ML18152A321

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Insp Repts 50-280/91-33 & 50-281/91-33 on 911101-30. Violations Noted.Major Areas Inspected:Operations,Maint, Surveillance,Local Officials & Cold Weather Preparations
ML18152A321
Person / Time
Site: Surry  
Issue date: 12/30/1991
From: Branch M, Fredrickson P, Tingen S, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A322 List:
References
50-280-91-33, 50-281-91-33, NUDOCS 9201280083
Download: ML18152A321 (15)


See also: IR 05000280/1991033

Text

  • UNITED STATES
  • NUCLEA.R REGULATORY COMMISSION

REGION II .

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

. Report Nos.:* 50-280/91-33 and S0-281/91-33

itcen~ee: Virginia Electric and Power Company

5000 Dominion Boulevard:

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

Facility Name:

Surry 1 and 2

License Nos.:

DPR-32 and DPR-37

Approved by: lJ\\N ~

\\t-.vlL

Scope:

P. E. Fredrickson, Section thief

Division of Reactor Projects

SUMMARY

I ~~/J ()/e; (

Date Signed * *

This routine resident inspection was *conducted on site in the areas of plant

operatio~s, plant maintenance, plant surveillance, meeting. with local

officials, and cold weather preparations.

During the performance of this

inspection, the resident inspectors conducted review of the licensee

1s *

backshift or weekend operations on November 10, 13, 14 and 29, 1991.

Results:

In the operations functional ar~a, an unresolved item was identified

concerning the lack of safety evaluations for changes made in the facility

(paragraph 3.a).

.

_

. -

In the operations functional area, with the ,exception of performing safety

evaluations, implementation of the Administrative Control Program was

considered effective (paragraph 3.a).

9201280083 911230

PDR

ADOCK 05000280

G

.

PDR

2

In the operations functional area, a Technical. Specification violation was

  • identified involving administrative controls for containment isolation valves

(paragraph 3.c).

In the operations functional area, fire brigade and control _room staffing were

considered effective ( paragraph 3. b) ..

REPORT DETAILS

1.

Persons Contacted

L ken see *Enip 1 oyees * *

R~ Allen, Super~isor, Shift Operations

W. Benthall, Supervisor, Licensing

  • R. Bilyeu, Licensing Engineer

.

D~. Christian, *Assistant Station Manager

  • J. Downs, Superinte*ndent of -Outage and Planning

D. ~rickson, Superintendent of Health Physics

R. Gwaltney, Superintendent of Maintenance

M. Kansler, Station Manager

T. Kendzia, Supervisor, Safety Engineering

H. Kibler, Engineer, Testin~

  • J. McCarthy, Superintendent of Operations

. *A. Price, Assistant Station Manager

.

R. Saunders, Assistant Vice.President, Nuclear Operations

  • '.*E. Smith, *Site Quality Assurance Manager
  • T. Sowers, Superintendent of Engineering
  • G. Thompson, Supervisor Maintenance Engineering

NRC Personnel

M. Branch, Senior Resident Inspector

  • S. Tingen, Resident Inspector
  • J. York, Resident Inspector
  • Attended ex-it interview.

Other l i cense*e emp l 9yees contacted included contra l room opera tors, shift

technical advisors, shift supervisors and other plant personnel *

. On November 29, 1991, the Chairman _of the Nuclear Regulatory Commission,

Dr. Ivan Selin, visited the Surry_Power Station for a familiarization

tour, to _meet with licensee management and staff, a.nd to review the

current status of the station.

Chairman Selin was accompanied by the'

following pers~nnel: -

_J. Milhoan, Deputy ~egional Administrator, Region II

P. Fredrickson, Section Chief, Branch 2A, Region II

C. Peabody, Special Assistant to the Chairman

NRC Resident Inspectors

The Chairman met with the resident inspectors and selected station

perscinnel and was given a presentation on the status of the* station by

licensee management.

He also was taken on a tour of the station

.including the turbine building, control room, training simulator, and the

independent spent fuel storage installation. The Chairman held a press

2

conference at the Surry Nuclear .Infonnation Center at the end. of his

visit.

Acronyms and initial isms used throughout this report are listed in the

  • 1ast paragraph.

2.

Plant Status

Unit 1 began the reporting period in power operation.

The unit was at

power at the end. of the inspection. period, day 349 of. continuous

operation.

Unit 2 began the reporting period at 60 percent power because of leaking

condenser tubes but attained full power 1 ater in the same day. , The unit

was at power at the end of the inspection period, day 34 of continuous

operation.

3.

Operational Safety Verification (71707,42700,64704)

The inspectors conducted frequent visits to the control room to verify

proper st'affing, operator attentiveness a*nd adherence to approved

prbcedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to. verify operations safety and compliance*

with TS and to* maintain awareness of the overall operation of the

facility.

Instrumentation and ECCS lineups were periodically reviewed

from control room indication to assess operability. Frequent plant tours

were conducted to observe equipment status, fire protection programs,

radiological work practices, plant security programs and housekeeping.

Deviation reports were reviewed to assure that potential safety concerns

were properly addressed and reported.*

a.

Review of Administrative Control Program

Administrative Procedure SUADM-0-26, Administrative Control of

Operational Components, dated October 31, 1991, describes how to

implement AC of valves9 breakers, pumps and other components. Two

examples of the use of AC are when a manual action is required to

ensure that a specific component will operate correctly, and valves

that are required to be locked shut.

Administrative control for

safety-related equipment requires SNSOC approval prior to use. These

controls are req~ired to be specified on AC forms contained* in

SUADM-0-26 or in a procedure approved by SNSOC.

Procedure SUADM-0-26

requires that each AC evolution be screened for a safety analysis in

accordance with VPAP-3001, Safety Evaluations, dated April 1, 1991.

The inspectors reviewed the following SUADM-0-26 AC forms:

AC Sl-91-0825A, dated August 8, 1991, provided instructions for

shutting valve l-SA-226, ESGR pneumatic equipment air supply*

valve, if an SI or fuel handling accident occurred.

When

operating pneumatic equipment in the ESGR, *a special watch is

stationed to immediately shut valve l-SA-226.

This valve is

required to be shut so that a breach in.the SA system outside of

3

the ESGR would not depresslirize the ESGR during an accident

condition.

AC Sl-91-808B, dated August 22, 1991, provided instructions for

removing a temporary hose running through the ESGR door if. a

fire or pressurization cif the ESGR was required.

The ESGR door

is~ fire ba~rier and pressure barrier. A watch was required to

be stationed ai the door and be able tb close the door when

notified by the control room or fire watch.

AC SI-91-0808, dated August 8, 1991, provided instructions -for

establishing controls when the ESGR entrance door flood dike was

removed.

A roving flood watch was established. A second person

was stationed to reinstall the dike if turbine building flooding

was inminent.

Based on the latest flooding issues, the licensee

discon.tinued the use of all AC instructions for removal of

turbine building flood dikes.

AC S2-91-0708, dated July 9, 1991, provided instructions for

establishing controls for removing the A RSSW valve pit missile

_.*shield.

If adverse weather was approaching that could generate

.a missi1e, the missfle shield was required to be reinstalled.

.

.

Each AC form package contained a safety analysis. The inspectors

considered that the above ACs and safety analysis were adequate. The

inspectors also reviewed the following SNSOC approved procedures that

established ACs.

OP 6.2.3, Administrative Control of 1-EG-15, 2-EG-15 or 3-EG-15,

dated January 20, 1990, provided instructions for control of the

EOG air starting system crosstie valve for each EOG.

Each EOG

has two air start banks that are normally isolated from each

.other by valve EG-15~

Each airbank has its own air compressor

to supply pressurized air to the air flasks in the bank.

When

an airbank's compressor is not operable, the airbank must be

filled with air by crossconnecting with the other airbank by

opening EG-.15. * The 'inspectors monitored an evolution where

2-EG-15 was placed under AC in accordance with OP 6.2.3 and

concluded that all procedural requirements involving special

briefings, communications, and instructions were met.

Review of

the procedure's activity screening checklist indicated that a

safety evaluation was not required for this evolution.

The

inspectors reviewed section 8.5 of the FSAR which stated that

each EOG is designed for reliable operation through the use of

redundant components.

One of these redundant components

discussed in the FSAR was duplicate air starting systems with

independent compr~ssors, valves, and accumulators.

The

inspectors considered that crosstonnecting the airbanks

was a

method of operation not addressed in th~ FSAR and therefore a

safety evaluation may be required.

4

0-P 52.2.1, Administrative Control of 1-FP-36, dated October 27,

1989, provided instructions for c6ntr61 of the motor driven fire_

pump recirculation valve 1-FP-36.

This valve is _normally shut

so that the fire suppression system's motor driven fire pump is

able to provide full water flow when automatically started on

low fire-main pressure.

During certain plant evolutions, the

fire suppres$ion system fire pump is utilized to provide water

for non.fire related functions, such as hydrolazing heat

exchangers.

The m.otor driven fire pump is frequently operated

for long_ periods of time with the recirculation valve 1-FP-36

open, and a watch -stationed to en*sure that the valve is shut

within ten minutes if the system was required to combat a fire.

TSs and the FSAR state that* the motor drhen fire pump is

requited to provide 2500 gpm of water*to the fire suppression *

system.

When the pump is aligned in the recirculation -ode, it*

is unable to provide 2500 gpm to the fire suppression sy$tem~

The licensee considers the fire suppression system to- be

operable in this configuration.

The inspectors consider that a

safety evaluation may be required to evaluate whether this

activity will adversely affect the ability of the fire*

.. :suppression system to combat a fire. *

.

.

1-MOP-8.25, Overriding VVl-SW-263, dated No.vember 8, 1991,

-provided instructions for manually overriding the capability of*

VVl-SW-263 to automatically close on receipt of smoke or fire

alarm.

A watch would be stationed at VVl-SW-263 who would shut

the valve within. two minutes after control room notification.

There are two tr~ins of SW that provfde cooling for the* HHS!

pumps' lube oil and seal coolers.

Normally the suctions of the

two trains are cross-connected via VVl-SW-263.

When a smoke or

fire alarm occurs, VVl-SW-263 automatically closes to separate

the trains of SW to the HHS! pumps.

When VVl-SW-263 is under

AC, the fire watches are required to notify the control room of

a fire, and operators would notify the watchstander to shut

VVl-SW-263.

Although the function of VVl-SW-263 is not

discussed in the FSAR, the 1 icensee performed a safety

evaluation for this evolution as required.

2-0P-49.7, Filling And Draining RSHX Service Water Supply.*

Piping, dated September 18, 1991~ provided instructions. to open

normally shut vent and drain valves in the SW system in order to

Operators were

required to be stationed in the turbine and safeguards buildings

to shut the vent and drain valves if SW to the RSHXs.auto-

matically initiated.

Review of the procedure's activity

screening checklist i.ndicated that a safety evaluation was not

required for this evolution.

The licensee considers the SW

system operable in this configuration .. Operation of the -SW

system in this condition is not addressed in TSs or FSAR.* The

inspectors *consider that a safety evaluation may be required to

evaluate whether this activity will adversely affect the

operation of the SW ( i * e. , adequate SW fl ow) sys tern or other


~----

5

systems located iri the area of the open vent arid drain valves

(i.e., flooding or spraying).

1-0P-7.7.2, Filling SI Accumulators,_dated November 15, 1991,

provided instructions to operate valve 1-SI-32 when filling the

SI accumulators~

1-SI-32 is a manual containment i sol ati on

valve that is normally locked shut.

When 1-SI-32 is open to

fill the accumulatbrs, an op~rator is stationed to shut the

valve if_ containment isolation is required.

Review of the

procedure's activity screening checklist indicated that a safety

evaluation was not required for this evolution.

Because the

above AC for locked manual containment isolation valves are

addressed by TSs, the -inspectors concluded that a safety

evaluation.was not_required.

10 CFR 50.59 and VPAP-3001 state that a documented technical

evaluation of a proposed facility or procedure ,change as described in

the safety analysis be performed to determine whether an activity

wi_ll have an adverse affect on plant systems or constitute .an

unreviewed safety question.

Pending further NRC review of this

matter,-

the need to perform safety evaluations for - procedures

OP-6.2.3, OP-52.2.1, and 2-0P-49.7 is identified as UNR 50-280,

281/91-33-01, Safety Evaluations for Changes in the Facility'.

b.

Adequacy of Nuclear -Power Plant Backshift Staffing When the Fire

Brigade is Required

c.

The inspectors reviewed the licensee's minimum shift crew composition

to ensure that there were an adequate number of operators on shift to

combat a fire and safely shutdown the plant.

10 CFR 50.54 control roorri minimum staffing requirements, TS Table

6.l-lminimum shift crew composition requirements, and TS 6.1.B.7

fire brigade staffing requirements were compared to actual .shift

staffing.

The inspectors concluded that shift staffing was adequate.

The fire brigade was composed of ROs not assigned to control room -

duties, non-licensed operator~, and security force members.

Administrative Control of Containment Isolation Valves

At the end of the previous inspection period, the -C MSTV bypass

valve, 2-MS-155 could not b~ fully closed.

This is a manual

containm~nt isolation valve that is required to be locked shut in

-order to establis_h containment integrity.

Because containment

integrity was required at the time of the valve failure, the licensee

entered the action statement of TS 3.0.1 that requires the equipment

be returned to service or the unit be in hot shutdown within six

hours.

Operators were able to shut the valve utilizing a hydraulic

jacking device and e~ited the LCO action ~taiement.

During subse-

quent tours of the-plant, the inspectors noted that the MSTVs

1 bypass

6

valves 1/2-MS-84, l/2~MS-116, and 1-MS-115, altho~gh shut, were not

locked shut.

Discussion with the licensee indicated that the valv.es

  • had never been locked shut..

TS 3.8.A. l requires that* containment

integrity as defined in TS section 1.0, be established ~nless the

reactor is in a cold shutdown condition. TS 1.H defines containment

integrity as existing when an non-automatic isolation valves, except

those required for intermittent operation in the performance of .

normal

operation* activities are locked closed* and under

administrative control.

The failure to lock closed and maintain

administrative controls for containment isolation valves 1/2-MS-84, .

  • l/2-MS-116, and l/2-MS-155 in accordance with TS 3.8.A.1 is *

identified as Violation 50-280,281/91-33-02, Failure to Maintain *

  • Administrative Control* For Containment Isolation Valves *.

As a result

of this issue, the licensee reviewed containment integrity

requirements and identified a~ditional valves that. were not being

properly control led.

At the end of the inspec;tion period, the

licensee was in the process of establishing the reqtiired controls;

Containment isolation valves *a*re spec;:ified in TS Table 3.8.1 and

Section 5.2 of the FSAR.

Per the licensee, 10 CFR 50, Appendix A*

. reactor containment design basis criteria are not applicable to the

plant.

The inspectors review of TS and FSAR indicated that in some

instances these documents. do not specify the same requirements or

requirements are not clearly stated. For example, TS's list the main

steam line isolation valve~ as the main steam trip val~es, while the

FSAR states that.the turbine throttle valves and non-return valves

are the mainsteam* isolation valves.

Neither TSs nor FSAR state that

the MSTVs

1 bypass valves are containment isolation valves, however

the licensee considers them containment isolation valves.

At the end

of the inspection period, the licensee was inittating a corrective

.. action plan to improve the TS and FSAR*ba:sis for containment

isolation valves.

WitMn the areas inspected, one violation was identified.

4.

Surry Internal Flooding IPE Corrective Action Review (71500)

As discussed in IR 50-280,281/91-29 and IR 50-280,281/91-31, the licensee

committed in their October 28 and 29, 1991 letters, to implement several

interim and short term corrective actions to reduce the vulnerability of

the Surry plant to core damage due to postulated flooding scenarios. At

the conclusion of the special team inspection documented in IR 50-280,281/

91-31, the licensee agreed to continue their interim* programs and to .

complete the modifications discussed in their October 29, 1991, letter.

The purpose of this inspection was to document the NRC review of those

modifications and to document recent equipment failures and personnel

errors that may impact assumptions made as part of the IPE.

7

a.

Modifications.

On November 19 and 20, the inspectors reviewed the status of the two

modifications discus~ed in the licensee's October 29, 1991 letter.

The modifications described in the licensee's letter were as follows:

(1)

(2)

Charging pump cubicl~ drain lines will be modified to preverit

backflow.

Planned installation of backflow devices or temporary

installation of blank flanges to close the drain. lines will' be

completed.

This modification eliminates core damage sequences

that initiate from RWST supply floods in either safeguarqs

building.

Flow shields on the six expansion joints in the service water

supply lines for the BC and CC heat exchangers will be

installed.

The inspectors verified the licensee's implementation of these two

modi fi cati ans by reviewing the completed design change packages91-031 and 90-178.

The licensee elected to install backflow devices

in the charging pump cubicles rather than blanking them -0ff.

b.

Recent Equipment Failures and Personnel Errors

(1)

While removing Unit 1 C waterbox from service in accordance with

MOP-48.5, l-CW-MOV-106C was deenergized and tagged prior to the

valve being closed from the control room.

The valve was tagged

shut but was actually in the open position.

The error was

rectified by the licensee's independent verification process.

  • The probable cause of this error was failure to follow the MOP

procedure and a failure to properly implement the tagging

process.* The licensee's corrective action involved discussions

with the operator and evaluation of the event using the HPES

process.

(2) While attempting to throttle open the D waterbox outlet valve,

2-MOV-CW 200D, the licensee discovered the MDV would not move in

. the open direction.

Ari operator at the MOV power supply

verified that the breaker contactor closed and the MOV motor did

energize to 6pen the valve as verified by the. operator at the

MDV Operator attempts to manually (or locally) close the MDV

were also unsuccessful.

The licensee quarantined the valve and

subsequent investigation indicated that the problem was in the

valve operator.

Since the NRC's MDV team was on site the resident inspectors

requested that the team *evaluate the licensee's corrective

actions associated with this recent failure *

(3)

An approximate 10 GPM leak from a 1/2 inch diameter corrosion

pit developed on the outlet side of IC waterbox.

The leak was

5.

(4)

8

on the South side of th~ 96 inch CW outlet .pipe approximately 20

inches above floor.

The piping is designed AWWA class and the

licensee* installed a 1/4 inch thick patch on the external _

surfac~ of the 96 inch pipe.

The* licensee determined that the

corrosion pit appea~ed to be localized and probably resulted

from a failure of the internal coating.

Plans were made to

effect final repair~ during the next refueling outage. At that

time the internal surface can be* repaired by .welding and

relocating.

Inspection of portions of the 96 inch outlet pipes for all eight

water boxes revea 1 ed that there have been many s_uch failures and *

_ repairs in the past.

Additionally, the inspectors questioned

the licensee on the apparent external rusting of the outlet

-piping where it penetrates the conc_rete floor.

During operation of 2-CW-MOV-206D, the manual clutch engagement

. linkage was found to be stuck.

To free the clutch engage~ent

linkage, two operators were required, one on the mezzanine and

one in the* ciftulating water inlet valve pit, tri reposition the

linkage.

This action was necessary to allow local manual

operation of 2-CW-MOV-206D.

The licensee's initial corrective-

action was to submit WR No. 801051, issue a deviation report ,and

notify the shift supervisor.

The previous events were discussed with the NRR risk assessment branch who

  • were evaluating the licensee_' s IPE.

The NRR personnel indicated that the

recent events would be considered as part of their !PE review.

Another commitment made by the licensee was to perform a visual inspection

-of one of the circulating water expansion joints on Unit 1 and this*

activity is discussed in paragraph _5.a.

Within the areas inspected, no violation was identified.

Maintenance Inspections (62703, 42700, 71500)

During the reporting period, ttie inspectors *reviewed mafotenance

activities*to ass*ure compliance with the appropriate procedures.

.

.

The following maintenance activities were reviewed.

a.

Visual Inspection of CW Expansion Joints

During the NRC exit meeting on November 21, 1991, the licensee

committed to visually inspect the condenser outlet B waterbox rubber

expansion joint.

An engineering work request (EWR No. 91~139) was

written to cover this work. This EWR gave the following conditions

that needed to be reported and evaluated:

-e

e

9

Internal Inspection of Expans{on Joint

Areas that feel soft and spongy (indication cif break in rubber

cover and water saturation of underlying fabric)

Thin areas or exposed fabric (indicative of an abrasion problem)

Crackin~ or hardened rubber (indicative of excessive temperature

or heat).

.

External Inspection of Expansion Joint

Leaking at the flange

Cracking on the outside cover (could be environmental attack or

aging)

Cracking at the base of the flange (this is the most critical

stress point)

. *Soft spots/delamination .(indication of p_ly separation)

Bulge between arch and flange (indication of broken reinforcement

caused by overpressure)

.

The inspectors observed the visual examination of the B waterbox

expansion joint on November 25~

There was some bulging, concavity,

sponginess, and linear separations found during the internal visual

examination.

Examination of the outer surfaces of the expansion

joint revealed spongy areas, several thinned areas, an area where the

outer ply was separated (almost one quadrant in length) and exposing

two metal ree_nforcing rings.

One of the rings had rusted

approximately half through the diameter.

As a result of the Unit 1 inspection, the licensee decided to inspect

the same B waterbox on Unit 2.

Visual inspection of the inside of

this joint revealed only three tears that exposed the fabric.

The

external inspection revealed-a number of soft spots but only one area

approximately five inches long where the metal reenforcing ring was

exposed.

As a result of these inspections and discussions with the

vendor, the licensee concluded that significant degradation to these

expan~ion joints had occurred.

A justification for continued opera-

tion (No. C-91-0006 dated November 29, 1991) has been completed and

reviewed by the inspectors.

The licensee has dee i ded to. inspect the remaining six expansion

joints (three for each unit) and is modifying the bottom periphery of

the existing expansion joint shields. This modification would reduce

the flow from 13,000 gpm to approximately 3,000 gpm or less from*a

ruptured expansion joint. The inspectors will continue to follow the

modifications and the inspections of the remaining expansion-joints.

- -**

10

b.

Troubleshooting the First Stage P~essure Loop

c.

On October 6, during the performance of .1-PT-2.8, First Stage

Pressure P-1-446, dated September 18, 1986, the unit began to ramp

back approximately 10 to 20 megawatts.

This occurred *while testing

channel III of first stage pressur~ loop 446.

The inspectors were

present in the control room for the retest on October 8,

arid the

unit began to decrease in power again (the No. 2 governor valve *began

to close).

On November 7, troubleshooting operations were performed

by selectively lifting leads* on the modules for the P 250 computer,

the AMSAC system, and the steam dump system.

The indication was that*

steam dump module TM-l-408W was* affecting. the perodic *test.

Work

Order No. 3800119385 was written to do further troubleshooting to

determine the exact cause of the problem.

The inspectors will

continue to follow this maintenance activity. -

Review of Maintenance Backlog

During the previous SALP period, it was pointed out that a maintenance

backlog problem continued to exist.

This problem had_ also been

identified in several of the previous SALP periods.

In the previous

period, both the number and average age of the non-outage items

increased.

The inspectors reviewed the current status of the

no".1-outage maintenance backlog with the licensee.

The corrective

maintenance work order backlog was approximately 800 at the beginning

of the current SALP assessment period and had dropped to 451 during

this inipection period.

The average age of these work orders. was

approximately 220 days at the beginning of this SALP period a*nd had

dropped to 68 days during this inspection period.

Within the areas inspected, no violations were identified.

6. _ Surveillance Inspections (61726, 42700) *

- During the reporting period, the inspectors reviewed surveillance

~ctivities to assure compliance with the appropriate procedure ~nd TS

requirements.

The following surveillance activity was reviewed:

a.

Unit 2 Containment Door Air Leakage Test

On November 15, the inspectors witnessed the performance of periodic

test 2-0PT-CT-303, Personnel Airlock Leakage Test (Door Seal Test),

dated March .12,1991.

The purpose of this procedure is to .test the

personnel airlock inner and outer door seals within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> after

opening to verify that the door seals were not damaged during use in

accordance with TS 4.4.B.2.

The inspectors witnessed the testing of

the Unit 2 containment* door.

The test was accomplished satisfac-

torily with no deficiencies noted.

Within the areas inspected, no violations were identified.

,*

11

7.

Information -Meetings with Local Officials (94600)

The Senior Resident Inspector met with the Board *of Supervisors of Surry

County on November 7, at the Surry Courthouse Complex.

The purpose of

this meeting was to discuss with the board the results of the_NRC's

inspection of corrective actions associ~ted with internal flooding as

noted .in the IPE and to answer any questions concerning this matter.

8.

Cold Weather Preparations (71714)

During this inspection period, the inspectors reviewed the licensee's

. program for implementation of protective measures for extreme cold

  • weather.

The program is .implemented by monthly performances (October

through March) of STP-52, Cold Weather Protection, dated February 27,

1990.

This special procedure is a detailed checklist of areas and

.components that need to be routinely inspected to ensure that there is

. adequate protection to prevent freezing.

The majority of* STP-52 is

performed by operations department personnel.

Maintenance department

personnel are required to verify that piping heater tape operates satis-

. factory.

Deficienc-ies that are noted during the performance of STP-52 are

documented* *and provided to planning to schedule corrective action.

The

inspectors reviewed the performance copy of STP-52 that was completed in

November, reviewed the list of deficiencies generated by the performance

of STP-52, and also checked the w6rk-status of these deficiencies.

The *

inspectors concluded that STP-52 contained adequate instructions to

prevent freezing, and that operations and maintenance department personnel

satisfactorily performed the procedure.

However, the inspectors noted that the deficiencies generated by the

performance of STP-52 were not being completed in a timely matter.

Specifically, the inspector monitored the status of the low-level intake

structure. and noted that the .completion of the insulation of the recent

heat tracing for the service water system was* not scheduled until the end

of December.

The inspectors discussed the late December completion of

heat tracing insulation with plant management.

The licensee has placed

  • additional* attention* on the timely completion o.f the needed freeze

protection repairs as indicated by placing it .on the station priority

list.

The inspectors. did not consider this*. a significant deficiency

because extreme cold weather has not occurred, and if extreme cold weather

was forecast, the list of STP-52 deficiencies could be corrected in a .

short period of time if they are .assigned a higher priority on the POD ..

Additionally, installation of temporary insulation and space heaters could

also be used to correct the identified deficiencies.

Within ihe areas inspected, no ~iolations were identified *

12

9.

Exit Interview

The inspection scope and results were sununar.ized on ~ovember 8, 1991, with

those individuals identified by an *asterisk in paragraph 1. The following

sununary of inspection activity was discussed by the* inspectors during this

exit.

Item Number

URI 280,281/91~33-01

VIO 280,281/91-33-02

Status

Description and Reference

Open

Safety Evaluations for Changes in the

Facility, paragraph 3.a.

Open

Failure To Maintain Administrative

Controls For Containment Isolation

Valves, paragraph 3.c.

The licensee acknowledged the inspection conclusions.

However, the

1 icensee indicated that they did not agree that there was a need to

perform a safety evaluation for those procedures listed in UNR 280,281/

91-33..;.Ql.

The inspectors informed the 1 i censee that their position would

be co~sid~ted as part of the NRC review of this issue .. The licensee did

not identify as proprietary any of the materials provided to or reviewed

by the inspectors during this inspection.

11.

Index of Acronyms and Initialisms

AC

AMSAC

AWWA

BC

cc .

CFR

cw

ECCS

EOG

ESF

ESGR

EWR

FSAR

GPM

HHSI

HPES

IPE

LCO

LER

MER

MOP

MOV

MSTV

NCV

NRC

ADMINISTRATIVE CONTROLS

ATWAS MITIGATION SYSTEM ACTUATION CIRCUIT

AMERICAN WATER WORKS ASSOCIATION

BEARING COOLING

COMPONENT COOLING

CODE OF FEDERAL REGULATIONS

CIRCULATING WATER

EMERGENCY CORE COOLING SYSTEM

EMERGENCY DIESEL GENERATOR

ENGINEERED SAFETY FEATURE

EMERGENCY SWITCHGEAR ROOM

ENGINEERING WORK REQUEST

FINAL SAFETY ANALYSIS REPORT

GALLONS PER MINUTE

HIGH HEAD SAFETY INJECTION

HUMAN PERFORMANCE ENHANCEMENT SYSTEM

INDEPENDENT PERFORMANCE EVALUATION

LIMITING CONDITION OF OPERATION

LICENSEE EVENT REPORT

.

MECHANICAL EQUIPMENT ROOM

MAINTENANCE OPERATING PROCEDURE

MOTOR OPERATED VALVE

MAIN STEAM TRIP VALVE

NON-CITED VIOLATION

NUCLEAR REGULATORY COMMISSION

NRR

POD

RCS

RSHX

RO

RSSW

RWST

SALP

SI

SNSOC

SRO

STA

SUADM

.sw

TS

URI

WR

-*

.,.

13

OFFICE OF NUCLEAR REACTOR REGULATION

C PLAN OF THE DAY

REACTOR COOLANT SYSTEM

RECIRCULATION SPRAY HEAT EXCHANGER

REACTOR OPERATOR

RECIRCULATION SPRAY SERVICE WATER

REFUELING WATER STORAGE TANK

SERVICE AIR

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

SAFETY INJECTION

STATION NUCLEAR AND SAFETY OPERATING COMMITTEE

  • SENIOR REACTOR OPERATOR

SHIFT TECHNICAL ADVISOR

SURRY ADMINISTRATIVE PROCEDURE

SERVICE WATER

TECHNICAL SPECIFICATIONS

UNRESOLVED ITEM

\\ilORK REQUEST