ML18152A454

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Insp Repts 50-280/93-23 & 50-281/93-23 on 930905-1002. Violations Noted.Major Areas Inspected:Plant Status, Operational Safety Verification,Maint Insps,Suveillance Insps,Ler & Action on Previous Insp Items
ML18152A454
Person / Time
Site: Surry  
Issue date: 10/28/1993
From: Belisle G, Branch M, Tingen S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A455 List:
References
50-280-93-23, 50-281-93-23, NUDOCS 9311160201
Download: ML18152A454 (14)


See also: IR 05000280/1993023

Text

Report Nos.:

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

50-280/93-23 and 50-281/93-23

Licensee:

Virginia Electric and Power Company

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

Sept~mber 5 through October 2, 1993

Inspectors:

Accompanying

Approved by:

Scope:

M. W. Branch, Senior Resident

Inspector

S. G. Tingen, Resldent Inspector

NRC Inspector: L. W. Garner

t:'\\J~-i.l'li,\\-LV-- '\\/ .. ~k-v.-G-

G. A. Belisle, Section Chief

Division of Reactor Projects

SUMMARY

/ 0/ 2 *,_ / 7 3

Date Signed

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Dat~ Signed

i C J_:'~ 1:S

Date Signe

This routine resident inspection was conducted on site in the areas of plant

status, operational safety verification, maintenance inspections, surveillance

inspections, licensee event review, action on previous inspection items, and

meeting with local officials. During the performance of this inspection, the

resident inspectors conducted reviews of the licensee's backshifts, holiday or

weekend operations on September 14 and 23, 1993.

Results:

In the operations area, the following items were noted:

Examples were identified where the tagout program was being used to

isolate equipment abandoned in place which circumvents the design change

process (paragraph 3.a).

9311160201 931028

PDR

ADOCK 05000280

B

PDR

2

In the maintenance area, the following items were noted:

The pre-job brief for removing a screw lodged in a reactor protection

relay was thorough.

Good co11111unication and coordination among

operations, maintenance, and engineering were evident during the

evolution (paragraph 4.a).

Although Kaman radiation monitor spiking has been identified by the

licensee as a recurring problem, corrective actions implemented to date

have not corrected the problem (paragraph 4.c).

Violation 50-280/93-23-0l was identified for activities affecting

quality not being accomplished in accordance with prescribed

instructions, in thijt,

(1) fuses l-EP-FUSE-EH-14H-6 and l-EP-FUSE-EJ-

14H-6 were removed instead of the specified fuses on Tagging Record No.

(S)l-93-EP-0053 and (2) the components' alignment was not properly

independently verified as required by OPAP-0010 step 6.4.6 (paragraph

4.d).

The seven day look ahead schedule did not identify that scheduled

maintenance on the steam driven auxiliary feed water pump conflicted

with, and therefore prohibited, the performance of a scheduled monthly

periodic test of the reactor protection system (paragraph 5.b).

REPORT DETAILS

I.

Persons Contacted

Licensee Employees

  • W. Benthall, Supervisor, Licensing
  • R. Bilyeu, Licensing Engineer

H. Blake, Jr., Superintendent of Nuclear Site Services

R. Blount, Superintendent of Maintenance

D. Christian, Assistant Station Manager

J. Costello, Station Coordinator, Emergency Preparedness

J. Downs, Superintendent of Outage and Planning

D. Erickson, Superintendent of Radiation Protection

A. Friedman, Superintendent of Nuclear Training

  • M. Kansler, Station Manager

C. Luffman, Superintendent, Security

J. McCarthy, Superintendent of Operations

  • A.Meekins, Supervisor of Administrative Services
  • A. Price, Assistant Station Manager
  • R. Saunders, Assistant Vice President, Nuclear Operations
  • E. Smith, Site Quality Assurance Manager
  • T. Sowers, Superintendent of Engineering
  • J. Swientoniewski, Supervisor, Station Nuclear Safety

NRC Personnel

  • M. Branch, Senior Resident Inspector
  • S. Tingen, Resident Inspector
  • Attended Exit Interview

Other licensee employees contacted included control room operators,

shift technical advisors, shift supervisors and other plant personnel.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Plant Status

Unit 1 began the reporting period in power operation and was at power at

the end of the inspection period.

Unit 2 began the reporting period in power operation and was at power at

the end of the inspection period.

The unit operated at 98.5% power for

most of the period in order to minimize level oscillation in the C SG.

3.

Operational Safety Verification (71707, 42700}

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to ~pproved

2

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operational safety and

compliance with TSs and to maintain awareness of overall facility

operations.

Instrumentation and ECCS lineups were periodically reviewed

from control room indication to assess operability.

Frequent plant

tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping.

Deviation reports were reviewed to assure that potential

safety concerns were properly addressed and reported.

a.

b.

c.

Tagout Review

During the inspection period, the inspectors reviewed the -

outstanding Op~rations Department Tagging Record List dated

September 17, 1993.

The inspectors noted several active tagouts

that were three years old or more.

Although most of these long

term tagouts were for non-safety related equipment (boron

recovery, condensate, etc.), several involved safety-related

equipment such as SW and electrical power.

Through the tagout

reviews and discussions with operations personnel, the inspector

determined that the tagout process was being used to isolate

abandoned equipment.

For example, the stated purpose on tagging

records 2-91-EP-0007 dated January 30, 1991, and 2-90-WT-0002

dated July 12, 1990, was to isolate equipment abandoned in place.

This method circumvents the design change process normally used to

facilitate permanent modification and eliminates/removes equipment

that is described in the UFSAR.

Several tagging records indicated

that a OCR had been initiated to permanently modify the plant

configuration. This issue was discussed with plant management.

The licensee acknowledged the inspectors concern and noted that

extended tagouts were not desirable and would be reviewed.

The

licensee also stated that, in accordance with procedures, safety

impact reviews were conducted every 30 day for these existing

tagouts.

Licensee 10 CFR 50.72 Report

On September 28, the licensee made a non-emergency four hour

10 CFR 50.72 report due to an ERFCS failure that rendered the SPDS

unavailable.

The ERFCS failed at 1:10 a.m. and was returned to

service at 5:15 a.m.

The failure was attributed to a failed data

link.

Plant tours

During routine plant tours of the facility on September 28, the

inspectors observed boric acid deposits around pump casing

studs/nuts on two charging pumps.

This was discussed with the

system engineer who showed the inspector that work orders to

correct the conditions had already been initiated.

In fact, one

charging pump was removed from service, as previously scheduled,

3

missing the stem cover plate. The condition was reported to

Operations personnel and a work order was initiated to correct the

condition.

Within the areas inspected, no violations were identified.

4.

Maintenance Inspections (62703) (42700)

During the reporting period, the inspectors reviewed the following

maintenance activities to assure compliance with the appropriate

procedures.

a.

Removal of Loose Screw From Unit 1 RP Relay

While performing a monthly periodic test on September 8, I&C

technicians discovered that a small screw had vibrated loose and

had fallen into relay 1-RP-REL-RT3YA's internals.

On high

pressurizer pressure, low pressurizer pressure, or high

pressurizer level this relay changes state and opens the A reactor

trip breaker. The screw was from a spare contact on the

Westinghouse BFD relay. Relay 1-RP-REL-RT3YA was declared

inoperable and an eight hour LCO to Hot Shutdown was entered in

accordance with TS Table 3.7-1, Item 19 due to the loss of one

channel of automatic trip logic. The technicians also identified

loose screws on spare contacts for seven other relays in the Unit

1 reactor protection racks.

The loose screws were still attached

to the terminals and therefore, these relays were considered

operable.

The inspectors witnessed the screw removal from relay 1-RP-REL-

RT3YA's contacts.

The screw was removed in accordance with

written troubleshooting instructions approved by SNSOC contained

in WO 268360.

Screw removal and relay contact inspections

involved an I&C technician, a system engineer, and an electrician.

The screw was removed with a magnet.

The inspector attended the

pre-job brief and reviewed the post maintenance test requirements.

The brief was thorough and good communication and coordination

between operations, maintenance personnel and engineering was

evident. After the screw was removed, the relay was

satisfactorily tested in accordance with 1-PT-8.1, Reactor

Protection Logic.

On September 10, the loose spare contact screws on the other seven

relays were tightened.

On September 20, the licensee inspected

the Unit 2 Reactor Protection Cabinets and identified one loose

screw.

The loose screw on the Train A relay 81-69AX was

subsequently tightened.

No additional discrepancies were

identified.

  • *

b.

c.

4

Trouble Shooting Charging Pump TCV Inconsistent Stroke Time

On September 17, the inspectors witnessed troubleshooting on Unit

2 C charging pump lube oil SW TCV, 2-SW-TCV-20SC.

The licensee

was obtaining inconsistent stroke times for all six charging pump

SW TCVs.

The purpose of the troubleshooting was to identify the

cause of the TCVs inconsistent stroke times.

The stroke times for

these air operated valves varied from 5 to 74 seconds.

Valve 2-

SW-TCV-208C was the first valve to be investigated for

inconsistent stroke time.

The charging pump TCVs automatically regulate the SW flow though

each charging pump lube oil cooler.

The TCVs modulate open and

closed in order to maintain the lube oil within the desired

temperature range.

The charging pump lube oil temperature

regulates the TCVs' position.

AIRCET test equipment was installed on the valve and the valve was

cycled several times.

The AIRCET test equipment measures valve

stem travel, air operator dome pressure, control air pressure and

supply air pressure. Test results indicated several problems.

The controller's span needed adjustment and the valve was binding

slightly when initially opening.

The span was readjusted and the

valve was cycled satisfactorily. The licensee determined that the

binding did not affect valve operability and a WR was submitted to

investigate the binding at a later date.

No discrepancies were

identified. At the end of the report period, troubleshooting and

repair of the other valves were in progress.

Kaman Radiation Monitor Spikes

TS Table 3.7.6, specified operability requirements for accident

monitoring instrumentation.

Item 12 of this table specified that

the ventilation vent effluent monitor must be operable.

Kaman

vent monitors 1-VG-RI-131-1/2 fulfill this requirement.

Monitor 1-VG-RI-131-1 and 1-VG-RI-131-2 were low and high range

radiation monitors, respectively.

The high range radiation

monitor is normally deenergized and energizes automatically prior

to the low range radiation monitor exceeding its range.

Throughout the inspection period, the low range Kaman monitor was

spiking.

Four DRs were initiated.

On September 16, the radiation

monitor was declared inoperable due to spiking and remained

inoperable for the remainder of the inspection period.

As a

result, the high range monitor was also inoperable.

In accordance

with TS Table 3.7.6, an alternate method to monitor the

ventilation vent effluent was initiated.

The low range Kaman radiation monitor has a history of spiking.

In 1992, nine DRs were initiated due to spikes on the Kaman

radiation monitor.

On four occasions in 1992, the Kaman radiation

monitor was declared inoperable due to spikes.

The licensee's

d.

5

trending programs have identified this as a recurring problem and

corrective actions have been implemented.

During this inspection

period, additional corrective action has been initiated. Although

the Kaman radiation monitor spiking has been identified by the

licensee as a recurring problem, the corrective actions

implemented have not corrected this problem and has forced

reliance on compensatory measures.

Failure To Implement Unit 1 Tag-out Procedure

On September 28, 1993, an on-coming Unit 1 SRO observed that the A

LHSI pump breaker indication was not lit. Investigation revealed

that the breaker t~p/position indication*circuit control fuses

for the pump had been inadvertently removed during a tag-out.

Furthermore, the breaker closing circuit control fuses for the A

ISRS pump had also been removed.

The fuses were immediately

replaced.

The total time the pumps were degraded, i.e., the fuses

were not in the circuits, was less than 30 minutes.

During this

time; the A ISRS pump was unavailable for automatic or remote

starting. The A LHSI pump was available for automatic or remote

starting but the pump could not be shut down remotely.

During the

event, both the redundant ISRS and LHSI train B pumps were fully

functional.

These minimized the event's safety significance.

However, the human performance problems which precipitated the

event were significant.

Through document reviews and interviews with the SRO, the involved

electricians and the HPES investigator, the inspectors constructed

the following event sequence.

At 1:50 p.m. approval was granted

to perform Tagging Record No. (S)l-93-EP-0053.

This tag-out form

directed that fuses l-EP-FUSE-EH-14Hl-6 and l-EP-FUSE-EJ-14Hl-6 be

removed to allow a new breaker to be installed per DCP 90-07-3

(new control room HVAC unit additions). At approximately 3:10

p.m., two electricians were assigned the task to perform the tag-

out and proceeded to the electrical switchgear room.

Both 14Hl

and 14H switchgear were located in this room.

The electricians

opened the panel to breaker cubicle 6 in 14H, located fuses marked

EH and EJ, removed these fuses and attached the red danger tags.

The electricians did not independently verify component alignment

for the fuses listed on the tagging record.

Independent

verification was required by step 6.4.6 of OPAP-0010, Tag-Outs,

dated March 1, 1993.

The tagging record indicated that this task

was completed at 3:15 p.m.

The electricians noted that the

removed 15 amp fuses were a different rating than the 30 and 35

amp rating provided in the component description.

The

electricians returned to the shop and, at approximately 3:30 p.m.,

left the site for the day.

Shortly before 3:30 p.m., the on-

coming SRO performed his pre-shift control board walkdown and

observed no A LHSI pump breaker indication. Attention was

immediately focused on tag-out (S)l-93-EP-0053 as a possible

cause.

This was substantiated, and at 3:30 p.m. authorization was

6

granted to remove the danger tags and re-install the pulled fuses.

At 3:45 p.m., the tagging record was signed verifying the fuses

were properly reinstalled.

Several human performance, deficiencies were identified. Directly

contributing to the event was a failure to properly perform self-

checking, in that, the electricians went to switchgear 14H whereas

14Hl was the specified switchgear. A secondary casual factor was

a time restraint perception by the two electricians. The

electricians had surmised from operations that this tagout was

needed invnediately. This perception arose from the operations

person's vocal tone, .a task assignment near the end of the shift,

and the need to provide the completed paperwork to Operations

before the one~hour shift turnover "quiet time" that began at 3:30

p.m.

This time restraint apparently resulted in the task being

performed in a rapid manner with minimal preparation.

No pre-job

walkdown was performed, a cabinet drawing was not obtained to help

locate the fuses inside the switchgear, and the fuse size

discrepancy was not adequately pursued.

10 CFR 50 Appendix B Criterion V requires that activities

affecting quality be prescribed by documented instructions,

procedures, or drawings, of a type appropriate to the

circumstances and be accomplished in accordance with these

instructions, procedures, or drawings.

Failure to remove the

fuses specified on the tagging record and perform independent

alignment verification is a violation of Criterion V.

This is

identified as VIO: Fuse removal not accomplished in accordance

tagging record and OPAP~OOlO, 50-280/93-23-01.

Although the events associated with this violation were self-

disclosing, the violation was cited because the following similar

occurrences of electricians not following instructions were

identified in IRs in the past year:

NCV 50-280/92-22-02, Maintenance Personnel Failed To

Independently Verify Danger Tags.

NCV 50-281/93-11-01, Maintenance Personnel Lifted Incorrect

Lead Rendered RHR Inoperable.

NCV 50-281/93-11-02, Failure to Follow Maintenance

Procedure.

As discussed above, the tagging record identified the fuses to be

removed as 30 and 35 amps.

This information was obtained from

drawing 11448-FE-9BS revision 3, dated July 29, 1993.

However,

the Power Fuse Schedule, l-DRP-015, revision 0, dated April 16,

1992, identified the fuses as spares and as 15 amps.

Drawing

11448-FE-9BS revision 2, dated September 8, 1989 was subsequently

reviewed.

This previous revision, in effect at the time the Power

7

Fuse Schedule was developed, also showed the fuses as 30 and 35

amps.

At the end of the report period, the licensee was

investigating the cause for this discrepancy.

Within the areas inspected, one violation was identified.

5.

Surveillance Inspections (61726, 42700}

During the reporting period, the inspectors reviewed surveillance

activities to assure compliance with the appropriate procedure and TS

requirements.

a.

l-SI-MOV-18628 Stroke Test

During the previous inspection period, the inspectors identified a

concern with valve l-SI-MOV-1862B's operation.

The valve had a WR

tag attached that stated that the MOV would not automatically

return to the electrical mode of operation after the handwheel was

manually declutched.

The inspectors were concerned that-if l-SI-

MOV-18628 declutch lever was inadvertently moved, the MOV would

become disengaged from the motor and not operate electrically when

required.

During this inspection period, the inspectors witnessed

stroke testing of the valve in accordance with l-OPT-SI-003,

Quarterly Test of SI MOVs and RWST XTie TVs, dated May 27, 1993.

The evolution was thoroughly briefed prior to its performance.

The valve was initially stroked electrically to verify that it was

operable in the as-found condition.

The MOV was then manually

clutched and operated.

During this evolution, the inspectors

noted that in order to clutch and engage the manual operator the

clutch lever and handwheel had to be operated simultaneously.

The

inspectors concluded that it was not probable to inadvertently

disengage the motor from the operator because the clutch lever and

handwheel had to be operated simultaneously. Afterwards, the

valve was cycled electrically in accordance with l-OPT-SI-003 to

demonstrate that it was left in an operable condition.

The inspectors reviewed the results of l-OPT-SI-003 performed on

September 17.

No discrepancies were identified.

b.

2-PT-8.1

On September 22, the inspectors attended the pre-job brief for

monthly periodic test 2-PT-8.1, Reactor Protection Logic.

During

the pre-job brief, the SRO identified that the test, scheduled for

September 22, could not be performed because the conditions

specified in procedure step 4.10 could not be met at the present

time.

Step 4.10 cautioned that during part of the test, the

control switch for the motor driven AFW pump in the train being

tested must be placed in the pull-to-lock position to prevent the

pump from automatically starting.

On that same day, the steam

..

" *

a

driven AFW pump was tagged out and was inoperable for planned

maintenance. Since TSs prohibit more than one AFW pump in a unit

to be inoperable, 2-PT-8.1 had to be rescheduled.

The seven day

look ahead schedule process was established to preclude these

types of conflicts. The inspectors discussed with management the

seven day look ahead schedule process' failure to identify that

maintenance on the steam driven AFW pump prohibited performing

2-PT-8.1.

Within the areas inspected, no violations were identified.

6.

Licensee Event Review (92700)

The inspectors reviewed the LERs listed below and evaluated the

corrective action's *adequacy and implementation.

a.

b.

(Closed) LER 281-92-06, Auxiliary Ventilation Exhaust Filter

System Train Rendered Inoperable When Fan Tripped Due to Filters

Being Near The End of Their Service Life. This issue involved

both auxiliary ventilation exhaust fans being inoperable which

required entry into a six hour LCO to Hot Shutdown in accordance

with TS 3.0.I. While the A exhaust fan was inoperable due to

planned maintenance, the B fan was operating and tripped on

excessive vacuum.

The excessive vacuum that caused the B fan to

trip was attributed to dirty auxiliary ventilation exhaust

filters.

As corrective action to prevent recurrence, procedures

were to be revised to replace auxiliary ventilation exhaust

filters at a lower differential pressure value.

The inspectors

reviewed quarterly surveillance procedure O-OPT-VS-002, Auxiliary

Ventilation Filter Train Test, dated September 24, 1993, and the

auxiliary building operator logs and verified that these documents

placed reduced differential pressure limits on the auxiliary

ventilation exhaust filters.

(Closed) LER 280-91-03, Station Record Storage Vault Halon System

Inoperable. This issue was reported when the licensee's QA review

identified that several previous surveillance test had been

determined acceptable even though the Halon system bottle pressure

was outside its limits. The licensee's report indicated that the

bottle pressure was corrected and that confusion in the procedure

may have led to the personnel error. The licensee revised

procedures to prevent recurrence.

The inspectors reviewed this issue and determined that the actions

described above were completed.

However, the procedure and

equipment described in the LER was subsequently deleted in 1992

when the licensee moved the station records vault to the new

administrative building.

The new records vault fire suppression

system is a dry standpipe water system that is actuated by a

,.

9

combination of smoke and heat. Since the new facility fire

suppression system represented a change in design, the inspectors

verified that the licensee's QA topical report co11111itments for

fire protection of QA records were satisfied.

Within the areas inspected, no violations were identified.

7.

Action on Previous Inspection Items (92701,92702)

a.

(Closed) VIO 50-280/92-07-02, Failure to Establish Containment

Integrity in Accordance with TS 3.10.A.l. While moving fuel

during the Unit 1 spring 1992 RFO, the licensee failed to maintain

containment integrity as required by TSs.

The failure occurred

because SG and MS maintenance activities were not properly

controlled.

The licensee-responded* to this vicilation in a letter

dated May 29, 1992.

In the letter, the licensee stated that the

following corrective actions would be implemented:

Revise procedures to provide more detailed and specific

requirements for establishing refueling integrity.

Plan for refueling integ~ity windows during outages. During

periods when refueling integrity is required, modifications

to containment boundary will be administratively restricted.

Notify operations when restarting work on an extended job to

ensure work is not performed on a component which has become

part of the refueling integrity boundary.

Place precautions on work orders when working refueling

integrity boundary components.

The inspectors reviewed 2-0PT-CT-210, Refueling Containment

Integrity, revision 3, and verified that the procedure was

enhanced to provide more detailed and specific requirements for

establishing refueling integrity. During the previous Unit 2 RFO,

the inspectors periodically monitored containment integrity during

refueling operations. The inspectors noted that maintenance

effecting containment integrity was properly controlled during

periods when refueling integrity was required.

The inspectors

also selected approximately ten containment isolation valves to

verify that the model work orders for the valves contained special

instructions identifying the valves as containment integrity

components.

The inspectors noted that the licensee was in the

process of initiating a new program, PASSPORT, for planning WOs.

This program currently does not identify components which may be

used to establish containment integrity. During the inspection

10

period, the licensee was in the process of evaluating methods to

inform maintenance personnel that they were working on a

containment integrity component.

The previous program for

planning WOs, WPTS, did identify which valves were required to

establish containment integrity.

Within the areas inspected, no violations were identified.

8.

Meeting With Local Officials

On September 14, 1993, the NRC and Virginia Power met to discuss the

SALP Report for the Surry Facility. Local officials and the media were

invited to this meeting and were also invited to meet with the NRC

afterwards.

The following local officials and members of the media met

with the NRC on September 14 at the Surry Facility:

G. Urquhart, Conunonwealth of VA, Department of Emergency Services

M. Weaver, Reporter (Virginian Pilot}

B. Marriott, Director of Newport News Emergency Services

R. Lowry, Jr., James City County Emergency Service Coordinator

B. Geddy, Williamsburg Emergency Service Coordinator

T. Lewis, Surry County Administrator

During this meeting, the local officials stated that cooperation between

the local governments, Virginia Power and NRC was good.

G. Urquhart

discussed the local governments' recent emergency response to impending

Hurricane Emily and requested local officials to document what emergency

actions were taken.

The state plans to evaluated whether the emergency

actions taken for the impending hurricane could be substituted for the

states participation in the Surry annual emergency exercise scheduled

for December 8, 1993.

The NRC officials informed the participants that

timely letters to FEMA and the NRC would be necessary to receive credit

for hurricane response and partial or full relief from participation

during the annual exercise.

Within the areas inspected, no violations were identified.

9.

Exit Interview

The results were sununarized on October 6, 1993, with those individuals

identified by an asterisk in Paragraph 1.

The following summary of

inspection activity was discussed by the inspectors during this exit:

Item Number

Status

VIO 50-280/93-23-01

Open

Description

(Paragraph No.}

Fuse removal not accomplished

in accordance tagging record

and OPAP-0010 (paragraph 4.d) .

LER 281-92-06

11

Closed

Auxiliary Ventilation Exhaust

Filter System Train Rendered

Inoperable When Fan Tripped

Due to Filters Being Near The

End of Their Service Life

(paragraph 6.a).

LER 280-91-03

Closed

Station Record Storage Vault

Halon System Inoperable

(paragraph 6.b).

VIO 50-280/92-07-02

Closed

Failure to Establish

Containment Integrity in

Accordance with TS 3.10.A.l

(paragraph -7.a).

Proprietary information is not contained in this report. Dissenting

comments were not received from the licensee.

10.

Index of Acronyms and Initialisms

AFW

DCP

OCR

DR

ECCS -

ERFCS -

FEMA -

HPES -

HVAC

-

I&C

IR

ISRS -

LCO

LER

LHSI -

MOV

MS

NCV

NRC

QA

RFO

RHR

RP

RWST -

SALP -

SRO

SG

SI

SNSOC -

SPDS -

AUXILIARY FEEDWATER

DESIGN CHANGE PACKAGE

DESIGN CHANGE REQUEST

DEVIATION REPORT

EMERGENCY CORE COOLING SYSTEM

EMERGENCY RESPONSE FACILITY COMPUTER SYSTEM

FEDERAL EMERGENCY MANAGEMENT AGENCY

HUMAN PERFORMANCE EVALUATION SYSTEM

HEATING VENTILATION AND AIR CONDITIONING

INSTRUMENTATION AND CALIBRATION

INSPECTION REPORT

INSIDE RECIRCULATION SPRAY SYSTEM

LIMITING CONDITION OF OPERATION

LICENSEE EVENT REPORT

LOW HEAD SAFETY INJECTION

MOTOR OPERATED VALVE

MAIN STEAM

NON-CITED VIOLATION

NUCLEAR REGULATORY COMMISSION

QUALITY ASSURANCE

REFUELING OUTAGE

RESIDUAL HEAT REMOVAL

REACTOR PROTECTION

REFUELING WATER STORAGE TANK

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

SENIOR REACTOR OPERATOR

STEAM GENERATOR

SAFETY INJECTION

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SAFETY PARAMETER DISPLAY SYSTEM

SW

TCV

TS

TV

UFSAR -

VIO

WO

WPTS -

WR 12

SERVICE WATER

TEMPERATURE CONTROL VALVE

TECHNICAL SPECIFICATION

TRIP VALVE

UPDATED FINAL SAFETY ANALYSIS REPORT

VIOLATION

WORK ORDER

WORK PLANNING AND TRACKING SYSTEM

WORK REQUEST