -

LER

LOOSP -

MFWP -

MOV

MRB

MSLB

-

MSTV -

MSRC

-

NI

NCV

NOB,

AUXILIARY FEEDWATER

ABNORMAL OPERATING INSTRUCTION

ALLOWED OUTAGE TIME

BUILDING OFFICIALS AND CODE AUTHORITIES

BALANCE OF PLANT

CENTRAL ALARM STATION

CAUSE DETERMINATION EVALUATION

CODE OF FEDERAL REGULATION

CORPORATE NUCLEAR SAFETY

COMMITMENT TRACKING SYSTEM

DEVIATION REPORT

EMERGENCY CORE COOLING SYSTEM

EMERGENCY DIESEL GENERATOR

EMERGENCY PLAN

EMERGENCY PLAN IMPLEMENTING PROCEDURES

FEEDWATER REGULATION VALVE

INSTRUMENTATION & CONTROL

INSTITUTE OF NUCLEAR POWER OPERATION

INDIVIDUAL PLANT EVALUATION

INDIVIDUAL ROD POSITION INDICATION

JUSTIFICATION FOR CONTINUED OPERATION

LIMITING CONDITION FOR OPERATION

LOCAL EMERGENCY OPERATIONS FACILITY

LICENSEE EVENT REPORT*

.

LOSS OF OFFSITE POWER

MAIN FEEDWATER PUMP

MOTOR.OPERATED VALVE

MANAGEMENT REVIEW BOARD

MAIN STEAM LINE BREAK

MAIN STEAM TRIP VALVE

MANAGEMENT SAFETY REVIEW COMMITTEE

NUCLEAR INSTRUMENTATION

NON-CITED VIOLATION

NUCLEAR OVERSIGHT BOARD

I

..

,)

NRC

OER

osc

PRA

QA

QC

QMT

RCE

RCP

RCS

RHR

RS

SALP

SAS

SE

SG

SI

SNS

SNSOC -

SOER -

SW

TPUP* -

TS

TSC

UFSAR -

URI

VPAP -

WO

WOG

19

NUCLEAR REGULATORY COMMISSION

OPERATIONAL EXPERIENCE REVIEW

OPERATIONS SUPPORT CENTER.

PROBABILISTIC RISK ASSESSMENT

QUALITY ASSURANCE

  • QUALITY CONTROL

QUALITY MAINTENANCE TEAM

ROOT CAUSE EVALUATION

REACTOR COOLANT PUMP

REACTOR COOLANT SYSTEM

RESIDUAL HEAT REMOVAL

RECIRCULATION SPRAY

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

SECONDARY ALARM STATION

SAFETY EVALUATION

STEAM GENERATOR

SAFETY INJECTION

STATION NUCLEAR SAFETY

SURRY NUCLEAR SAFETY AND OPERATING COMMITTEE

SIGNIFICANT OPERATING EVENT REPORT

SERVICE WATER

TECHNICAL PROCEDURES UPGRADE PROGRAM

TECHNICAL SPECIFICATION

TECHNICAL SUPPORT CENTER

UPDATED FINAL SAFETY ANALYSIS REPORT.

UNRESOLVED ITEM

VIRGINIA POWER ADMINISTRATIVE PROCEDURE

WORK ORDER

WESTINGHOUSE OWNERS GROUP