ML18152A325

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Insp Repts 50-280/92-13 & 50-281/92-13 on 920510-0606. Violations Noted.Major Areas Inspected:Operations,Maint, Surveillance,Lers,Action on Previous Insp Items & Safety Assessment
ML18152A325
Person / Time
Site: Surry  Dominion icon.png
Issue date: 07/01/1992
From: Branch M, Fredrickson P, Tingen S, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A326 List:
References
50-280-92-13, 50-281-92-13, NUDOCS 9207140044
Download: ML18152A325 (15)


See also: IR 05000280/1992013

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION 11

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report-Nos.:

50-280/92-13 and 50-281)92-13

Licensee~

Virginia Electric and Power Company

- 5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

May 10 through June 6, 1992

Inspectors: ~

~

M. --arn,entorResident Inspector

a~ 2h:::

J. W. York,~t Inspector

a~~

S. G. Tinge~nt Inspector

Approved by: *

M V 5 .J,uk-

P. E. Fredricson, Section Chief

Division of Reactor Projects

SUMMARY

Scope:

D~~

  • ~<--

Daeigned

~-d,

D!te1gne

. 7(, [1~

Date Signed

This routine resident inspection was conducted on site in the areas of

operations, maintenance, surveillance, licensee event review, action on

previous inspection items, and safety assessment and quality verification.

During the performance of this inspection, the resident inspectors conducted

review of the licensee's backshift or weekend operations on May 22, 28, and

June 3, 1992.

Results:

In the maintenance/surveillance area, the following items were noted:

Management oversight and controls associated with replacement of

the No. 1 emergency diesel generator governor reflected the

implementation of improvements as a result of corrective action

for previous weaknesses in this area {paragraph 4.a).

9207140044 920701

PDR

ADOCK 05000280

G

PDR

2

The emergency diesel generator procedure for adjusting scribe'~

marks appeared to need strengthening to eliminate confusion

{paragraph 5.a).

In the safety assessme~t/quality*verification area, the following items were

noted:

The failure to perform safety evaluations for procedures that were

used to operate plant systems differently than that described in

the Updated Final Safety Analysis Report was identified ~s

Violation 280,281/92-13-0l {paragraph 7).

The Management Safety Review Co1R11ittee meeting was thorough and

the discussion of issues were detailed to make

decisions/recommendations {paragraph 8).

1.

Persons Contacted

Licensee Employees

REPORT DETAILS

R. Allen, Superintendent of Operations (Acting}

  • W. Benthall, Supervisor, Licensing

R. Bilyeu, Licensing Engineer

  • H. BJake, Superintendent of Site Services
  • R .. Blount, Superintendent of Engineering
  • D. Christian, Assistant Station Manager
  • J Demease, Nuclear Oversight Board

J. Downs, Superintendent of Outage and Planning

  • R. Gwaltney; Superintendent of Maintenance
  • W. Hartley, Nuclear Oversight Board
  • M. Holdsworth, Supervisor, Security

M. Kansler, Station Manager

.

  • A. Keagy, Superintendent of Materials
  • J. McCarthy, Assistant Station Manager (Acting}
  • A. Meekins, Supervisor, Administrative Services
  • D. Modlin, Supervisor, Shift Operations (Acting}
  • J. O'Hanlon, Vice President-Nuclear, Corporate
  • E. Smith, Site Quality Assurance Manager
  • R. Wells, Supervisor, Maintenante

NRC Personnel

M. Branch, Senior Resident Inspector

  • S. Tingen, Resident Inspector
  • J. York, Resident Inspector
  • Attended exit interview.

Other licensee employees contacted included control room operators,

shift technical advisors, shift supervisors and other plant person~el.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Pl ant Status

Unit 1 began the reporting period in power operation.

The unit was at

power at the end of the inspection period, day 31 of continuous

operation.

Unit 2 began the reporting period in power ope rat i o'n. * The unit was at

power at the end of the inspection period, day 171 of continuous

operation.

3.

- - - - - - -

2

Operational Safety Verification (!1707,42700)

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to approved

.

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operations safety and

compliance with TSs and to maintain awareness of the overall operation

of the facility.

Instrumentation and ECCS lineups were periodically

reviewed from control room indication to assess operability. Frequent

plant tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping. Deviation reports were reviewed to assure that potential

. safety concerns were properly addressed and reported.

a.

Licensee 10 CFR 72 Reports

On May 11, the licensee made a 10 CFR 50.72 report concerning

operation of Unit 1 since the startup on May 1, 1992, in non-

compliance with the requirements of TS 3.3.B.2 (Safety Injection

System) for alignment of the CH/HHSI pumps.

The control switches

for the CH/HHSI pumps were aligned such that the A CH/HHSI pump

would trip on an undervoltage condition. This CH/HHSI pump

configuration was identical to the condition that resulted in

escalated enforcement action in September, 1991. This event is

covered in detail in IR 280,281/92-12.

b.

Troubleshooting Motor Driven Fire Pump

While securing the motor driven fire pump on June 3, the breaker

for the pump cycled twice and tripped.

The diesel driven fire

pump then automatically started but was secured when the operator

observed air coming out of a vent on the pump's casing. Deviation

report No. S-92-0977 was written and work request No. 800386 was

issued.

The licensee declared both fire pu,mps inoperable and initiated a

one hour clock to establish a continuous fire watch with backup

suppression equipment for Unit 1 and 2 cable vault and tunnels as

required by TS 3.21.B.3. A 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> LCO was initiated to establish

a backup firi suppression wJter system in accordance with TS 3.21.8.2.b. The plant fire truck was designated as the backup

fire suppression water system and it was verified as operable.

The inspectors observed operation personnel coordinating with the

~ystem engineer in the filling and venting of the system and

evaluating the problem.

It was concluded that a check valve

between a hydropneumatic tank and both fire pumps caused the

problem.

The failure of this check valve allowed the pressure to

be lowered in the tank and the air to migrate to the two pumps

causing cavitation. After filling and venting, the pressure was

returned to normal in the hydropneumatic tank.

The check valve

3

appears to be performing normally and an annunciator in the

control room would indicate any return of this problem.

Within the areas inspected, no violations were identified.

4.

Maintenance Inspections (627Q3, 42700,)

During the reporting period, the inspectors reviewed maintenance

activities-to assure compliance with the appropriate procedures.

The following maintenance activities were reviewed.

a.

No. 1 EDG Governor Replacement

On May 19, the No. 1 EDG-did not start during a post maintenance

test and the problem was later attributed to a failed governor.

The EDG was operated on the previous shift; therefore, the EDG

governor failure was quickly identified. The inspectors observed

portions of the maintenance to replace the No. 1 EDG governor;

Procedure O-MCM-0705-01, Emergency Diesel Injector Rack, Governor

Compensation, and Speed Limit Switch Adjustments, dated February

13, 1992, and WO 3800127359 were used to accomplish this

maintenance.

The governor was removed and replaced with a spare

governor.

Prior to installing the new governor it was sent to a local test

facility.

The governor was adjusted and tested. The test

facility was not on the licensee's QA approved vendor list. The

inspectors reviewed ENAP-0004, Procurement Technical Evaluation,

dated May 4, 1992 which allows the use af non-qualified vendors

provided'Virginia Power's QA program is extended to cover the

vendor.

During the test, the licensee's QA program was extended

to cover the vendor with the presence of a corporate QA i~spector

who monitored the test activities~

In addition, an SNSOC approved

procedure was used for adjustments and testing of the governor.

This procedure was incorporated into procedure O-MCM-0705-01.

The inspectors reviewed the PMT requirements for this maintenance

and did not identify any discrepancies.

An EDG fast speed start

was required.

The inspectors also reviewed O-MCM-0705-01 and did

not identify any deficiencies. The inspectors concluded that

management oversight and control functions related to the governor

replacement were successful in satisfactorily accomplishing this*

maintenance.

For example, a formal maintenance procedure was

utilized that specifically addressed governor replacement, correct

PMT requirements *were specified, procedures were followed, and

communications between operation, maintenance, and engineering

were good.

b.

4

Mechanical Equipment Bolting

During the walkdowns of plant areas, the inspectors noted a

questionable condition regarding the mounting of sev~ral safety-

related and nonsafety-related pumps, motors, and engines.

Specifically, the jacking bolts which are normally used only to

align the foundation bolts prior to tightening were found to be.

contacting the foundation of the equipment and had not been backed

off. This condition could mask equipment vibration problems and

did not appear to be addressed by the licensee maintenance

procedures.

The inspectors discussed this condition with the Maintenance

Manager and a walkdown by the licensee indicated that

approximately 30 percent of .the equipment inspected had the same

condition (i.e. jacking bolt tight against the equipment

foundation).

The li~ensee indicated that, although the procedures

do not detail the need to loosen the jacking bolts after equipment

alignment, discussion with mechanics involved with equipment

mounting revealed that they were aware of the need to loosen the

jacking bolts after alignment.

The inspectors did not identify any cases where excessive

equipment vibration was being dampened by the use of the jacking

bolts.

However, the lic.ensee was reluctant to just loosen the

jacking bolts with out measuring the resultant equipment

vibration.

The licensee agreed to verify proper equipment

vibration with t~e jacking bolts loosened during the scheduled

predictive maintenance vibration measurement.

The licensee

proposed resolution of the inspectors concern in this area appears

to be acceptable when combined with the evaluation of possible

procedure enhancements as well.

Within the area inspected, no .violations were identified.

5.

Surveillance Inspections (61726, 42700) *

During the reporting period, the inspectors reviewed surveillance

activities to assure compliance with the appropriate procedure and TS

requirements.

The following surveillance activity was reviewed:

a.

No. l EDG Post Maintenance Testing

On May 20, the inspectors witnessed the testirig of the No. l EDG

following the replacement of the governor.

The testing was

accomplished in accordance with l-OPT-EG-004, *Number l Emergency

Diesel Generator Quarterly Fast Start Exercise Test, dated April

16, 1992. The inspectors attended the pre-job briefing, witnessed

portions of the test, and reviewed the completed test procedure .

The EDG was initially started in slow speed in accordance with

5

step. 5. 2 .17 of operating procedure 1-0P-EG-001, Number 1 Emergency

Diesel Generator, dated April 16, 1992.

The engine increased in

speed and stabilized at approximately 420 rpm versus the desired

470 to 490 rpm value stated in the procedure. A slow speed

adjustment was made in accordance with the procedure.

The inspectors' review of the above operating procedure identified

an area that needed strengthening by the licensee. Specifically,

step 5.3 of 1-0P-EG-001 which was used to shutdown the EOG from

the main control room contained confusing instructions associated

with verification of governor speed control scribe marks after

engine shutdown.

The governor speed control knob and gears had

  • been scribed with a distinct marking on all three EDG following

the August 1991 EOG failure as part of the corrective actions.

Procedures were developed to require verification that *these

scribe marks were in alignment locally to ensure that the EDG

would achieve rated speed during emergency starting. The

confusing instructions were contained in steps 5.3.11 and its

preceding note and 5.3.12. Step 5.3.11 requir~d that the

alignment of scribe marks on the gears and the speed control knob

be verified. However, the preceding note stated that, if the

scribe marks are found not aligned during the verification, no

alignment should be attempted. Step 5.3.12 states that if the

scribe marks are not in alignment then notify the shift

supervisor.

It was not clear as to whether alignment of the

scribe marks were an option or whether the operator was not to

make the adjustments and the shift supervisor would recognize the

need to have maintenance adjust the scribe marks.

The potential

for leaving an EOG in an unknown inoperable condition was further

complicated in that there was no other mention of verifying the

scribe marks prior to declaring the EOG fully operable per the

note after step 5.3.19 of the procedure.

The inspectors discussed the above concerns with station

management who indicated that a procedure revision would be

considered to resolve the confusion.

Within the areas inspected, no violations were identified.

6.

Licensee Event Review (92700)

The inspectors reviewed the LERs listed below and evaluated the adequacy

of corrective action.

The inspector's review also included followup on

the licensee's implementation of corrective action.

a.

(Closed) LER 280,281/90-20, Startup and Power Operation With One

Train of Containment Spray System Inoperable Due to Improper

Deletion of Pressure Switch Repair From Outage Work Scope.

This

issue involved the failure of limit switches 1-CS-PS-103A and 1-

CS-PS-103C.

This issue and immediate corrective actions were

previously discussed in IR 280,281/91-06.

long term corrective

actions involved performing a CFE on the failed limit switches,

b.

6

performing an engineering study to evaluate the removal of th~~.

switches, performing a root cause evaluation, review of test

records to determine if other systems may have the same type of

switches, upgrade l&C PM program, and.stre~gthen the ~tartup

assessment process. A CFE has not been performed for th- failed

limit switches; however, this item is being tracked by CTS No.

1212 until completion.

The MOVs that automatically operated in

response to actuation of these limits switches were failed opened,

control power was removed, and stem locking devices were installed

as described in IR 280,281/91-06.

The inspectors walked .down the

system and verified the installation of stem locking devic.es and

that the control room indication for the MOVs were deenergized.

The root cause evaluation ~as performed and is discussed in IR

280,281/91-06.

The startup assessment process was enhanced by

requiring corrective actions, in response to station deviations

which are initiated during a RFO, be tracked and have SNSOC

concurrence if corrective measures were not implemented before

startup of the unit.

In addition, a representative from the

Outage & Planning Department is required to attend SNSOC meeting

during review of station deviations to ensure that outage related

station deviations are scheduled to be worked during the outage.

The l&C PM program was enhanced by incorporating it into the

station PM.program which requires written approval to defer a PM.

In addition, deferred PMs are tracked monthly by the PM

coordinator and are reviewed by the MRB during restart

assessments.

The inspectors consider that the corrective actions

were properly implemented or were being properly tracked.

(Closed) LER 280,281/91-17, Diesel Generator Rendered Inoperable

Due to Personnel Error in Adjusting the Governor.

This issue

involved the No. 3 EDG being inoperable for a period of time*

greater that allowed by TSs due to an improperly adjusted governor

speed control dial. Violation 280,281/91-24-01, Failure to Comply

With the Requirements of TS. 3.16.B.1 with the No. 3 EDG

Inoperable, was issued as a result of this event.

The corrective

actions for this LER and the violation are the same and are

discussed below ..

Within the areas inspected, no violations were identified.

7.

Action On Previous Inspection Items (92701,92702)

a.

(Closed) Violation 280,281/90-36-0l, Low SW Flow Th~ough the

RSHXs.

This issue involved inoperable RSHXs in both units due to

reduced SW flow rates. The reduced SW flow rates were caused by

macrofouling of the RSHXs.

Short term corrective actions

involving inspection, cleaning, testing, alternating SW BC supply

headers, and placement of RSHXs SW supply headers in partial wet-

layup were discussed in IR 280,281/90-36.

The licensee responded

to this violation in a letter dated March 14, 1991.

In that

letter, the licensee stated that the following long term

corrective actions would be implemented: (1) chemically treat the

~*

b.

7

48 inch SW headers to the RSHXS in order to control hydroid

growth; (2) monitor 48 inch SW supply headers for temperature,

salinity, PH, conductivity, dissolved oxygen, chlorine and anvnonia

and correlate results with visual inspections; (3) perform flow

testing and post test inspection on a RS SW subsystem and perform

as~found inspection on the remaining RS SW subsystem during the

1991 Unit 2 RFO and 1992 Unit 1 RFO; (4) initiate an ecosystem

study to support a long-term biological control strategy; and

(5) clean, inspect, repair and epoxy coat RSHX supply piping.

The inspectors walked down the SW system and verified installation

of equipment utilized to chemically treat the 48 inch SW headers

to the RSHXs.

Additonally, the inspectors reviewed procedures -

l,2-0P~49.1, Startup and Shutdown of the SW System and Chemical

Injection of Headers, dated August 22, 1991, 1,2-0P-49.7, Draining

RSHX SW Piping in Wet Lay-UP, dated May 31, 1991, and l,2-0SP-SW-

001, Maintenance and Sampling of RSHX SW .Piping in Wet Lay-up,

dated April 23, 1992. These procedures are utilized to add

chemicals, fill, and sample the system.

The inspectors also

reviewed the the monthly PT schedule and verified that the SW BC

headers are alternated on a weekly basis. During the.Unit 1 1992

RFO, the inspectors inspected internal portions of the 48 inch SW

piping and considered the program effective in minimizing hydroid

growth.

During the previous Unit~ 1 and 2 RFOs, the inspectors

monitored flow testing of the RSHXs and inspected the RSHXs

following the tests. Results of these inspections also indicated

that corrective actions have been effective.

IRs 280,281/91-10

and 92-07 discussed these inspections. The Virginia Institute of

Marine Science monitors hydroid growth and makes recommendations

to the licensee for long term control. This item is being tracked

by CTS No. 220 until completion. Approximately 80% of the Unit 1

and 50% of the Unit 2 RSHX SW supply piping has been coated with

epoxy.

Completion of epoxy coating is scheduled during the

upcoming RFOs and is being tracked by CTS No. 1180.

At the end of

the inspection period, the licensee was evaluating the need to

routinely flow test the SW piping to the RSHXs.

The inspectors

consider that the corrective actions were properly implemented.

{Closed) UNR 280,281/91-33-01, Safety Evaluations for Changes in

the Facility. This issue involved three examples in which the

licensee had operated plant systems in a different manner *than

-described in the UFSAR but had not first prepared written safety

evaluations pursuant to lOCFR 50.59.

Based on guidance from Part

9900 of the NRC Inspection Manual and NSAC-125, the inspectors

concluded that a safety evaluation should have been done for each

example.

The licensee disagreed. Because of this disagreement,

the NRC further reviewed this issue and concluded that the

licensee should have recognized these configurations as changes to

procedures described.in the FSAR and therefore, should have

performed safety evaluations to justify these changes.

The basis

for this conclusion is that the UFSAR's description of the

operation of a plant system, including its alignment or

,

8

configuration, constitutes a procedure as described in 10 CFR

50.59~ Thus, proposed procedures for operating a plant system in

a different manner than described in the UFSAR should be evaluated

pursuant to 10 CFR 50.59.

10 CFR 50.59(b)(l) requires records of

changes in procedures as described in the safety analysis report

to include written safety evaluations which provide the basis for

the determination that the procedure changes do not involve

unreviewed safety questions.

The failure to perform safety

evaluations for the procedures that were used to operate plant

systems differently than that described in the UFSAR was

identified as Violation 280,281/92-13-01.

Examples of procedures

that operated plant systems differently than described in the

UFSAR were OP 52.2.1, Administrative Control of 1-FP-36, dated

October 27, 1989, 2-0P-49.7, Filling and Draining RSHX Service

Water Supply Piping, dated September 18, 1991, and OP 6.2.3, *

Administrative Control of 1-EG-15, 2-EG-15 or 3-EG-15, dated

January 20, 1990.

-

c.

(Closed) IFI 2ao,281/90-30-0l, Followup on Licensee Corrective

Action and Testing Deficiencies Identified During RSHX SW Flow

Testing. This issue involved reduced RSHX SW flow rates and

incorrect indication of control room RSHX SW flow identified

during testing accomplished in Unit 1 during the 1990 RFO.

Violation 280,281/90-36-01 was issued as a result of reduced SW

flow rates which was discussed in the previous paragraph. During

the Unit 1 1992 RFO, new RSHX SW flow instrumentation was

installed in Unit 1 and satisfactorily tested. Testing of the new

flow instrumentation was discussed in IR 280,281/92-07.

Installation of new RSHX SW flow instrumentation in Unit 2 is

scheduled for the 1993 RFO.

d.

(Closed) VIO 280,281/91-24-01, Failure to comply with the

. requirements of TS 3.16.B.1 with the No. 3 EOG inoperable. This

issue involved the No. 3 EOG being inoperable for a period of time

greater that allowed by TSs due to an improperly adjusted governor

speed control dial. Immediate corrective actions required to

restore the EOG to an operable status are discussed in IR

280,281/91-24.

The licensee responded to this violation in

letters dated November 20, and December 20, 1991.

In these

responses, the licensee stated that the following long term

corrective actions would be implemented: (1) scribe the governor

gearing and speed knobs at the 900 rpm setting and install a see-

through cover plate on each governor limit switch enclosure so the

the scribed match marks may be observed without cover removal

(2) revise operator logs to verify that match marks are properly

aligned on each shift, (3) revise PMT requirements to specify that

fast start testing requirements following any governor

maintenance, upgrade procedures for governor maintenance and fast

start operation, (4) train select station personnel with vendor

participation on EOG governors in order to increase overall

knowledge level, (5) establish special task teams to review root

causes and review EOG governor and control circuits to ensure

9

reliable operation, and (6} perform a QA assessment on

implementation of the PMT program.

The inspectors walked down all three EDGs and verified that the

governors' gears were matched, marked, and aligned. The

inspectors also verified the installation of see-through cover.

plates on the EDG governors and that plant logs were revised to

require verifiation of the governor match marks.

Procedure No.

IA, Plant Log Readings, dated May 28, 1992, was reviewed to verify

that governor match marks were checked for alignment on each

shift. Review of EDG upgraded procedures and PMT requirements are

discussed in paragraphs 4.a and 5.a and were considered adequate.

The licensee has not completed the governor training but this item

was being tracked by CTS item 1473.

Present licensee plans are to

train station personnel in September 1992.

The inspectors

reviewed CFA*Report 91-1991, dated December 27, 1991, on EOG

governors, and verified that the EOG failure was analyzed and that

EDG governor enhancements were investigated. The inspectors

reviewed the PMT followup assessment, dated Hay 27, 1992. This*

assessment concluded, in general, that the specified PMT assured

equipment was operable before return to service.

The inspectors

consider that the corrective actions in response to the violation

were properly implemented or were being properly tracked ..

e.

(Closed} VIO 280/90-39-01, Failure to Follow Precaution 4.19 While.

Performing Continuity Checks During the Performance of Procedure

l-OPT-ZZ-001. This issue involved the inadvertent automatic start

of the Nos. I and 3 EDGs caused by an electrician improperly

performing a continuity check.

The licensee responded to this in

a letter dated February 25, 1991.

In the letter, the licensee

stated that the following corrective actions would be implemented;

strengthen standards for conducting prejob briefings, include this

. example in training lesson plans for electricians, and revise ESF

test procedures to include precautionary statement alerting

workers to the possibility of voltage being present during

continuity checks of electrical circuits. The licensee formed a

team to develop standards for conducting prejob briefings. Once

these standards were developed, the team issued them via a station

letter to the different departments.

Each department reviewed

these standards and incorporated them into the applicable

department procedures.

The operations department incorporated the

new prejob brief criteria in Revision 2 to VPAP-1401, Conduct of

Operation.

The inspectors reviewed this document and verified

that these instructions were added. The engineering department

incorporated the new prejob brief criteria into Revision 3 of

SUADM-ENG-09, T~st Control, and Revision I of SUADM-ENG-11,

Special Tests. The inspectors reviewed these documents and

verified that instructions were added. The inspectors reviewed

procedures l-OPT-ZZ-001, ESF Actuation With Undervoltage and

Degraded Voltage IH-Bus, dated February 27, 1992 and 2-0PT-ZZ-002,

ESF Actuation With Delayed Undervoltage 2J-Bus, dated August 29,

1991, and ~erified that these procedures were revised to provided

f.

g.

10

a precautionary statement was added to alert workers of the

possibility of voltage being present during continuity checks.

The tnspectors reviewed Revision 2 to the lesson plan titled,

Event Training Using Test Equipment, and verified that it covered

this event; The inspectors consider that the corrective actions

in response to the violation were properly implemented.

{Closed) VIO 280/90-39-02, Failure to Provide Adequate

Instructions for Testing, Resulting in the Unintentional Actuation

of B Train CLS HI {SI). This issue involved inadequate

instructions in an ESF procedure for removal of a test jumper

which resulted in the inadvertent initiation of B train CLS HI

{SI).

The licensee responded to this in a letter dated February

25, 1991.

In the letter the licensee stated that the following

corrective actions would be implemented; revise the ESF procedure

to specify the correct jumper and strengthen administrative

controls governing procedure development by requiring an

additional technical review for complex pro~edures that have the

potential to cause inadvertent ESF actuations. The inspectors

reviewed procedure l-OPT-ZZ-001 and verified that it was revised

to provide adequate instructions for removal of the test jumper.

Station Procedure Directive 001, dated February 13, 1991, which

was revised, instructed procedure writers of the additional

technical review.

The inspectors consider that the corrective

actions in response to the violation were properly implemented.

(Closed) VIO 280/90-39-03, Inadequate Field Change Resulting in

Unreliable Reactor Vessel Level Indication. This issue involved a

field change to a DCP that modified the reactor head vent piping.

The field change was inadequate because it did not recognize that

the standpipe had been turned over to operations for unrestricted

use.

As a result, the reactor vessel standpipe indication was

unreliable while the modification to the reactor head vent piping

was being performed.

The licensee responded to this violation in

a letter dated February 25, 1991.

In the"letter the licensee

stated that the following corrective actions would be implemented;

issue a lessons learned memorandum to Design, System and Testing

Engineering personnel discussing this issue; issue a memor~ndum to

operations personnel emphasizing that a step may be marked as NA

only when specifically authorized in the body of the DCP or EWR

and enhance administrative procedures governing field change

preparation and technical review processes to ensure notification

of shift supervisors and retagging of system boundaries before

working on systems returned to operations under a partial

technical review.

The inspectors reviewed the memorandum to

engineering personnel titled, Lessons Learned-DC 86-15-1 Partial

Technical Review/Subsequent Field Changes, dated December 4, 1990.

This memorandum discussed the event and how to prevent similar

occurrences.

The inspectors reviewed Operations department

memorandum dated January 9, 1991 which explained that steps in

EWRs or DCPs may not be marked NA unless specifically allowed by

the procedure.

The inspectors also reviewed SUADM-ENG-13, DCP/EWR -

h.

11

Implementation and Closeout, dated March 10, 1992 and verified

that it contained instructions that shift supervisor notification,

retagging of system boundaries and review of initial conditions

and precautions are required for continued work or rework on a

system previously released under a partial technical review.

The

inspectors consider that the corrective actions in response to the

violation were properly implemented.

(Closed) VIO 280,281/90-41-01, Failure to Correctly Classify SW

pumps 1-VS-P-IA, 8, and C and CD pumps l-VS-P-2A, 8,.and C in

Accordance With Regulatory Guide 1.26. This issue involved the

improper classification of SW pumps l-VS-P-1A, 8, and C and CD

pumps l-VS-P~2A, 8, and C as non Class 3 components and therefore

erroneously omitted from the licensee's IST p~ogram.

The licensee

responded to this violation in a letter dated March 22, 1991.

In

the letter, the licensee stated that the pumps and valves in the

control-room-envelope air conditioning system were added to their

Section XI program.

The inspectors reviewed Revision 4 to the

Inservice Testing Program Plan and verified that the pumps and

valves in the control room envelope air conditioning system were

in the program.

The inspectors consider that the corrective

actions in response to the violation were properly implemented.

Within the areas inspected, no violations were identified.

8.

Safety Assessment and Quality Verificat1on (40500)

The inspectors attended portions of the June 2 MSRC meeting.

During

that meeting, the plant managers from both stations discussed recent

plant performance and regulatory history. Several proposed TS

amendments were presented and the inspectors determined that an

appropriate level of detailed discussion occurred before approval of

amendments.

The inspectors also monitored the discussion of the CNS

subcommittee report on a new performance monitoring program that was

being proposed. The program was only in the development stage and the

MSRC members had a lot of discussion over the definition of some of the

indicators being monitored. Specifically, there was concern that

indicators such as "nuclear safety" needed to be better defined because

a declining trend may indicate unacceptable performance to one person

but not to another~

The CNS subcommittee chairman indicated that the

comments would be considered and a new draft would be presented during

the next scheduled MSRC meeting.

The inspectors considered the MSRC

meeting was thorough and that discussion of issues at the appropriate

level occurred before decisions/recommendations were made.

9.

12

Exit Interview

The inspection scope and results were summarized on, June 9, with those

individuals identified by an asterisk in paragraph 1.

The following

summary of inspection activity was discussed by the inspectors during

this exit.

Item Number

Status

VIO 280,281/92-13-01

Open

VIO 280, 281/91-24-01

Closed

VIO 280/90-39-01

Closed

VIO 280/90-39-02

Closed

VIO 280/90-39-03

Closed

VIO 280,281/90-36-01

Closed

VIO 280,281/90-41-01

Closed

UNR 280,281/91-33-01

Closed

IFI 280,281/90-30~01

Closed

Description and Reference

Failure to perform safety

evaluations for procedures that were

used to operate plant systems

differently than that described in

the UFSAR.

Failure to comply with the

requirements of TS 3.16.B.1 with the

No. 3 EDG inoperable.

Failure to Follow Precaution 4.19

while performing continuity checks

during the performance of procedure

1-0PT-ZZ-001.

Failure to provide adequate

instructions for testing, resulting

in the unintentional actuation of B

Train CLS HI (SI).

Inadequate field change resulting in

unreliable reactor vessel level

indication.

Low SW flow through the RSHXs.

Failure to correctly classify SW

pumps 1-VS-P-IA, B, and C and CD

pumps l-VS-P-2A, B, and C in

accordance with Regulatory Guide

1.26.

.

Safety evaluations for changes in

the facility.

Followup on licensee corrective

action and testing deficiencies

identified during RSHX SW flow

testing.

13

L(R 280,281/90-20

Closed

LER 280,281/91-17

Closed

Startup and power operation with one

train of containment spray system

. inoperable due to improper deletion

of pressure switch repair from

outage work scope.

Diesel Generator Rendered Inoperable

Due to Personnel Error in Adjusting

the Governor.

10.

Index of Acronyms and Initialisms

BC

CFA

CFE

CLS

CFR

CNS

CTS

DCP

ECCS

EOG

ESF

EWR

. FSAR

HHSI

IFI

  • l&C

IR

1ST

LER

LCO

MOV

MRB

NRC

MSRC

OP

PM

. PMT

PT

QA

RS

.RSHX

SNSOC

SW

TS

UFSAR

UNR

VIO

WO

BEARING COOLING

COMPONENT FAILURE ANALYSIS

COMPONENT FAILURE EVALUATION

CONSEQUENCES LIMITING SAFEGUARD

CODE OF FEDERAL REGULATIONS

CORPORATE NUCLEAR SAFETY

COMMITMENT TRACKING SYSTEM

DESIGN CHANGE PACKAGE

EMERGENCY CORE COOLING SYSTEM

EMERGENCY DIESEL GENERATOR

ENGINEERED SAFETY FEATURE

ENGINEERING WORK REQUEST

FINAL SAFETY ANALYSIS REPORT

HIGH HEAD SAFETY INJECTION

INSPECTOR FOLLOWUP ITEM

INSTRUMENTATION AND CONTROLS

INSPECTION REPORT

INSERVICE TEST

LICENSEE EVENT REPORT

LIMITING CONDITIONS OF OPERATION

MOTOR OPERATED VALVE

MANAGEMENT REVIEW BOARD

NUCLEAR REGULATORY COMMISSION

MANAGEMENT SAFETY REVIEW COMMITTEE

OPERATING PROCEDURE

PREVENTIVE MAINTENANCE

POST MAINTENANCE TEST

PERIODIC TEST

QUALITY ASSURANCE

RECIRCULATION SPRAY

RECIRCULATION SPRAY HEAT EXCHANGER

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SERVICE WATER

TECHNICAL SPECIFICATION

UPDATED FINAL SAFETY ANALYSIS REPORT

UNRESOLVED ITEM

VIOLATION.

WORK ORDER