ML18152A107

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Insp Repts 50-280/91-14 & 50-281/91-14 on 910512-0608. Violations Noted.Major Areas Inspected:Plant Operations, Plant Maint,Plant Surveillance,Ler Closeout & Licensee Self Assessment Capability
ML18152A107
Person / Time
Site: Surry  
Issue date: 07/08/1991
From: Branch M, Frederickson P, Holland W, Tingen S, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A108 List:
References
50-280-91-14, 50-281-91-14, NUDOCS 9107160227
Download: ML18152A107 (23)


See also: IR 05000280/1991014

Text

-

UNITED STATES

NU-AR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos.:

50-280/91-14 and 50-281/91-14

Licensee:

Virginia Electric and Power Company

5000 Dominion Boulevard

Glen Allen, VA

23060

e

Docket Nos.:

50-280 and 50-281

Facility Name:

Surry 1 and 2

License Nos.:

DPR-32 and DPR-37

Inspector

7

"-1

Dat Signed

7/rj,,

Date Signed

o:Zffis;~

1

- J

Accompanying Personnel:

B. Buckley, Senior Project Manager, NRR

Approved by:

SUMMARY

Scope:

7fa'ft1

DateSigned

This routine. resident inspection was conducted on site in the areas of plant

operations, plant maintenance, plant surveillance, licensee event report

closeout, and licensee self assessment capability.

During the performance of

this inspection, the resident inspectors conducted review of the licensee's

backshift or weekend operations on May 13, 15, 16, 19, 21, 22, 26, 28, 31,

June 1, 2, 5, and 7.

Results:

In the safety assessment/quality verification functional area, one example of a

violation was identified for failure to provide adequate instructions and/or

  • procedures when implementing a revision to TS 3.11 regarding waste gas decay
  • tank H2/0 2 limitations.

A similar North Anna problem occurred in March, 1991,

9107160227 910708

PDR

ADOCK 05000280

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PDR

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2

and the resultant corrective actions could have prevented this violation.

(paragraph 3.a)

In the operations functional area a continuing strength was identified

regarding operator attention to detail and sensitivity to plant conditions and

reactivity management during the Unit 2 startup.

Good communi cati ans and

selfchecking techniques were frequently observed between operations personnel.

(paragraph 3.b)

In the engineering/technical support functional area, an additional example of

the violation for failure to provide adequate instructions and/or procedures

was identified.

This involved a failure to implement safety analysis

assumptions contributin~ to a Unit 1 reactor load increase above licensed power

limits. (paragraph 3.c)

In the maintenance/surveillance functional area, a weakness was identified

regarding previous corrective actions, associated with air lock deficiencies,

being ineffective in correcting material condition problems of the equipment.

(paragraph 3.d)

In the safety assessment/quality verification functional area a strength was

identified regarding the licensee making available a second means of level

indication for reduced inventory operations ahead of their commitment and prior

to entry into reduced inventory condition. This action demonstrated a positive

sensitivity to safety.

(paragraph 3.g)

In the safety assessment/quality verification functional area, a violation

associated with the seal head tank low level alarms was identified for failure

to promptly identify and correct conditions adverse to quality (paragraph 5.a).

...


,--------------------------~

  • e

1.

Persons Contacted

Licensee Employees

REPORT DETAILS

R. Allen, Supervisor, Shift Operations

  • W. Benthall, Supervisor, Licensing
  • R. Bilyeu, Licensing Engineer
  • R. Blount, Supervisor, Station Procedures
  • D. Christian, Assistant Station Manager

J. Downs, Superinterident of Outage and Planning

D. Erickson, Superintendent of Health Physics

  • R. Gwaltney, Superintendent of Maintenance

M. Kansler, Station Manager

T. Kendzia, Supervisor, Safety Engineering

  • J. McCarthy, Superintendent of Operations
  • A. Price, Assistant Station Manager
  • H. Royal, Supervis*or, Nuclear Training
  • E. Smith, Site Quality Assurance Manager
  • T. Sowers, Superintendent of Engineering

NRG Personnel

  • W. Holland; Senior Resident Inspector
  • M. Branch, Senior Resident Inspector

S. Tingen, Resident Inspector

  • J. York, Resident Inspector
  • Attended exit interview.

e

Other licensee employees contacted included control room operators, s,h.ift

technical advisors, shift supervisors and other plant personnel.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Plant Status

Unit 1 began the reporting period in power operation.

The.unit operated

at or about 100% power for the duration of the in~pection period.

However, on June 6, 1991, reactor power was reduced to approximately 93%

when the unit experienced turbine iontrol problems.

This item is further

discussed in paragraph 3.c.

Unit 2 began the reporting period in refueling shutdown (day 45 of a

scheduled 67 day refueling/maintenance outage).

During this period the

.unit entered reduced inventory conditions for approximately four pays to

conduct maintenance activities on safety injection check valves.

This

item is further discussed in paragraph 3.g.

Also the unit completed

,**

,*

e

2

refueling/maintenance evolutions and Type.A containment testing. The* unit

exited cold shutdown conditions on May 31 and had reached hot shutdown

conditions when identified leakage greater than TS allowable limits were

identified. AUE was declared and the unit returned to cold shutdown to

correct the leakage problem. This issue is further discussed in paragraph

3.f. Corrective actions were completed and the unit commenced heatup from

cold shutdown on June 4.

The unit was taken critical on June 5 and

physics testing was conducted over the next 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

The unit was

connected to the grid on June 7. However, approximately 25 minutes after

connection, an electrical problem in the switchyard occurred resulting in

opening of an electrical breaker in the yard.

This problem is further

discussed in paragraph 3.b. After the electrical problem was corrected,

the unit was reconnected to the grid on June 7 to continue startup testing

and was operating at approximately 30 percent power when the inspection

period ended.

3.

Operational Safety Verification {71707 & 42700)

a.

Daily Inspections

The inspectors conducted daily inspections in the following areas:

control room staffing, access, and operator behavior; operator

adherence to approved procedures, TS, and LCOs; examination of panels

containing instrumentation and other reactor protection system

ele~ents to determine that required channels are operable; and review

of control room operator logs, operating orders, plant deviation

reports, tagout logs, temporary modification logs, and tags on

components to verify compliance with approved procedures.

The

inspectors also routinely accompanied station management on plant

tours and observed the effectiveness of their influence on activities

being performed by plant personnel.

On May 24, during routine review of operator logs, the inspectors

noted that the following information was recorded with regards to

concentrations of oxygen and hydrogen in the waste gas holdup tanks.

On May 24, at 0025 hours2.893519e-4 days <br />0.00694 hours <br />4.133598e-5 weeks <br />9.5125e-6 months <br />, routine sample results of the A WGDT

revealed that the oxygen and hydrogen concentrations exceeded the TS

limits.

The A WGDT oxygen concentration was 8.6%, and the hydrogen

concentration was 4.6%.

TS 3.11.A.1 states that the concentration of

oxygen in the waste gas holdup system shall be limited to 2% by

volume when the hydrogen concentration exceeds 4% by volume.

TS 3.11.A.1.a states that with the concentration of oxygen in the waste

gas holdup system greater that 2% by volume but less than or equal to

4% by volume, and the hydrogen concentration greater than 4% by

volume reduce the oxygen concentration to the required limits within

48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />.

TS 3.11.A.l.b states that with the concentration of oxygen

greater than 4% by volume immediately suspend all additions of waste

gases to the affected tank and reduce the concentration of oxygen to

less than or equal to 4% by volume.

3

A backup sample of a WGDT A on May 24, 1991, confirmed that the

oxygen and hydrogen concentration level exceeded the TS limits.

Operators suspended all additions of waste gases to A WGDT, made

preparations to release the tank in accordance with procedure

OP-23.2.3, Placing 1-GW-TK-lA On Bleed, dated February 8, 1990. Prior

to releasing the A WGDT, operators determined that OP-23.2.3 needed

to be revised and decided to wait until day shift to revise the

procedure.

The procedure was revised on day shift and at 0946 hours0.0109 days <br />0.263 hours <br />0.00156 weeks <br />3.59953e-4 months <br />,

operators initiated the release of the A WGDT.

The following day,

May 25, at 1448 hours0.0168 days <br />0.402 hours <br />0.00239 weeks <br />5.50964e-4 months <br /> the A WGDT oxygen and hydrogen concentration

levels were within the TS limitations.

The release of the tank was

then secured and the TS LCO exited.

The inspectors reviewed the licensee's actions and considered that

the actions did not meet the requirements of TS 3.11.A.1.b because

action was not taken irrnnediately to reduce the concentration of

oxygen in the A WGDT to less than 4% by volume.

It took

approximately 38 hours4.398148e-4 days <br />0.0106 hours <br />6.283069e-5 weeks <br />1.4459e-5 months <br /> to reduce the oxygen concentration to less

than 4% by conducting a long tank drain prior to actually reducing

the oxygen concentration with nitrogen.

Only several hours are

necessary to reduce the concentration, if the nitrogen addition is

conducted at the beginning of the evolution.

A primary contributor to this problem was a TS amendment effecting

this activity.

TS 3.11.A, Explosive Gas Mixture, was amended on

April 17, 1991.

This new amendment required ilTD'Tiediate action be

taken when WGDT oxygen and hydrogen concentrations exceeded 4% by .

volume.

The old TS 3 .11. A a 11 owed 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> to reduce the oxygen

concentration to less than 4% by volume.

The inspectors concluded

that the licensee did not develop an adequate plan to correctly

implement the requirements of TS 3.11.A.1.a and 3.11.A.l.b when the

TS 3 .11 amendment was approved.

As a result, procedures and

instructions were not in place to immediately reduce the A WGDT

hydrogen/oxygen concentrations on May 24.

10 CFR 50, Appendix B, Criterion V, requires that activities

affecting quality be prescribed by* documented instructions or

procedures of a type appropriate to the circumstances and shall be

accomplished in accordance with instructions, or procedures.

The

failure to provide adequate instructions and/or procedures when

implementing the revised TS 3.11 is identified as one example of a

Violation, 50-280,281/90-10-0l, Inadequate Implementatinn of a Waste

Gas Decay Tank TS.

North Anna had a similar problem in March 1991

where releasing the tank contents, instead of purging with nitrogen,

was used in an attempt to reduce the concentration.

During review of the waste gas problems.described above, the

inspectors noted that tank sampling was necessary as a compensatory

measure because the H2/02 monitors were not operable.

TS 3. 7-2.E

for the explosive gas monitoring instrument requires that the

equipment have an alarm/trip setpoint set to ensure that the limits

..


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4

of TS 3.11.A.1 are not exceeded.

The actions for inoperable

monitoring instrumentation requires that a grab sample be taken at

least once per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and analyzed within the following 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.

The inspectors observed that grab samples were being taken at

approximately 12-hour intervals. Even with this increased sample

frequency, though, on four occasions during the inspection period,

the samples were in the range that required entry into TS 3.11.A.1

LCOs.

Since the purpose of the grab samples was to compensate for .

inoperable instrumentation and to ensure that the TS 3.11 limits were

not exceeded, the inspectors questioned as to whether the licensee

had considered further increasing the sample frequency.

Discussions

with station management on this issue resulted in implementation of a

policy to review sampling frequency and increase the frequency based

on sample results.

b.

Weekly Inspections

The inspectors conducted weekly inspections in the following areas:

operability verification of selected ESF systems by valve alignment,

breaker positions, condition of equipment or component, and

operability of instrumentation and support items essential to system

actuation or performance.

Plant tours were conducted which included

observation of general plant/equipment conditions, fire protection

and preventative measures, control of activities in progress,

radiation protection controls, physical security controls, missile

hazards, and plant housekeeping conditions/cleanliness.

The

inspectors routinely noted the temperature of the AFW pump discharge

piping to ensure increases in temperature were being properly

monitored and evaluated by the licensee.

During this period, the licensee returned Unit 2 to power operation

after a refueling/maintenance outage that lasted over two months.

The inspectors monitored the performance of the operations department

during the restart and made the following observations:

New startup controlling procedures were used by the operators

during the unit startup.

These procedures appeared to provide

for good control of startup evolutions.

However, the procedure

for unit startup, 2-GOP-1.1, Unit Startup, RCS Heatup From

AMBIENT TO 195 F, revision 0, should have been clearer in

recognizing the pl ant entry conditions for restart after

correction of the valve leakage problem discussed in paragraph

3.f.

Similar to previous startups, operator attention to detail and

sensitivity to plant conditions and reactivity management

continued to be very good.

Good co111T1unications and self

checking techniques were frequently observed between operations

personnel and was considered to be a continuing strength.

5

On June 6, approximately 25 minutes after Unit 2 was connected to the

grid, a loss of electrical load was experienced.

The unit was

supplying approximately 80 megawatts of power at the time.

The loss

of load occurred when a crew working in the switchyard noticed that

one of the electrical disconnects in the electrical flowpath from

Unit 2 to the grid was arcing and appeared to be on fire.

The

supervisor of the crew notified the load dispatcher of the condition.

In accordance with normal policy, the dispatcher opened a breaker in

the switchyard to remove the load from the arcing disconnect. After

the load was disconnected, the arcing stopped.

The operators on Unit

2 responded to the loss of load and were able to stabilize the unit

and reduce reactor power from approximately 25 percent to less than 5

percent over the next hour.

Based on the excellent performance by

the operators, no reactor or turbine trip occurred. Several problems

were encountered during the transient including improper operation of

the A feed regulation bypass valve, and setpoint drifting of the A

steam generator PORV.

All problems were corrected over the next 18

hours and the unit was again connected to the grid early on June 8,

1991.

c.

Biweekly Inspections

The inspectors conducted biweekly inspections in the following areas:

verification review and walkdown of safety-related tagouts in effect;

review of sampling program (e.g., primary and secondary coolant

samples, boric acid tank samples, plant liquid and gaseous samples};

observation of control room shift turnover; review of implementation

of the plant problem identification system; verification of selected

portions of containment isolation lineups; and verification that

notices to workers are posted as required by 10 CFR 19.

On June 6, 1991, Unit 1, while operating at 100 percent power,

turbine control problems occurred that resulted in an 80 MWE power

increase.

The operator noticed and logged the following and

immediately took manual control of the turbine:

All turbine governor valve went to 100% open

  • Rods stepping out in auto
  • Turbine load going to 880 MWE

Reactor high power alarm at 103%

  • High steam line flow on two out of three channels

The turbine control problem was caused by a failure of the main speed

pickup card for the turbine governor control circuit.

The licensee

wrote station deviation S-91-0887 to document and evaluate the event.

The inspector witnessed portions of the licensee's response to the

transient and reviewed several of the control room recorder and alarm

printouts.

The inspector noted that the licensee was operating the

turbine with the governor valve position limiter set at 100 percent

turbine load which did not restrict governor valve movement.

The

turbine is oversized when compared to the 100 percent reactor power

d.

6

limit and two of the governor valves are not full open at 100 percent

reactor power.

Therefore, when all of the governor valves came full

open, reactor power exceeded the licensed limit for a brief period of

time.

The inspectors reviewed the safety analysis chapter of the UFSAR

(Chapter 14) to determine if there was any restriction on turbine

load limits.

Section 14.2.8, .Excessive Load Increase Incident,

stated that excessive loading by the operator or by system demand

would be prevented by the turbine load limiter.

The UFSAR further

indicated that reactor protection is provided by the high reactor

power and delta-T trip setpoints. * The inspectors reviewed the

turbine operating procedure 1-0P~2.2.1, dated January 2, 1990 and the

turbine inlet valve stroke test procedure 1-PT-29.1, dated January 6,

1990, for information on use of the turbine load limiter.

Both

station procedures instructed the operator to set the limiter at 100

percent.

With the turbine oversized with respect to full reactor

power, setting the limiter for 100 percent valve open does not

prevent exceeding the 100 percent licensed reactor power limits.

Thus, the load limiter requirements from Section 14.2.8 of the UFSAR

have not been incorporated into station procedures .

10 CFR 50, Appendix B, Criterion V, requires that activities

affecting quality be prescribed by documented instructions or

procedures of a type appropriate to the circumstances and shall be

accomplished in accordance with instructions, or procedures.

The

failure to provide adequate instructions and/or procedures to

implement the UFSAR operating requirements is identified as a second

example of Violation, 50-280, 281/90-10-01, Inadequate Turbine

Operating and Testing Procedures.

Other Inspection Activities

Inspections included areas in the Units 1 and 2 cable vaults, vital

battery rooms, steam safeguards areas, emergency switchgear rooms,

diesel generator rooms, control room, auxiliary building, cable

penetration areas, Unit 2 containment, low level intake structure,

and the safeguards valve pit and pump pit areas.

RCS leak rates were

reviewed to ensure that detected or suspected leakage from the system

was recorded, investigated, and evaluated; and that appropriate

actions were taken, if required.

The inspectors routinely

independently calculated RCS leak rates using the NRC Independent

Measurements Leak Rate Program (RCSLK9).

On a regular basis, RWPs

were reviewed, and specific work activities were monitored to assure

they were being conducted per the RWPs.

Selected radiation

protection instruments were periodically checked, and equipment

operability and calibration frequency were verified.

During a control room observation on May 13, 1991, the inspectors

noted that the Unit 1 CRO and SRO became involved with a problem

associated with the inside personnel airlock door.

Specifically, a

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team of electricians who were exiting containment, reported that the

inside airlock door was jammed and would not close.

This*condition

resulted in the electricians being stuck in the airlock and not being

able to open the outside door because of containment integrity

interlocks and differential pressure.

The inspectors observed

operations response to this condition and noted that there was some

question as to what actions should be taken.

The Operations*

Superintendent's response to the situation which included calming the

team of electricians was considered good.

Discussions with the.

control room operators, though, revealed that many riperators had a

personal experience associated with being stuck in the airlock.

The inspectors reviewed a printout of DRs associated with the airloc.k

over the past 2 years and noted that there has been a continuing

problem with this equipment.

The airlock doors are required by TS 3.8 to be operable and closed for containment integrity.

Addition-

ally, the inspectors inspected the material condition of the Unit 2

inside airlock door which is identical to the Unit 1 door.

A combin-

ation of original design (i.e. single point of attachment and closure

mechanism) with the age and condition of the doors appears to have*.

contributed to the door failures and jamming.

Additiona.lly, it was

not clear .that the electricians operating the door had the training

. or experience to ensure proper operations.

The inspectors discussed the above observations and findings ~ith

plant management.

The station manager indicated that airlock door

operation was a continuing problem for both units and that actions

were planned.

The licensee sated that upgrading of the doors had

been evaluated and was at one time on the proposed plarit improvements

list.

However, priority of this ~pgrade has decreased to make way

  • for more ~ressing items.

The station manager indicated that airlock

improvements will be reviewed in light of recent problems and that

short term actions, which may include using a tra:ined door operator

to operate the. door, will *be implemented.

Previous corrective

actions, associated with air lock deficiencies, have been ineffective

  • . in correcting the material condition of the equipment and is identi-

fied as a weakness.

It should be noted, that establishing contain-

ment integrity for the heatup of Unit 2 from the current refueling

outage had to be delayed, due in part.to air lock door problems.

e.

Physical Security Program Inspections

In the course of monthly activities, the inspectors included a review

of the licensee's physical security program.

The performance of

various shifts of the security force was observed in the conduct of

daily activities to include: protected and vital areas access

controls; searching of personnel, packages, and vehicles; badge

issuance and retrieval; escorting of visitors; and patrols and

compensatory posts.

No discrepan'Cies were noted.

.*

f.

e

Licensee 10 CFR 50.72 Reports

On June 3, 1991, the licensee made a report in accordance with 10 CFR

50.72 regarding entrance into the station emergency plan.

At 1431

hours, Unit 2 declared a UE due to uncontrolled RCS leakage exceeding

TS 3.1.C.5 limits of 10 GPM.

The unit was in hot shutdown with RCS

temperature and pressure in the normal operating range (i.e. 547

degrees F and 2235 psig) at the time of the event. The leakage rate

was calculated to be approximately 16 GPM and was from the packing

area of the "C" RCS RTD manifold isolation valve 2-RC-95 and was

observed blowing into the containment.

The leakage was unisolable

from the

RCS

loop and the licensee commenced a plant

cooldown/depressurization at approximately 1432 as required by the

TS.

The UE was terminated at 0506 on June 3, after the unit reached

cold shutdown at 0454.

The RCS leakage first appeared as a 6 GPM

leak into the POTT through the packing leakoff line and the licensee

attempted to backseat the valve to stop the leakage.

The packing

blew out after several attempts to backseat the valve. Operati.ons

personnel, who had just climbed down from trying to backseat the

valve, were not hurt when the packing failed.

The resident

inspector was on-site monitoring startup evolutions when the event

  • occurred and observed the licensee actions and followup.

The

reporting requirements of 10 CFR 50. 72 were met and the 1 icetisee

actions associated with taking the plant to a cold shutdown condition

were in accordance with the TS.

The Operations Manager's decision to

take the plant to cold shutdown was not delayed and action was

started within the first ten minutes after determining that the

leakage rate exceeded TS limits.

The valve repairs and failure determination is further discussed in

paragraph 4.d.

g.

Reduced Inventory Conditions - Unit 2

Unit 2 entered a reduced inventory condition on May 17, 1991 in order

to conduct maintenance activities on safety injection check valves.

This condition was exited .on May 21, 1991.

Prior to entry into this

condition, the inspectors conducted a review of the 1 icensee' s

responses and implemented actions with regards to the requirements of

Generic Letter 88-17, Loss of Decay Heat Removal.

No discrepancies

were noted during the review.

The specific items reviewed were:.

Generic Letter 88-17 - The inspectors reviewed the subject

letter including the licensee's response to the letter dated

January 6, with supplemental responses dated February 3,

September 29, October 31, 1989, October 5, and November 16,

1990 .

Administrative Controls - The inspectors discussed controls and

procedures in affect to control reduced inventory operation with

the Operations Superintendent as well as several senior reactor

operators and licensed operators.

Additionally, the inspectors

attended a reduced inventory planning.meeting on May 14, 1991,

.

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9

where controls, precautions and required equipment status were

reviewed.

Containment Closure Activity - The licensee's procedures require

that the status of the containment configuration be established

and verified prior to entering a reduced inventory condition.

In addition, the procedure for loss of RHR capability directs

containment closure action to be initiated and continued until

the RHR system is returned to service and core conditions are

verified normal. The inspectors verified that the licensee has

prepared procedures to reasonably assure that containment

closure wi 11 be achieved prior to the time at which core

uncovery could occur.

This was done by reviewing 2-0P-3.4,

Draining the Reactor Coolant System, dated March 28, 1991,

2-0P-lG, Refueling Containment Integrity and RCS Mid-Loop

Containment Closure Checklist, dated April 28, 1989, and

2-AP-27, Loss of Decay Heat Removal Capability, dated March 28,

1991.

Other than the containment personnel entry hatch and the

equipment hatch, no containment openings will exist.

During a

containment tour on May 15, 1991, the inspector verified that

there was little obstruction in the way of the equipment hatch

and that the containment closure crew should have little

difficulty in closing the hatch.

RCS Temperature - The inspectors verified that the controlling

procedure for draining the RCS, 2-0P-3.4 required at least two

operable incore temperature indicators prior to draining the RCS

to a reduced inventory condition.

The inspectors also verified

that the control room operators record the temperatures every

six hours in their log as required by periodic test 2-PT-36,

Instrument Surveillance.

In addition a supplemental check list,

Control Room Operator Reduced RCS Inventory Relief Checklist,

requires at least two operable core exit thermocouples (i.e. one

from each train).

RCS Level Indication - The licensee has installed one means of

level indication which provides continuous readout in the

control room.

This system is calibrated and provides a low

level alarm for both low level and loss of level.

In a letter

dated October 31, 1989, the licensee committed to install a

second means of RCS level indication prior to the end of the

current Unit 2 refueling outage.

The licensee had completed the

construction portion of this modification, and this instrumenta-

tion was available to operators during this reduced inventory

period and provided additional assurance to operators of the RCS

water level.

The licensee plans to validate this equipment

during this reduced inventory evolution and operators

interviewed by the inspector were aware of the current status.

During the May 14, 1991, planning meeting, the 1 icensee

indicated that during the initial drain-down to mi d-1 oop an

operator will be stationed inside the containment to visually

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10

monitor the standpipe level.

Additionally, operations was

instructed to monitor the UT system and if differences between

the two level monitoring systems were noted, the draining

operation was to be stopped. The licensee's actions to make

available this second means of level indication ahead of their

commitment and prior to entry into reduced inventory condition

demonstrated a positive sensitivity to safety and was identified

as a strength.

RCS Perturbations - The inspectors verified that the licensee

has a procedure, OC-28, Assessment of Maintenance Activities for

Potential Loss of Reactor Coolant Inventory dated January 22,

1991, that allows for operations' assessment of work on systems

for potential loss of reactor coolant inventory during reduced

RCS inventory conditions.

RCS Inventory Addition - The inspectors verified that procedure

2-0P-3.4 required at least two available and operable means of

adding inventory to the RCS.

These are in addition to the RHR

system.

The procedure requires that in a reduced inventory

condition, one charging/safety injection pump and one LHSI pump

must be available with appropriate flowpaths to the core .

However, during the review of the licensee's procedure 2-0P-3.4

the inspector noted that the procedure did not specify a

preferred injection path to the RC hot leg as specified in the

licensee's respqnse to GL 88-17, dated January 6, 1989.

In that

response the licensee stated that,

11The flow path checklist

specifies that the hot leg injection flow path is preferred,

with cold leg injection available as an alternative."

The

inspector discussed with the 1 icensee a concern that the

controlling procedure (2-0P-3.4) did not specify the preferred

flow path.

The licensee indicated that the checklist referenced

in their response is 2-0C-6 which does specify the hot leg as

the preferred path.

This checklist is performed every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />

by the control room operators. However, use of the checklist to

establish the preferred flow path in-lieu of the operating

procedure may not ensure that the pref erred fl ow path is

available as a prerequisite for the intended inventory

reduction.

The inspector was satisfied that the preferred flow.

path wi 11 be a 1 i gned for the majority of the reduced inventory

operations scheduled for May 17, 1991.

The licensee is

evaluating the need to reference the checklist or to specify the

preferred flow path in the operating procedure as well as in the

turnover checklist.

Loop Stop Valves - -The licensee utilizes RCS loop isolation

valves for loop isolation.

Nozzle dams are not used.

The

licensee uses an operational checklist (OC-28) to ensure that

the reactor vessel upper plenum is adequately vented when

maintenance activities require opening of a RCS cold leg

pressure boundary.

The licensee ensured that the reactor vessel

11

was adequately vented by maintaining A and Bloops unisolated

with the loop bypass valves open.

Contingency Plans to Repower Vital Busses - The vital and

emergency electrical distribution system receives offsite power

from the A and C reserve station service transformers during

normal plant operations.

The RHR pumps and the CCW pumps, the

latter providing cooling water to the RHR heat exchangers,

operate off stub busses attached to the 2J and 2H emergency

buss es.

The stub buss es are shed during degraded or under-

voltage situations, but can be reconnected to the emergency

buss es by closing a breaker.

The equipment for the two

additional*means for adding inventory to the RCS, charging pumps

and LHSI pumps are powered off the 2H and 2J emergency busses.

During normal operations, the number 2 EOG supplies power to the

2H emergency bus in case of a degraded or undervoltage

situation, and the number 3 EOG supplies power to the 2J bus.

During this period, the licensee had the A and C reserve station

service transformers powering the emergency busses, and 2 and 3

EOGs available as emergency power sources.

The inspector noted

during a review of planned testing that the licensee had

scheduled performance of the number 2 EOG survei 11 ance test

while in reduced inventory. This test which is a 6-hour test,

aligns the EOG to the el ectri cal grid for loading and grid

perturbations could affect the EOG availability.

  • These

conditions have occurred in the past and are recognized in

industry and regulatory information.

The licensee subsequently

informed the inspector that they reevaluated testing of the EOG

during reduced inventory operation and elected to either test

the EOG prior to or after reduced inventory operations as long

as their required surveillance grace period was not exceeded.

During the above review the inspector noted that a number of

procedures were required to perform reduced inventory operations.

This is similar to other procedure problems that have been noted at

Surry and the licensee indicated that consolidating the reduced

inventory evolution will be considered during the procedure upgrade

program.

Within the areas inspected, no violations were identified.

4.

Maintenance Inspections {62703 & 42700)

During the reporting period, the inspectors reviewed maintenance

activities to assure compliance with the appropriate procedures.

The following maintenance activities were reviewed:

a.

Non-Regenerative Heat Exchanger 2-CH-E-2

12

The inspectors reviewed the licensee's repair efforts on plugging two

tubes and repairing one leaking plug.

The work was performed using

WO. 3800097306.

Corrective maintenance procedure MMP-C-CG-119,

Disassembly, Leak Detection, Repair, Reassembly of Non-Regenerative

Letdown Heat Exchanger-Safety Related, dated October 30, 1989, was

used for the repair.

The licensee used a mechanical plug rather than

the welded plug for the repair.

The use of the mechanical plug

decreased the radiation exposure. A problem was encountered when the

warehouse stock flexitalic gasket did not have the same dimensions as

those on the tubesheet.

Part of the old gasket had to be reused.

The inspectors will followup on this problem during the next

inspection period.

b.

Modification of 2-SW-MOV-205D

The inspectors monitored the licensee's activities associated with

the modification of 2-SW-MOV-205D HBC adapter and valve. * The

maintenance was accomplished in accordance with WO 380011483.

The WO

had an engineering transmittal attached that provided instructions

and specifications for performing this modification.

The inspectors

periodically visited the job site, and while at the job site reviewed

the WO, the post-maintenance test fa 11 ower, and the engineering

transmittal.

The purpose of this minor modification was to replace the screws that

secured the HBC adapter to the valve body with larger diameter cap

screws.

This was required because movement between the HBC adapter

and valve body was noted during operation of the valve.

More torque

could be applied to the larger cap screws to ensure that the HBC

adapter would remain secure to the valve body.

The modification

required removal of the Limitorque operator and HBC adapter, drilling

and tapping the valve body, enlarging the HBC adapter bolt holes,

reinstallation of the Limitorque operator and HBC adapter to the

valve body, and setting of the L imi torque operator switches and

stops. This same modification was performed on the 2-SW-MOV-205A, B,

and C valves and also on the 2-SW-MOV-204 A, B, C, and D valves.

The licensee considered the modification to be an equipment enhance-

ment and that the MOVs were operable in the as-found condition. This

was based on the MOVs satisfactorily passing their surveillance

tests, and that the previous condition, before the modification, did

not affect the valves ability to reposition to the open accident

position.

Unit 1 and 2 SW-MOV-204, and 205 valves and operators are

scheduled for replacement during the next refueling outages.

While monitoring the modification, the inspectors noted that the

contractors performing the work were not provided a SNSOC approved

procedure to accomplish the work, and that the WO was annotated that

a procedure was not required.

The inspectors reviewed VPAP-801,

Maintenance Program, Revision 1, Maintenance Program.

VPAP-801

provides guidelines that specify when procedures are required.

  • -

13

Although a SNSOC approved procedure was not available the craft were

working per the instructions of an engineering transmittal.

The

inspectors questioned the purpose of the engineering transmittal.

The inspectors were informed that the engineering transmittal

provided written guidance from maintenance engineering to . craft

personne 1 for performing the modi fi ca ti on, and that normally

engineering transmittals are *not utilized as procedures.

The

inspectors discussed the use of engineering transmittals as

procedures with the Maintenance Superintendent. The Maintenance

Superintendent considered engineering transmittals to be documented

instructions and therefore an acceptable procedure.

The inspectors

did not consider engineering transmittals as documented instructions

because station administrative procedures did not address the use of

engineering transmittals as an alternative to a SNSOC approved

procedure.

With minor modification in process for 2-SW-MOV-205D, the inspectors

ques1;:ioned why the craft was not utilizing an EWR to perform the the

work, and why an EWR was not approved prior to the performance .of the

modification.

The inspectors were informed that in order to

expedite maintenance, an EWR is prepared in parallel with or after

the.maintenance is completed.

The system that contains the modified

components is not declared operable until SNSOC approves the EWR that

documents the modification.

The inspectors concluded that station administrative instructions

SUADM-ENG-01, Engineering Work Request, Revision 1, and SUADM-ENG~13,

DCP/EWR Implementation and Closeout, Revision O, 'did not clearly

address the process of issuing an EWR in parallel with or after

completion of the work and that SNSOC approval of the EWR was

required prior to declaring the .system operable. This was discussed

with the Superjntendent of Engineering who stated that administrative*

procedures that govern modifications are currently being revised, and

that these issues would be clarified by the revisions.

The

inspectors reviewed EWR 90-272, revision K, MOV Modifications Surry.

1/2, and verified that SNSOC approval was obtained prior to the time

the recirculation spray system was required to be operable.

c.

Repairs to Check Valve 2-SI-85

The inspectors reviewed the work package for the open/inspect/repair

of check valve 2-SI-85. This maintenance was performed in accordance

. with WO 3800088856 and procedure 2-MPT-0417-04, Inspectipn of SI

.Check Valves 2-SI-79, 2-SI-82, and 2-SI-85, dated March 5, 1991.

  • Inspection of the valve internals revealed that valve seat and disc.

were worn.

The valve disc was replaced and the valve was

reassembled.

Replacement of the valve seat would have required

installation of a new check valve which was a significant increase in

the job scope and therefore not performed.

Other diffjculties

encountered during the maintenance was high, radiation dose rates and

water in the maintenance area.

Water in the maintenance area

e

14

prevented the mechanics from obtaining a satisfactory blue check.

The inspectors also reviewed the post-maintenance test requirements.

No discrepancies were noted.

On May 28, check valve 2-SI-85 was

satisfactorily seat leak checked.

The testing is discussed in

paragraph 5.b.

d.

Repairs to Valve 2-RC-95

As discussed in section 3.f of this report, attempts were made to

back seat 2-RC-95 to stop a valve packing leak. Subsequently, the

packing blew out resulting in entry into the emergency plan and the

declaration of a UE.

The µnit had to be taken to cold shutdown to

depressurize the leak for fepairs.

Even after reducing the pressure

to 15 psig the leakage was still approximately 15 gpm.

The licensee

was considering the use of a freeze seal to isolate the valve for

repairs.

The other alternative was to go into reduced inventory

since the valve was not isolable from the RCS loop.

In order for the

successful application of a freeze seal the licensee's procedure

required the flow rate in the area to be decreased *to less than 5

gpm.

To accomplish this,* the valve stem was turned in the shut

posit ion to reduced 1 eakage and system pressure was reduced to 15

psig.

After safety evaluation 91-146 was reviewed and approved by

the SNSOC, the freeze seal was accomplished by procedure

MMP-C-FS-260, dated April 24, 1991.

The inspectors reviewed the

freeze seal procedure and the safety evaluation.

Conments on the

freeze seal procedure in thi area of operations involvement with the

authorization to melt the seal and conments associated with the

1 i censee' s oversight of the freeze seal contractor were given to

plant management.

The freeze seal was installed and no leakage was noted when valve

2-RC-95 was disassembled.

Inspection of valve 2-RC-95 revealed that

the valve stem had separated from the disc. The licensee determined

that the valve is no longer needed for plant operations and a plant

modification was made that removed the internals from the valve and

blanked the bonnet.

The licensee determined that the valve stem and

disc were separated (unscrewed) when initial back seating operations

were performed to stop the valve packing leak.

The valve yoke

bushing prevented the stem from being ejected from the .valve.

The

licensee plans to have a failure analysis performed on the valve disc

and stem.

The Operations Department issued a shift order to establish the

following guidelines associated with valve operation:

The guidelines

were:

Do not use a valve wrench on any safety related valve.

If RCS leakage is identified, do not backseat the valve without

concurrence frol)1 both the Operation Manager on ca 11 and

engineering.

  • . *

15

Review of the failure analysis will be performed after the results

are received by the licensee.

Within the areas inspected, no violations were identified.

5.

Surveillance Inspections (61726 & 42700)

During the reporting period, the inspectors reviewed various surveillance

activities to assure compliance with the appropriate procedures as

follows:

Test prerequisites were met.

Tests were performed in accordance with approved procedures.

Test' procedures appeared to perform their intended function.

Adequate coordination existed among personnel involved in the test~

Test data was properly collected and recorded.

The following surveillances were either reviewed or observed:

a.

LHSI and Outside RS Testing

During surveillance testing on the Unit 2 LHSI pumps, 2-SI-P-lA and

2-SI-P-lB, and Unit 1 outside RS pump 1-RS-P-2A, the inspectors

noted, during review of the operator logs, that seal head tank low

level annunciators actuated.

The inspectors monitored the licensee's

corrective actions in response to the seal head tank low level

alarms.

The inspectors reviewed the seal designs and noted that each of the

LHSI and outside RS pumps contain an inboard and outboard seal.

The

purpose of the seals are to provide a pressure boundary so

radioactive fluid is not released into the safeguards building when

the pumps take a suction from the containment sump during accident

conditions.

The inboard seal cooling water is supplied from the

discharge of the pump and the outboard seal is cooled by the action

of a pumping ring and cooler unit.

The cooler unit (one for each

pump) is a closed loop filled with water.

The cooler unit contains a

seal head tank with high and low level switches and a cooling coil.

During pump operation, the pumping ring circulates water from the

area between the inboard and outboard seals through the cooling coil

and back to the area between the seals.

The seal head tank level

switch annunciator alarms in the control room.

Maintenance performed on the LHSI pumps' seal cooler units during the

refueling outage required that the systems be drained.

On April 20,

-

16

maintenance on the Unit 2 A LHSI pump seal cooler unit was completed.

The seal cooler unit was filled with water and the pump was

satisfactorily tested in accordance with 2-PT-18.1, LHSI Test and

Flushing of Sensitized Stainless Steel Piping, dated October 25,

1991.

On May 8, the Unit 2 A LHSI pump was again tested in

accordance with 2-PT-18.1.

When the pump was initially started, the

seal head tank annunciator alarmed and the pump was secured.

The

seal head tank was filled in accordance with the procedure and

operators restarted the pump.

The seal head tank annunciator again

alarmed and pump was secured.

WO 3800111182 was initiated to

troubleshoot the seal head tank low level switch.

The switch was

inspected but no problems were identified.

On the following day, the

seal head tank was refilled.

The Unit 2 A LHSI pump was started and

operated without the seal head tank low level annuciator alarming.

On May 21, the Unit 2 A LHSI pump was operated several times to

support reactor fill evolutions.

On one occasion the seal head tank

low level annuciator alarmed for several seconds and cleared.

On May

22, during the first two start attempts of A LHSI pump, the seal head

tank low level annunciator alarmed and the pump was secured. The seal

head tank was refilled in accordance with procedure and the pump was

restarted and operated without the seal head tank level annunciator

alarming.

The inspector noted that no DRs were initiated for the

above annunciated conditions.

On May 23, the Unit 2 B LHSI pump was started and secured because its

seal head tank annunciator alarmed.

In this case, however, a DR

{S-91-0779) was initiated.

Troubleshooting identified that air was

present in the pump's seal cooling system.

When the the LHSI pumps

were started the air in the cooling system would compress and level

in the seal head tank would decrease.

The system was designed to be

operated full of water.

The air was introduced when the system was

opened for maintenance during the refueling outage.

The system's

configuration is such that it is extremely difficult to vent the air

out while filling the system.

The Unit 2 LHSI pumps seal cooling

systems were vented and the pumps operated without the low level seal

head tank annunciator alarming.

The licensee considers that most if

not all of the air is out of the system and that the Unit 2 LHSI

pumps were operational.

On June 4, during the performance of Unit 1 surveillance test

1-PT-17.3, Containment Outside Recirculation Spray Pump, dated

February 1990, the seal head tank low level annunciator alarmed when

the containment outside RS pump 1-RS-P-2A was started.

The pump was

secured and the seal head tank filled in accordance with procedure.

The pump was restarted and operated without the seal head tank low

level annunciator alarming.

The pump was considered fully operable.

A DR was not initiated for this abnormal condition.

The inspectors

questioned why a DR was not initiated and if there was air in the

seal cooling system.

17

As a result of the inspectors concern with regard to seal head tank

operation, discussions were held on June 6 with the licensee.

The

inspectors were informed that the seal cooling systems for the Unit 2

LHSI and Unit 1 containment outside RS pumps were similar in

configuration and that air in the. system was the probable cause of

the June 4 seal head tank low level alarm that occurred on pump

1-RS-P-2A .. The inspectors were a 1 so informed that in February and

August of 1990 the seal head tank low level alarm annunciated on the

same pump.

In August 1990, DR Sl-90-1104 was initiated as a result

of the seal head tank low level annunciator alarming after the pump

was started.

The inspectors reviewed the corrective action assigned

to the DR.

The corrective action involved refilling the seal tank

when the alarm occurred and did not require any actions to

investigate the cause of the alarm.

A DR was not initiated for the

February 1990 alarm.

T~e licensee stated that pump 1-RS-P-2A was considered operable with

air in the seal cooling system because there was an adequate volume

of water in the seal cooling system to provide cooling to the pump

outboard seals.

The inspectors questioned what operators would do

during an accident when the outside containment RS pumps were started

and the seal head tank low level annuciator alarmed.

The inspectors

were informed that there was no specific guidance in this area and

the shift supervisor would have to make a judgement call on securing

the pump or continuing to operate it in the alarm condition.

The

inspectors consider that annunciation of the seal head tank low level

alarms during an accident would add unnecessary work and confusion

for the operators during a critical time.

The inspectors consider that the seal head tank low level annunciator

alarms on the Unit 2 LHSI pumps and the Unit 1 containment outside

recirculation pump 1-RS-P-2A were conditions adverse to quality that

were not promptly identified nor was adequate corrective action

initiated.

During the Unit 2 refueling outage the A LHSI seal head

tank annuciator alarmed numerous times.

DRs were not initiated to

document these conditions.

Also, seal head tank low level alarms

have occurred on pump 1-RS-P-2A and DRs were not always initiated to

document thes~.conditions.

When a DR was issued to document a low

level alarm on pump 1-RS-P-2A, the corrective action was inadequate

to prevent reoccurrence.

Failure to promptly identify or correct the conditions adverse to

quality associated with the seal head tank low level alarms is

identified as a violation of 10 CFR 50, Appendix B, Criterion XVI

50-280, 281/91-14-02, Fai 1 ure to Identify and Correct Conditions

Adverse to Quality.

b.

Event V Pressure Isolation Valve Seat Leak Testing

TS 3.1.c.7a and TS Table 4.1-2A, item 18 specifies test frequency and

seat leak rate limits for Event V pressure isolation valves SI-79,

18

SI-241, SI-82, SI-242, SI-85, and SI-243.

On May 28, the inspectors

monitored portions of the seat leak testing accom~lished on Unit 2

check valves 2-SI-79, 2-SI-82, and 2-SI-85.

The inspectors also

reviewed the completed copy of 2-PT-18.11, SI Cold Leg Check Valve

Leakage-Primary Coolant System Pressure Isolation Valves, dated June

5, 1990. Results of this review indicated that individual leak rates

in lieu of combined leakage rates were obtained, leakage rates

obtained at lower than normal operating pressure were normalized,

and all procedure calculations were correct.

No discrepancies were

noted.

c.

Control Rod Drop Testing

On June 5, 1991, the inspectors witnessed portions of 2-PT-7.1, Cold

Rod Drops, dated May 28, 1991.

The purpose of this test was to

ensure rod freedom after the cooldown of Unit 2 for repairs to valve

2-RC-95.

The licensee elected to perform this test during hot

shutdown conditions and a PAR was issued on May 30, 1991, to allow

this.

Additionally, the safety evaluation to allow continued

operations during cycle 10 with rod M-12 stuck was modified to

recognize that rod freedom testing could be performed either hot or

cold but prior to criticality.

Equipment performed as expected and

no discrepancies were noted.

Within the areas inspected, one violation was identified.

6.

Licensee Event Report Review

(92700}

The inspector reviewed the LER's listed below to ascertain whether NRC

reporting requirements were being met and to evaluate initial adequacy of

the corrective actions.

The inspector's review also included followup on

implementation of corrective action and review of licensee documentation

that all required corrective actions were complete.

(Closed}

LER 280/91-04, Two of Three Emergency Diesel Generators

Inoperable.* The issue involved a tagout of one of the two redundant fuel

oil transfer pumps for an EDG which was required to be fully operable

based on plant conditions at the time.

This event was addressed in

Inspection Report 280,281/91-10 and an NCV was identified in that report.

The inspector reviewed licensee actions at that time and also reviewed

additional corrective actions addressed in this report. Licensee correc-

tive actions appear to be adequate.

(Closed} LER 280/91-06, Unit 1 Auxiliary Feedwater System Cross-Connect

Capability From Unit 2 Inoperable In Excess of Technical Specifications

Allowed Time Due to a Drawing Error.

The issue involved an incorrect

configuration condition for underground suction line for a safety-related

  • AFW pump.

This event was addressed in Inspection Report 280,281/91-10 and

an NCV was identified in that report.

The inspectors reviewed the

licensee actions at the time of the event and also reviewed the corrective

,,

19

actions addressed in this report.

Licensee corrective actions appear to

..

be adequate.

Within the areas inspected, no violations were identified.

7.

Evaluation of Licensee Self-Assessment Capability (40500)

During this inspection period, the NRR project manager for Surry conducted

a review of the licensee's program for the screening of plant ~hanges, and

proposed tests and experiments* to determine if a safety evaluation is

required and the process for preparing, reviewing, and approving safety

evaluations.

This review focused on the testing of main steam safety

valves accomplished during the past 12 months.

In October, 1990, testing of the Unit 1 main steam safety valves lift

setpoints was performed using the Furmanite Trevitest method.

Similar

testing of the Unit 2 main steam safety valves at approximately 70 percent

of rated power was conducted in March, 1991.

The licensee has previously

performed a 10 CFR 50.59 safety evaluation dated October 2, 1990, which

concluded 'that testing of the above cited safety valves at power did not

present an unreviewed safety question. A review of the safety e'valuation

showed that it was prepared using the then current. Surry Power Station

Procedure SUADM-LR-12 which has subsequently been superseded by*Station

Administrative Procedure No. VPAP-3001 dated April 1, :*1991.

The safety

evaluation referenced the steamline break analysis in Section 14.3.2 of

'the Station UFSAR.

Section 14.3.2 of the UFSAR indicated that if a safety

valve were to inadvertently stick open, the most severe transient would

occur at zero load without unacceptable consequences.

The analysis.

assumed, among other things, a steam release rate of 247 pounds per hour

which is equal to or greater than the relief capacity of any single dump

or main steam safety valve and the results indicated compliance with the

design basis as defined in the UFSAR.

The inspection concluded that the

analysis was procedurally correct and supported the lic.ensee's findings

that testing of the main steam line safety valves at power would not

constitute an unreviewed safety question.

Also, the inspector concluded

that the licensee's analysis methodology is in compliance with the

licensing basis as described in the UFSAR.

Within the areas inspecte~, no violations were identified.

8. *Exit'Interview

The inspection scope and results were sununarized on June 11, 1991 with

those individuals identified by an asterisk in paragraph 1.

The following

sununary of inspecti_on activity was discussed by the inspectors during .this

exit.

Item Number

VIO 50-280,281/91-14-01

Description and Reference

Failure .to provide adeq~ate procedures

and/or instructions with two examples.

.,

.

'

20

a. Inadequate implementation of a

waste gas decay tank TS.

(paragraph 3.a)

b. Inadequate turbine operating and

testing procedures.

(paragraph 3.c)

VIO 50-280,281/91-14-02

Failure to identify and correct

conditions adverse to quality. (paragraph

5.a)

Licensee management was informed of the strengths and weaknesses

identified in paragraph 3 and of the items closed in paragraph 6.

The licensee acknowledged the inspection conclusions with no dissenting

comments.

The licensee did not identify as proprietary any of the

materials provided to or reviewed by the inspectors during this

inspection.

9.

Index of Acronyms and Initialisms

AFW

CCW

CFR

CRO

DR

EOG

ESF

EWR

F

GL

GPM

LER

LCO

LHSI

MOV

MWE

NCV

NOUE

NRC

NRR

PAR

POTT .

PSIG

PORV

RC

RCS

RHR

RS

AUXILIARY FEEDWATER

COMPONENT COOLING WATER

CODE OF FEDERAL REGULATIONS

CONTROL ROOM OPERATOR

DEVIATION REPORT

EMERGENCY DIESEL GENERATOR

ENGINEERED SAFETY FEATURE

ENGINEERING WORK REQUEST

FAHRENHEIT

GENERIC LETTER

GALLONS PER MINUTE

LICENSEE EVENT REPORT

LIMITING CONDITIONS OF OPERATION

LOW HEAD SAFETY INJECTION

MOTOR OPERATED VALVE

MEGAWATT ELECTRICAL

NON-CITED VIOLATION

NOTICE OF UNUSUAL EVENT

NUCLEAR REGULATORY COMMISSION

NUCLEAR REACTOR REGULATION

PROCEDURE ACTION REQUEST

PRIMARY DRAIN TRANSFER TANK

POUNDS PER SQUARE INCH

POWER OPERATED RELIEF VALVE

REACTOR COOLANT

REACTOR COOLANT SYSTEM

RESIDUAL HEAT REMOVAL

RECIRCULATION SPRAY

,I

21

RTD

RESISTANCE TEMPERATURE DETECTOR

RWP

RADIATION WORK PERMIT

SRO

SENIOR REACTOR OPERATOR

SI

SAFETY INJECTION

SNSOC

STATION NUCLEAR AND SAFETY OPERATING COMMITTEE

SW

SERVICE WATER

TS

TECHNICAL SPECIFICATIONS

UFSAR

UPDATED FINAL SAFETY ANALYSIS REPORT

UE

UNUSUAL EVENT

UT

ULTRASONIC TEST

VPAP

VIRGINIA POWER ADMINISTRATIVE PROCEDURES

WGDT

WASTE GAS DECAY TANK

WO

WORK ORDER