ML18152A242

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Insp Repts 50-280/92-07 & 50-281/92-07 on 920308-0404. Violations Noted.Major Areas Inspected:Operations,Maint, Surveillance,Reliable DHR During Outages,Loss of DHR & Quality Verification
ML18152A242
Person / Time
Site: Surry  Dominion icon.png
Issue date: 04/29/1992
From: Branch M, Fredrickson P, Tingen S, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A243 List:
References
50-280-92-07, 50-280-92-7, 50-281-92-07, 50-281-92-7, NUDOCS 9205190103
Download: ML18152A242 (17)


See also: IR 05000280/1992007

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report No~.:

50-280/92-07 and 50-2?1/92-07

Licensee:

Virginia Electric and Power Company

5000 Dom~nion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50~281

Facility Name:

Surry 1 anc\\ 2

License Nos.:

DPR-32*and DPR-37 *

Inspection Conducted:

March 8 through April 4, 1992

Inspectors:

Approved by:

Scope:

. E.F.'ckson, Section Chief

  • vision d' Reactor Projects

SUMMARY

DiJ;1~~~a

.., I~, I ~J..

Date Signed

. 'i ~)-; (1 }-

Da~

Signed

V>£/f2--

0'ate*signed

This routine resident inspection was conducted on -site in the areas of

operations, maintenance, surveillance, reliable decay heat removal duri.ng

outages, loss of decay heat removal, and qua 1 i ty veri fi cation and safety

assessment review.

During the performance bf this inspection, the resident.

inspectors conducted *review of the licensee's backshift or weekend operations

on March 11, 14, 15, 16, 21, 22, 28, 29, and April 2 and 4, 1992.

Results:

In the operational functional area, failure to align the No. 3 e~ergency diesel*

generator speed dial .scribe marks in accordance with the governoring procedures

was identified as Non-Cited Violation 280,281/92-07-01, Failure to Follow

Procedure When Testing No. 3 ~mergency_ Diesel Generator (paragraph 3.b).

In the operational functional area, weaknesses involving procedure adequacy,

and operator and shift technical advisor attention to detail were identified

when returning the No. 1 emergency diesel generator to service following relay

testing (paragraph 3.b).

9205190103 920429

PDR

ADOCK 05000280

G

PDR

2

In the operational functional area, Violation 280/92-07-02 was identified for

failure to establish adequate containment integrity when conducting refueling

operations {paragraph 3.c).

.

.. *

..

In the* maintenance functional ar*ea,* over the past year the licen~ee decreased

the number of open nonoutage* co.rrective maintenance work*orders by one~half and

the average age of these work orders by two-thirds (paragraph 4.a}.*

In th~ maintenance. furi~tional area, Violation 280/92-07-03 was identified for

the failure to prevent foreign mateiial from* entering the service water system

while maintenance was performed during the previous refueling outage (paragraph

5.a).

In the. safety assessment/quality verification area, the -Critical Parameter

Assessme*nt Matrix enhanced the licensee's ability to monitor the status of

plant parameters and systems important to safety during an outage.

During the

current outage, the licensee reev~luated the need to dr~in the reactor coolant

system to mid-loop level in order to drain steam generator tubes and concluded-

that draining to mid-loop was not necessary.

The elimination of this

previously routine mid-loop evolution was a another enhancement to outage plant

safety (paragraph 6).

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • W. Benthall, Supervisor, Licensing
  • R. Bilyeu, Liceniing Engineir
  • H. Blake, Superintendent of Sit~Services

D. Christian, Assistant Station Manager

  • *J. Downs, Superintendent of Outage and Planning

A. Fletcher, A_ssistant Superintendent of Engi-neering

R. Gwaltney, Superintendent of Maintenance

D. Hart, Supervisor, Quality Assurance

  • M. Kansler, Station Manager
  • A. Keagy, Superintendent of Materials
  • J. McCarthy, Superintendent of Operations
  • J. McGinnis, Human Performance Evaluation System Coordinator
  • A. Price, Assistant Station Manager
  • R~ F. Saunders, Assistant Vice President-Nuclear, Corporate
  • E. Smith, Site Quality Assurance Manager
  • T~ Sowers, Superintendent of Engineering
  • G. Woodzell, Senior lnstructor

NRC Personnel

M. Branch, Senior Resi~ent Inspector

  • S. Tingen, Resident Inspector
  • J. York, Resident Inspector
  • Attended exit interview.

Other licensee employees contacted included control room operators, shift

technical advisors, shift supervisors and other plant personnel.

Acronyms and initialisms used throughout this report are list~d in the

last paragraph.

2.

Plant Status

Unit 1 began the reporting period in a *refueling outage and continued in

thls mode throughout the inspection petiod. At the end of the inspection

period the unit was in day 36 of a 64 day outage.

Unit 2 began the reporting period in power operation.

The unit was at

power at the end of the inspection period, day 108 of continuous

operation.

2

3. Operational Safety Verification (71707,42700)

The inspectors conducted *frequent tours of the control room to verify

. proper staffing, operator attentiveness and adnerence to approved

procedures.* The inspectors attended plant status meetings and reviewed*

operator logs on a daily basis to verify operations.safety and compliance

.with TS and *to maintain awareness of the over a 11 opera ti on of the *

facility.

Instrumentation and ECCS lineups were periodically reviewed

from control room indication to assess operability.

Frequent plant tours

were conducted to observe equipment status, fire protection programs,

radi ol og i cal work practices, pl ant secliri ty programs and housekeeping.

Deviation reports were reviewed to assure that potential safety concerns

. were properly addressed and *reported.

a.

Licensee 10 CFR 72 Reports

b.

On March 17, at 2:32 a.~~~ the licensee report~d to the NRC that a

contractor was transported off site by the station ambulance.

The

contractor slipped on a wet floor .in the Unit 1 containment and*

injured his back.

The individual exited the containment under his

o~n power and was not contaminated.

On March 18 at 4~4j p.m., the litensee reported to the NRC*that the

No. 3 EDG automatically started due to personnel error. Maintenance

personnel were pulling cable in an energized Unit 1 J emergency bus

undervoltage 'panel and bumped a relay inside the panel causing the*

EOG to start.

An actual undervoltage condition did notexist and the

. No .. 3 EOG did not 1 oad on either of its emergency buses.

On Mar~h 23, at 5:20 p.m., the licensee reported tti the NRC that a

contractor was transported offsi te by the station.ambulance.

T.he *

individual had abdominal pains and was not contaminated.

On March 25, at 3:17 p.m., the license~ reported to the NRC that a

fisherman was tr.ansported offsite by the station ambulance.

The

individual was fishing in the station**s SW discharge canal and fell

into the canal.

The individual was conscious when pulled fr*om the

canal and was not contaminated. -

On March 31, at 6:27 p.m., the licensee report~d to the NRC that

three contractor~ were contaminated at approximately the same time

while erecting scaffolding in the Unit 1 containmeht.

The source of

contamination was insulation dust that became airborne after bei~g

bumped.

Whole body' counts and bioassay evaluations performed on*

. three individuals inaicated no internal contamination.

EOG Restoration Problems

During the inspection period, the No. 1 and 3 EDGs were taken out of

servic~ for maintenance.

On several occasions after completion -of

the maintenance, operators did not properly restore the EDGs.

3

On March 26, fol lowing maintenance, the 'No. 3 EDG was test~d in

accordance wi.th procedures O-OP-EG-001, Number 3 EDG, dated Ma~ch 25,

1992, and O-OPT-EG-6.l, Number 3 EOG Exercise Test, dated May 29,

1991.

At the completion of the test, No. 3 EDG_was declared fully

operable.

Two days later on March 28, operators noted that the

scribe marks on the No. 3 EOG. governor speed control dial were not

aligned;

The system engine~r was contacted and informed operati~ns

that a new governor was installed during the previous maintenance.

He stated that the speed control dial was at the correct setting, and

since it was a new governor, it needed to be rescribed.

Later that

day, the speed control dial was rescribed to ag_ree with the new

setting.

Step 5.3.12 of O-OP-EG-001 requires that the speed control dial.

scribe marks be aligned.

As ,a result of a corrective action

implemented in response to Violation 280,281/91-24-0l, the procedure

contains a verification that the scribe marks are aligned.

The

inspectors reviewed O-OP-EG-001 and verified that step 5.3;12 was

initialed by operators as being completed.

The inspector~ concluded

.that in order to comply with O-OP~EG-001 the ~cribe marks on the

speed control dial needed to be changed to the new setting or the

procedure changed to. recognize that the scribe marks were not

aligned.* It was concluded that although the procedure was not

. followed, the EDG was fully operable.

Failure to align the No. 3 EDG

speed dial scribe marks in accord~nce with O-OP-EG-001 was identified

as NCV 280,281/92-07-01, Failure to Follow Procedure When Testing No.

3 EOG.

This NRC identified violation is not being cited because *

criteria specified in Section V.A of the NRC Enfor*cement Policy were

satisfied.

On March 27, No. 1. EDG was placed in exercise in order to perform

scheduled relay testing and adjustment in accordance with. procedure

1-EMP-P-RT '."36, Protective Relay Maintenance for EOG No. 1 Differ-

entia_l Relays, dated May 28, 1987.

On March 28, this evolution was

completed and the No. 1 EDG was returned to service and considered

fully operable.* Approximately 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> later, on March 29, during a

walkdown of the control board, a the control room operator noticed

that the No. 1 EDG auto start disabled alarm was energiz~d.

Further

investigation revealed that the No. 1 EOG non-auto alarm was also

_en~rgiied.

The EDG was declared inoperable.

The cause of alarms was

determined to be the EDG's exciter field breaker being in *the tripped

position.

The licensee concluded that the exciter field breaker was

tripped during the performance of l-EMP-P-RT-36 and that the EOG was._

inoperable while the exciter field breaker was in the tripped

position.

However, no TS LCO action statement time restraints were

exceeded.

The inspectors identified*weaknesses *involving procedure

adequacy and attention to detail as a result of this event.

Procedure l-EMP-P-RT-36 did no~ provide instructions to restore the

exciter field breaker to its nor~al positi9n after being repositioned

by the procedure.

Also; for approximately one and a half s~ifts,

the operators and STAs failed to identify an energized control room

  • C *

4

board walkdowns.

Evaluation of Loss of Containment Refueling Integrity

On Apri 1 3, the 1 i censee detenni ned that containment integrity for

refueling was violated during the on-loading of fuel elements into

the the Unit 1 reactor vessel.

Breaches in containment involved

d*irect paths. from the containment to the environment via the FW and

MS line~ associated with the A and B SGs.

Details of the breached

containment condition and contributing causes are. provided below *.

Detaili of the Breaches

The first direct path from containment to the environment

existed via openings in the B SG whil.e at the same time work was

being performed on the B SG MSTV (1-MS-TV-101B) and its bypass

check valve (1-MS-117).

The hand ho)e covers were removed from

the B SG and the inte~na1s had been previously removed from the

MSTV which is located in the main steam line between the SG and

the turbine building.

There is a bypass. line around the MSTV

for warming up the MS piping, and this bypass line has a manual

valve and a downstream check valve (1-MS-117)'.

At the time of

fuel movement on April 2 the bonnet of 1-MS-117 was removed and .

a FME cover with no gasket was installed. This closure was not

in accordance with the refue 1 i ng integrity procedure 1-0P-lG,

Refue 1 i ng Con ta i riment Integrity And RCS Mid-Loop Containment

Closure Checklist, dated March 19, 1992, and would not have

provided a positive barrier from the environment.

This path

through 1-MS-117 was not recognized by operations or maintenance

planning in that, procedure 1-0P-lG did not tnclude this valve

in the verification.

Also, during the time of fuel movement an

active WO for removing valve 1-MS-117 was being worked and

pipi~g cuts for valve replacement had been started.

The second path from contain~eni ~o the environmerit involved an

open 3/4 inch drain valve (l~FW-9) on the A SG FW line at the

same time that the MSTV (1-MS-TV-lOlA) had its- internals.removed

with a wo6den FME cov~r installed on the ~onnet of the valve .

. The path would have been from the containment into the 3/4 inch

FW drain valve into the SG out through the MS line and to the

environment through the improp~rly sealed wbod~n blank on the

MSTV._

The FW drain valve had.been prevjously tagged open for

anticipated FW valve work and it was n6t realized at the time of

establishing refueling integrity in that, the barrier was

thought to b~ an intact SG inside containment since work on the

A MSTV was authorized and scheduled to work in parallel with

fue 1 movement.

While investigating thi~ event, the inspectors discovered that

during the core off-load between March 17 and 20 the second leak

5

path.through the FW drain valve also existed .. This conclusion

was determined throu~h interviews and .was bas~d on the time of.

tagging open 1.:.FW-9 { 3/l0/92.) and when work was being performed

on 1-MS-TV-lOlA.

This valve had only a* wooden* FME cover

installed..

The inspectors determined through interviews and review of work

logs, that although the openings on the valves in safeguards

were not sealed in accordance with the requirement of the*

refueling integrity procedure, 1-0P-lG; the openings were

covered at all time during fuel movement.

2.

Consequence of Loss of Containment Refueling ln.tegrity'

TS 3.10 provides *requirements and restrictions that are.

necessary for refueling activities.

The basis of this TS is to

ensure that refueling unit cortditions conform to the conditions

assumed in the accident analysis for a fuel handli.ng accident.

The fuel handling accident is described in section 14.4.1 of the

UFSAR which includes. several cases of releases from the

containment.

Case 3, which is the most limiting for offsfte

release but still well below the 10 CFR part 100 c"riteria,

involves a release from a fuel handling accident.without

isolation of the containment purge system.

Case 3 assumes that

all of the radionuclides released from a fuel handling accident

that reaches the surface of the water are rel eased from

containment through charcoal filters that remove 70 percent of

the iodine.

The licensee's NA&F group performed a ~pecial an~ly~is of the

Apri 1 2, 1 oss of refueling integrity event and compared the

results with the the UFSAR analyzed events.

The licensee's

analysis detenni.ned that the consequences of a fuel handling.

accident during the fuel movement of April 2 would be limited to

a dose much less than* that eva 1 uated in the UFSAR.

This

determination was based on two pri nci pa 1 reasons.

First the

April 2, loss of integ*rity occurred 34 days after shutdown

rather that 100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> as assumed in the UFSAR analysfs~

The

second difference was that the release assumed in the UFASR was

an~entire release of activity in the containment through the 70

. percent effi ci.ent fi 1 ters due to venti 1 ati on system not *

isolating.

Theref6re, the release volume through the improperly

sealed openings would be much less than the total release volume

assumed in the UF"SAR analysis.

  • The licensee's analysis also concluded that for the April 2,

event there was no pressure driving head to force any activity

through the openings.

The analjsis determined that there was no*

credible mechanism for significant containment pressurization~ *

Even with a complete loss of RHR, th*e cavity flooded and two

fuel elements in the core,. it would have taken many hours before

6

the RCS temperature reached saturation.

The boiloff rate would

be *slow and would not result in any significant containment

pressurization.

The licensee performed a second analysis for the March 17

through 20 event.

This analysis also concluded ~hat there was

no *pressure driving _head to force any activity through the

opening and that th~ total release volume through the improperly

sealed opening would be less that the total released volume

assumed in the UFSAR analysis.

The inspectors and the NRC staff reviewed the- licensee _analysis

and agree that for the conditions described, the consequences of

the events were bounded by the UFSAR analysis;-

However, as

discussed in the basis for TS 3.10, controls of refueling

activities have to be in place and properly controlled to ensure

adequate protection at all times and for all situations.

3.

Contributing Causes of the Los.s of Refueling *Containment

Integrity

The inspectors reviewed the licensee's program for establishing

and controlling refueling containment integrity as required by

TS 3.10.

The licensee's controls of the initial condition for

fuel movement is specified in refueling procedure OP-FH-01,

  • . Refueling Operations," dated March 6, 1992.

This procedure

requires the establishment of refOeling containment integrity

which is accomplished by completion of procedure 1-0P-lG.

This

  • procedure is also used as a surveillance procedure for periodic

reverification of integrity with each of the three zones being

verified twice a week.

The integrity established and maintained by 1-0P-lG is a single

barrier outside of containment.

Therefor~, for the case of the

breach that occurred from the A SG, while work. was being *

performed on 1-MS-TV-lOlA in parallel with refueling activities,

it is *not clear that procedure 1-0P-lG was appropriate.

The

barrier established was inside rather than outside as described

in the procedure.

The inspector's interviews with operation

personnel determined that there was no clear trail as towhat

was done to verify the integrity of the A SG boundary inside

containment. Additionally, it could not be determined if the FW

line for the A SG which had the tagged ope~ 3/4 inch drain valve

was included in the barrier verific~tion.

For the breach of the

barrier associated with work on valve l-MS-117 ," procedure

1-0P-lG did recognize the need for boundary extension due to

.removal of the internals of trip valve 1-MS-TV-1018.

Also, it

. was determi__ned that procedure 1-0P-lG re qui red the use of

special order tags for ensuring that barriefs associated with

7

temporary blanks are in. place but did not require valve

  • boundaries to be tagged.

As noted in * the sequence of events, work on severa 1 * of the

. valves that were being used for boundaries was authorized and in

some cases ongoing.

Operations and work planning groups were

trying to perform parallel tasks an.d control the moving

boundaries by verbal job holds or the use of special tags that

were intended to recapture the equipment to be used for barriers

even though authorized work re 1 eases were outstanding.

The

inspectors determined,*that due. to the outage scope and schedule

there were more work-around.maintenance it~ms being performed

this ou*tage than during previous outages. . These work-around

maintenanc~ items were also being done for the SW lines th~t

penetrated containment.

No instances of breach of integrity was

identified with the. SW work, and it appears that management had

recognized the potential problems in this area and concentrated

on better controls.

The containment refueling integrity breaches that occurred

during the Unit_ 1 core off-load ~nd portions of the core on-load

were identified as Violation 280/92-07-02, *Failure to Establish

Containment Refueling Integrity in Accordance with TS 3.10.A.1

. and Failure to Follow Procedure in Accordance with TS 6.4.D .

. Within the areas inspected one NCV and one cited violation were

identified.

4.

Maintenance Inspections (62703, 42700,)

During. the reporting* period,* the inspectors reviewed maintenance

  • . activities to assure compliance with .the appropriate procedures.

The following maintenance activity was reviewed.

a.

Maintenance Backlog

On March 24, the inspectors requested the status of the current

maintenance backlog and were provided the following information .

8

CORRECTIVE MAINTENANCE

NUMBER

Nonoutage corrective maintenance work orders (less minor work)

403

These WOs require action to repair or restore

functional capability of failed equipment.

Nonoutage corrective maintenance average age in days

88

Nonoutage minor corrective maintenance-work orders

1168

These WOs do not require engineering, tagout or

detailed maintenance procedures

Outage corrective maintenance work orders

These WOs do not include minor work.

2277

PREVENTIVE MAINTENANCE

Open nonoutage preventive maintenance work orders

Open outage preventive maintenance work orders

Deferred preventive maintenance work orders

-639

1120

22

Over the SALP assessment* period the licensee decreased the number of open

nonoutage corrective maintenance work orders by one~half and the average

age of these work orders by two-thirds.

Within the areas inspected, no violations were identified.

5.

Surveillance Inspections (61726, 42700)

During the reporting period, the .inspectors reviewed surveillance

activities to assure compliance with the appropriate procedure and TS

requirements.

The following surveillance activity was reviewed:

a.

Flow Testing of the Service_ Water Side of the Unit 1 RSHXs

During this inspection perio*d, -the inspectors witnessed flow testing

of Unit 1 RSHXs 1-RS-E-lB and 1-RS-E-lC. The test ~as performed in

accordanc~ with special test procedure l-ST-299, Recirculation Spray

Heat Exchangers Service Water Fl ow Test, dated December 12, 1991.

This test had three purposes:

(1) to co*l lect data to verify that

design basis accident SW flow is adequate to remove design basis heat

loads from containment, (2) to collect data to develop a calibration

curve for the new V-cone flow elements, and (3) to functionally test

modifications to the 58 and 5C SW radiation monitoring pumps .

-.

9

The pretest preparations, w~ich included i~stallation and checkout of

test equi pmerit and -the -pretest briefing, -were observed.

The

inspectors reviewed test procedure l-ST-299 and found the procedure

to be technically adequate~

The test began on March 16 at_l:36 a.m.

and was moni tared by the inspectors from both t_he control* room and

the Unit 1 safeguards area. The second objective of the special test

was successful, i.e., enough data was collected for a calibration

curve.

The third obje~tive was also successful. This objecttve was

identified d~ring the flow testing on Unit 2 on April 6, 1991, when

. the radiation monitor pumps on each of the SW outlet pipes fai-1 ed to

self prime.

Two different modifications were evaluated during the

test.

One modifitation involved the increase in size of the suction

line from three-fourths of an inch in diameter to two inches in

diameter and ihe installation of a check valve in the discharge line.

A second modific~tion involved the installation of a suction tank and

the installation of a check valve in the discharge line.

Each

modification was insta1led in a separate pump.

Both modifications

achieved acc_eptable results and the licensee decided to install the

larger size suction line/check ~alve combinations for these pumping

systems.

The preliminary test results for the adequacy of the SW fl ow showed

that the flow rate through the C RSHX was slightly less than

anticipated and the flow through the B RSHX was significantly less

than anticipated.

The preliminary calculations using the

conservative criteria of calculation_ ME-0266 revealed that- thi SW

flow in the C RSHX was approximately 20 percent blocked and the flow

in the B was approximately 55 percent blocked.

A* calculation was

performed that showed the heat transfer capability was such that both

of these RSHXs were co*ns i dered operable using a SW temperature of 92

degrees Fahrenheit and for the entire 18 mon_th period that Unit 1 had

operated.

Unit 2 was considered operable also because this unit had

_been placed in service five months later than Unit 1 and should have

less blockage potential due to fouling.

The inspectors accompanied licensee personnel to perform a visual

inspection of the B RSHX once the elbow .to vessel was removed.

This

inspection revealed that a rain jacket and rain pants wefe present in

the tubesheet area and* were the apparent reason for the 1 ow flow

(there were very few hydroids. present).* Durin.g a meeting on

March 30, the licensee postulated that this rain jacket and pants had

been left in the pipe during the previous- pipe coating operation

because there appeared to be a small amount of the coating on tbe

rain jacket.

A review of DCP no. 90-26-1, Heat Exchanger Service

  • _Water Piping Cleaning and Recoating/Surry/Unit 1, dated October 2,

1990, indicated that FME controls were in effect at the time the

piping was last coated.

This* is identified as VIO 280/92-07-03,

Failure _to Prevent Foreign *Material Exclu.sion in the SW System.

6.

10

b.

Reactor Head Vent Flow Pith Verificatiori

Prior to removal of ' the Unit 1 reactor head, the * RCS was

depressurized with level being maintained at about the ejghteen. foot

level which is slightly below the ~eactor head flange.

This was not

a reduced inventory condition.

The only visible means of RCS level

indi~ation at this level was th~ RCS standpip~ assembly and the unit

was in this condition for approximately a week.

For the first part*

of the week, level in the standpipe properly responded when fillihg

and draining reactor coolant from the vessel; however, at the end of

the week, the standpipe level was not i.ndicatirig properly when

filling the reactor from the VCT.

After securing from a filling

evolution it would take an additional twenty minutes for reactor

level* to stabilize.

On March 15, level in the reactor vessel

unexpectedly dropped one foot in level. Operators ilTITlediately added

approximately 1000 gallons to the vessel to. restore level.

Subsequent investigation revealed that the level dropped when the

last reactor head stud was detentioned. Detentioning the head vented

the top of the reactor vessel to containment atmosphere causing level

to drop.

The reactor head was then removed and standpipe assembly

secured.

  • In order for the standpipe assembly to indicate properly the reactor

head has to be vented to the pressurizer.

Piping and tygon tubing

are utilized to accomplish this task.

On March 19, this line was

flow tested with air in accordance with procedure l-TOP-4014, Reactor

Head Vent Flow Path, dated. March 18, 1992.

This testing was*

accomplished in the Unit 1 containment and was witnessed by the

inspectors.

The testing was accomp 1 i shed in accordance with the

procedure and did not identify any blockages. Several days later the

standpipe assembly was tested and satisfactorily operated.

At the

end of the inspection period, the 1 i censee had not reso 1 ved the

reason for the standpipe level perturbations.

After fuel is loaded.

into the co*re, the reactor head wi 11 be i nsta 11 ed and the standpipe

  • . assembly will be ~laced back into servite. The licensee will monitof

the standpipe assembly and if the problem reoccurs will attempt to

troubleshoot while the standpip~ is in service.

Within the areas inipected~ one violation was identified.

.

.

Reliable Decay Heat Removal .During Outages (TI.2515/113)

(Closed) 280 ,281/TI/2515/113

The inspectors reviewed 1 i censee procedures

to ensure reliable OHR capability during plant outages.

Implementation of

requirements ~nd condu~t of certain activities during the current Unit 1

RFO were reviewed for accuracy.

TSs 3.1.d, 3-:10.6 and 3.10.7 specify

minimum OHR requirements when RCS temperature is 1 ess that 350F.

The

1 i censee utilizes procedures and management oversight of day to day outage

activities to ensure reliable OHR..

-

STA~OI-22, Surry Power Station CSD/RSO Critical Parameters, dated March 4,

1992~ was developed by the licensee to provide an independent method for -

11

monitoring the status of plant parameters a*nd sy~tems important to safety

. during an outage.

The STA evaluates* and categorizes the critical

parameters and develops a Critical Plant Parameter Assessment Matrix on a

daily basis.

The matrix is distributed to management for review.

The

inspectors also review the matrix.

One of the purposes -0f this matrix~ is

to summarize and evaluate the status of systems required to provide DHR.

STA-01-22, also requires the develQpment of the CSD/RSD Critical Parameter

Seven Day Look Ahead Matrix.

The Outage and Planing d~partment is

required to provide SNS with a schedule of events for the upcoming week.

SNS evaluates and categorizes the status of critical ,plant parameters

based on the schedule.

This matrix also sunmarizes and evaluates- the

status of systems required to provide DHR and is distributed to mana~e~ent

for review.

Operation during redu.ced inventory operations is discussed- in paragraph *

7. AP-27, Loss of Decay Heat Removal*Capability, dated March 8, 1991,

is utilized for loss of RHR during reduced inventory operations, and is

also utilized on loss of RHR during bther cold shutdown operations.

AP-27

provides alternative methods of DHR including natural* circulation and

several methods of feed and bleed~

Also, during CSD and RSD conditions,

. STA

1s are required to monitor RCS inventory and leakrate in accordance

with 1-0PT-RC-10.2, RCS/CSD Inventory balance, dated March 19, 1992.

Calculations are performed each shift in order to identify RCS leakage *.

Operations_ personnel

perfor~ walkdowns * daily in accordance with

.

. OPT-RC-10.1, RCS Leakage Walkdown at Cold Shutdown, dated May 6, 1991*, in

order to identify anyRCS leakage to atmosphere.

Occasionally, a nonstandard backfeed. electrical lineup is utilized during

outages. * This is considered a special evolution, therefore, an SRO is

assigned *to coordinate this evolution.

Procedures are also utilized ..

Whenever there is fuel in the reactor, offsite power and emergency power*

are available to one emergency bus and offsite power or emergency power is

  • available to the other emergency bus.

The vital bus distribution system

is designed such that the vital buses remain energized during battery or

. DC bus maintenance.

Also, the licensee declares an EDG in6perable when

its field flashing source is removed for maintenance.

The inspectors concluded that the licensee's controls to ensure that decay*

heat removal capability is maintained during CSD/RSD are adequate and will.

continue to monitor these controls throughout the Unit 1 outage.

The

Critical Parameter Assessment Matrix which was recently . implemented,

S ignifi Cantly enhanced the 1; Censee IS *ability to monitor the Status Of

plant parameters and systems important to safety during an outage.

During the current outage, the licensee reevaluated the need to drain the

.RCS to mid-loop level in order to drain the SG tubes and concluded that

draining to mi.d-loop was* not necessary.

The elimfoatfon of this *

previously routine mid-loop evolution was a another enhance~ent to outage

plant safety.

Within the areas inspected, no violations were identified.

12

7.

GL 88~17~ Loss of DecaY Heat Removal (TI 2515/103)

(Closed) 280,281/TI/2515/103

GL 88-17 discussed expeditious actions and

program enhancements that licensees should implement to increase plant

safety when operating a plant at reduced inventory or mid-loop conditions.

In letters to the NRC dated January 6, February 3, September 29, and

October 31, 1989, October 5, and November 16, 1990, and November 14, 1991, *

the licensee responded to GL 88-17 *. In a letter dated July 26, 1991, the

NRC informed the licensee that their responses met the intent of GL 88-17.

The inspectors reviewed the 1 i censee' s response _to v,eri fy that the

licensee had implemented actions and program enhancements as corrmitted.

!Rs 286,281/90-30 ~nd 39 and 91-10, 14, and 18 dis~ussed implementation of

GL-88-17 commitments.

The inspectors concluded that the h_ardwa*re

-procedure changes were performed as corrmitted but noted the following:

In the licensee's February 3, _1989, response, the licensee stated

that a hard piped reactor vessel level indication system was

installed and operable.

During the present Unit 1 outage the

inspectors walked this system down.

The portion of this system that

contains the standpipe assembly was hard piped.

However, the portion

of the sys*tem that. vents the reactor vessel head contained one inch.

diameter har_d pipe with approximately twenty .feet of tygon tubing

connecting the hard piping to the . top of the pressurizer.

The

inspectors concluded that if steam formed in the reactor vessel, then

the reactor vessel standpipe level indicati9n system would not

indicate properly because the tygon tubing would melti or the small.

diamete.r head vent piping would not pass sufficient flow _to provide

an adequate vent path.

The licensee does utilize ~n ultrasonic

reactor vessel level indication system that measures RCS cold leg

level which is in addition to the standpipe assembly.

This system

would indicate properly with steam in the reactor vessel. During the

  • pre~ent Unit 1 RFO~ the ultrasohic re~ctor vessel level indication

system has not been operable due to spiking problems and theref6re

has not been used. Procedures only require that the ultrasonic. level

indication system be in service* when entering a reduced inventory

condition.

The GL requires that controls be established to assure that

containment closure can be achieved in the event that a 1 oss of

cooling occurs.

The GL also states that if RCS boiling occurs, a

potential exists for incfeased containment temperature and pressure .

. The licensee is in the process of evaluating the potential for

increased containment press~re in the event of a loss of RCS cooling.

Present procedures that establish containment closure* utilize

containment barriers that have not been evaluated for containment

~ressure requirements.

In. the October 31, 1989, res~onse to the GL, the.licensee stated that

the annunciator for high temperature at the RHR di~charge to RCS is

13

an aid in monitoring RHR system performance and identifying abnonnal

conditions.

The inspectors noted that this alann ocurrs at 340F.

The inspectors consider that with* the RCS system depressurized, an

alarm at 340F is too high for providing indication of*a loss of core

cooling *. The inspectors discussed this issue with the licensee, and

the .licensee was in-the process of revising procedures to lower this

alarm setpoint when the inspection period ended.

Within the areas inspected no violations we~e identified.*

8 *.

Safety Assessment and Quality ve*rification

During. the previous inspection period, the inspectors* monHored the

licensee's program for the review of generic industry issues and

experience.

This review was documented in IR 280,281/92~04 and indicated

that the appropriate level of corporate screening. of information was

occurring.

During this inspection period, the* inspectors reviewed the

process that the site uses to implement or evaluate the corporate

reco111T1endations for improvement.

The inspectors also.selected for review,

several items that had been forwarded to the station for implementation.

The site review process is controlled by procedure -VPAP 3002, Operating

Experience Review, dated 11-30-90.

Section 6.2.8 of this procedure

specifies the method that the station should use to handle industry

operating experience.

The procedure specifies that the SNS group is

responsible for the bnsite .implementation of the process and requires that

a station deviation be initiated if the-initial SNS review determines that

an item_ is directly applicable to _the station and may require immediate

corrective action.* In addition to receiving OE items from the corporate

process, the station al so directly routes industry experience for

infor~atfon to those departments th~t may be involved.

Although the extra

r~uting of information may be redundant to the process described iri IR

_ 280,281/92-04, personnel interviewed by the inspectors felt that it was a

safety net to the OE process. and provides more timely notification to

involved parties.

Within the areas inspected, no violations were identified.

9.

Ex_it Interview

_The inspection scope and results were summarized on, April 14, 1992, with

. those individuals identified by an asterisk in paragraph 1.

The following

summary of inspection activity was discussed by the inspectors during this

exit .

14

Item Number

NCV 280,281/92-07-01

Status

Closed

Description and Reference

Failure to Follow Procedure

When Testing No. 3"EDG (paragraph

3.b.).

VIO 280/92-07-02

Open

Failure to Establish Containment

Integrity in Accordance with TS 3.10.A.1 and Failure to Follow

Procedure in Accordance with TS 6.4.D {paragraph 3.c.).

VIO 280/92-07-03

Open

Failure to Prevent Foreign

Material From Entering Service

Water System (paragraph 5.a.).

TI 280,281/2515/113

Closed

Reliable Decay Heat Removal

During Outages (paragraph 6)~

TI 280,281/2515/103

Closed

GL 88-17, Lo~s of Decay Heat

Removal (paragraph 7).

10.

Index of Acronyms and Initialisms

CFR

CSD

DC

DCP

-OHR

ECCS

EOG

ESF

F

FME

FW

GL

IR

LCO

MS

MSTV

NCV.

NRC

OE

RCS

RFO

RHR

RSD

RSHX

SALP

CODE OF FEDERAL REGULATIONS

COLD SHUTDOWN

DIRECT CURRENT

DESIGN CHANGE PACKAGE

DECAY HEAT REMOVAL

EMERGENCY CORE COOLING SYSTEM

EMERGENCY DIESEL GENERATOR

ENGINEERED SAFETY FEATURE

FAHRENHEIT

FOREIGN MATERIALS EXCLUSION

FEEDWATER

GENERIC LETTER

INSPECTION REPORT

LIMITING CONDITION FOR OPERATION

MAIN STEAM

MAIN STEAM TRIP VALVE

NONCITED VIOLATION

NUCLEAR REGULATORY COMMISSION

OPERATING EXPERIENCE

REACTOR COOLANT SYSTEM

REFUELING OUTAGE

RESIDUAL HEAT REMOVAL

REFUELING SHUTDOWN

RECIRCULATION SPRAY HEAT EXCHANGER

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

SG

. SNS

SRO

STA

SW

  • _

TI

TS

UFSAR

VCT*

VIO

VPAP-

WO _

15

STEAM GENERATOR

STATION NUCLEAR SAFETY

- - -

SENIOR REACTOR OPERATOR

SHIFT TECHNICAL ADVISOR

SERVICE WATER

TEMPORARY INSTRUCTION

TECHNICAL SPECIFICATIONS

UPDATED FINAL SAFETY ANALYSIS REPORT

VOLUME CONTROL TANK

VIOLATION

VIRGINIA POWER ADMINISTRATIVE *PROCEDURES

WORK ORDER