ML18152A104

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Insp Repts 50-280/90-01 & 50-281/90-01 on 900101-0203. Violations Noted.Major Areas Inspected:Routine Resident Insp of Plant Operations,Maint,Surveillance,Ler Review,Action on Previous Insp Findings & Installation & Testing of Mods
ML18152A104
Person / Time
Site: Surry  Dominion icon.png
Issue date: 03/02/1990
From: Fredrickson P, Holland W, Larry Nicholson, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A105 List:
References
50-280-90-01, 50-280-90-1, 50-281-90-01, 50-281-90-1, NUDOCS 9003200281
Download: ML18152A104 (21)


See also: IR 05000280/1990001

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos.:

50-280/90-01 and 50-281/90-01

  • Licensee:

Virginia Electric and Power Company

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

Facility Name:

Surry 1 and 2

License Nos.:

DPR-32 and DPR~37

Inspection Conducte~:

  • January 1 - February 3, 1990

Inspectors:

W. 6o~nioR.sTuent Inspect

.Approved by:

Scope:

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J. W~ ~'sicrent Inspector

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L. E.Nic~o~sident Inspector

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P. E. Fredrickson. Section Chief

Division of Reactor Projects

SUMMARY

3)-Po

Date Signed

l-/-90'

Date Signed

3-/- ~t)

Date Signed

3 *-Z-cfc'J

Date Signed

. This routine resident inspection was conducted on site in the areas of. plant

operations. plant maintenance, plant surveillance, licensee event report

review, action on previous inspection findings. installation and testing of

modifications, and. evaluation of licensee self assessment capability.

Backshift and weekend tours were conducted ori January 6; 7. 15. 18. 21, *28 *. and

February 3.

Results:

During this inspettion period~ no violations or deviations we~e i~entified. A

strength was identified with regards to the licensee's propo?ed program and

schedule for conducting future safety assessments of major areas at the Surry

Power Station (paragraph 9).

  • However, weaknesses were identified in several

functional

areas

including operations. maintenance/surveillance,

and

engineering/technical support. These weaknesses were~

The licensee's actions for ens~ring that operations has good capabilities

to determine RCS leak rates have not occurreq in* a timely manner

(paragraph 3.d).

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ADOCK 6§666~80

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2

A weakness was identified regarding inadequate maintenance practices

involved in repairing a main feed water pump bearing lubrication system

(paragraph 4.a)~

Deficiencies in planning and procurement activities were identified as

weaknesses in the maintenance/surveillance area (paragraph 4.c).

Another example was identified of a weakness previously documented in

Inspection Report 280, 281/89-34 concerning a lack of aggressive identifi-

cation and evaluation of anomalies that occur during surveillance testing

(paragraph 5.a).

An NCV concerning the resin facility project and modification of a

recirculation spray pump was identified as a failure to provide and/or

follow procedures for plant modifications (paragraph 8). These items are

considered to be an indication of a weakness in the control and testing

process of plant modifications.

During closeout of LER 280/89-41, an NCV was identified for failure to meet the

requirements of TS 3. 22 when taking a safety-related fan out of service

(paragraph 6).

During closeout of LER 281/89-12, an NCV was identified for failure to comply

with the requirements of TS 3.12.E (paragraph 6).

1.

Persons Contacted

Licensee Employees

REPORT DETAILS

  • W. Benthall. Supervisor. Licensing

R. Bilyeu. Licensing Engineer

    • D. Christian. Assistant Station Manager

D. Erickson. Superintendent of Health Physics

      • E. Grecheck. Assistant Station Manager
  • D. Hart. Supervisor. Quality. QA Department
    • M. Kanslef. Station Manager
  • A. Keagy. Supervisor of Station Materials

T. Kendzia. Supervisor. Safety Engineering.

  • J. McCarthy. Superintendent of Operations
  • J. Ogren. Superintendent of Maintenance
  • S. Sarver. Superintendent of Planning
  • T. Sowers. Superintendent of Engineering
    • E. Smith. Site Quality Assurance Manager
  • NRC Employees
  • R. Mussei, Resident Inspector. RII
  • S. Shaeffer. Project Engineer. RII
  • Attended exit interview on Feb.ruary 6, 1990.
    • Attended exit interview on February 9, 1990.
      • Attended both exit interviews.

Other licensee employees contacted included control room operators. shift

technical advisors. shift supervisors and other plant personnel.

Ort January 11. 1990 a manageme~t meeting was held at the Surry Power

Station in order for Virginia Power to provide a progress update to NRC

regional and headquarters personnel on issues of mutual interest.* NRC

management in attendance at the meeting were:

S. Ebneter, Regional Administrator. RII

H. Berkow. Director. Project Directorate II-2. NRR

M. Sinkule. Branch Chief. DRP. RII

B. Buck1ey. Project Manager. NRR

The meeting focused on recent management and staffing changes; current

plant status; corporate support services updates; corporate engineering

and technical support updates; station radiological. operations. and

maintenance updates; and a quality assurance update.

Acronyms and initialisms used throughout this report are listed .in the

last paragraph.

2.

. 2

Plant Status

Unit 1 began the reporting period at power.

The unit operated at power

for the duration of the inspection period.

Unit 2 began the reporting period at power.

The unit operated at power*

for the duration of the inspection period~

3.

Operational Safety Verification

(71707 & 42700)

a.

Daily Inspectibns

The inspectors conducted daily inspections in the following areas:

control room staffing. access. and operator behavior;. operator

adherence to approved procedur~s. TS. and LCOs; examination of panels

containing instrumentation and other reactor protection system

elements to determine that required channels are operable; and review

of control room operator logs. operating orders. plant deviation

reports. tagout logs. jumper logs. and tags on components to verify

compliance with approved procedures.

The inspectors also routinely

accompanied station management on plant tours and observed the*

effectiveness of their influence on activities being performed by

plant personnel .

b.

Weekly Inspections

c.

The inspectors conducted weekly inspections in the followin~ areas:

verification of operability of se.lected ESF systems _by valve

  • alignment. breaker posit ions. condition of equipment or component.

andoperability of instrumentation and support items essential to

system actuation or performance~

Plant tours were

conducted which

included observ_ation of general plant/equipment conditions. fire

protection* and preventative measures. control of activities in

progress. radiation protection controls. physical security controls.

plant housekeeping conditions/cleanliness. and missile hazards.

The

inspectors routinely monitored the temperature of the AFW- pump**

discharge *piping* t_o ensure increases in temperature were being

properly monitored and evaluated by the licensee.

Biweekly Inspections

The inspectors conducted biweekly inspections in the following areas:

verification review and walkdown of safety-related tagouts in effect;

review of sampling program (e.g .* primary and secondary coolant

sam~les, boric acid tank s~mples *. plant liquid _and gaseous samples);

observation of .control room shift turnover; review of implementation

of the plant problem identification system (deviation reports);

verification of selected portions of containment isolation lineups;

and verification that notices to workers are posted as required by 10 .

CFR 19.

.

,

,,:

3

. * d.

Other Inspection Activities

Inspections included areas in the Units 1 and 2 cable vaults. vital

battery rooms. steam safeguards areas, emergency switchgear rooms. *

diesel generator rooms. control room. auxiliary building. cable *

penetration areas. independent spent fue 1 s torag*e f ac i 1 ity. 1 ow 1 eve 1

intake structure. and the safeguards valve pit and pump pit areas.

RCS leak rates were reviewed to ensure that detected or suspected

leakage from the system was recorded. investigated. and evaluated;

a~d that appropriate actions were taken. if required.

The inspectors

routinely and independently calculated RCS leak rates using the NRC

Independent Measurements Leak Rate Program (RCSLK9).

on* a regulaf

basis. RWPs were reviewed* and specific work activities were mon,tored

to assure they were bei~g conducted per the RWPs.

Selected radiation

protection instruments were periodically checked, and equipment*

_operability and calibration frequency were verified.

During this. period* the inspectors specifically focused on the

licensee's surveillance procedure which is performed on a daily basis

to determine RCS leak rates.

This review was conducted based on

recent unexplainable variances in reported leak rates for Unit 1. It

should be noted that at no time were leakage rates identified which

were close to TS limits; however. if leakage had increased on the

unit during this period. it may have been difficult to insure that TS

r~quirements were being met.

The survei 11 ance procedure~ PT-10, "Reactor Cool ant Leakage" revision

dated October 17. 1989 was reviewed by the inspector. It

was noted that the procedure had one temporary change attached which

corrected an incorrect density conversion.

The inspector also noted

that the procedure required the operator: to perform numerous

calculations with a hand calculator to average RCS temperatures and

pressurizer levels from different channels.

In addition. curve books

had to be used to determine equivalent tank levels and. numerous

calculations were required to convert different variables for

temperature differences.

The inspector discussed the described conditions with operations

supervision and other station management and questione*d whether any

actions were warranted. *The operations superintendent discussed the

same concerns with corporate engineering in the presence of the

inspector and requested that additional review of the procedure be

conducted in order to provide a more* user friendly product.

The

inspectors. as noted above. have had .the capability to run

independent leak rate calculations on the NRC personnel computer for

several years.

The licensee has incorporated a computer leak rate

program on to the plant's computers.

However, during this review;

these computers were not being used by the operators to perform leak

rate determinations.

This was due in part to the computer programs

needing a revision to correctly provide for density compensation.

In

addition. the SNSOC had not authorized normal use of the pl ant

  • .';.,:

....

computer for leak rate determination <;iue to the process not being

under the control of the QA program.

At the end of the inspection

period, the licensee corretted and authorized operations use of the

plant computers for calc.ulation of leak rates.

However. the

inspector noted that due to leakage into the PRT on Unit 1. the

computer was not providing_the required accuracy in leak rate. This

condition . required that the operators continue to use the hand

calculation method to determine leak rates. The inspector considers

that the licensee's actions for ensuring that tiperation~ has good

capabilities to determine RCS leak rates havenot occurred in a

timely manner.

e.

Physical Security Program Inspections

In the course of monthly activities. the inspectors included a review

of the 1 i censee I s phys i ca 1 security program.

The. performance of

various shifts of the security force was observed in the *conduct of

daily activities to .include: protected and vital areas access

contro 1 s; searching * of personne 1 * packages and veh i c 1 es; badge

issuance and retrieval;_escorting of visitors; and patrols and

compensatory posts.

Within the areas inspected~ no violations were identified.

4.

Maintenance Inspections (62703 & 42700)

During the reporting period, the inspectors reviewed maintenance

activities to assure compliance with the appropriate procedures.

Inspection ~reas included the following: *

a.

Main Feedwater Pump - Unit 2

On January 6. 1990, the inspector observed repairs being performed

on main feedwater pump 2-FW-P-lB.

Unit 2 had been ramped down to

less than 70% power in order to accomplish this activity.

The

maintenance activity was being conducted in order to determine why

excessive oil was leaking from oil lubricated bearings located

between the motors.

It should be noted that this component-had been

overhauled and reassembled during the refueling outage that had ended

in September 1989.

The current work was being performed under work

order number 3800090321 and to procedure number EMP-C-EPH-113.

Feedwater Pump Motors 1Bl and 1B2. 4160 Volts MFWP Motor Disassembly,

Repair. and Reassembly.

The cause of the leak was determined to be the result of a bolt that

was missing out of the inner seal on the inboard bearing of the

inboard motor.

The design of this bearing is such that the bolt

penetrates into the oil reservoir and; therefore. if the bolt is not

installed. a direct leakage path would occur.

Inspection of the

maintenance area by the craft determined that no bolt was present

which could have worked its way out of the bearing cap and dropped

5

beneath the motor during operation.

In a~ditfon. a second bolt w~s

found missing on the inner seal of the inboard bearing of the

outboard motor.

The inspector reviewed the work package and discussed this condition

with the maintenance craft supervision.

Based on this review. the

inspector concluded that the missing parts were a result of

inadequate maintenance practices and/or control Of work during the

refueling outage.

However, discussion with supervision indicated .

that the licensee did review this work with regards to insuring that

weak work practices were corrected.

The inspector considers that

this maintenance activity identified a weakness in the way some

balance of plant components were worked during the past refueling

outages.

b.

Main Feedwater Pump-Unit 1

. On January 7. 1990. the i,nspector observed a repair weld being.*

  • performed on the suction vent line to pump casing on main feedwater

pump 1-FW-P-lA.

This pump had developed a pin hole leak during

operation at the.interface of the socket weld and base metal.

The weld procedure and certain stages of the welding were reviewed

during the repair process.

The work was performed under work order

number 3800089113.

No discrepancies were id~ntified.

-

c.

Review of Maintenance Activities which Affect Plant Operations

During this inspection period. the inspector focused on two

maintenance activiti~s which were having a dir~ct affect on Unit 1

operations.

The first item was related to operations personnel

having to take administrative control of a cross-connect valv~ in the

  1. 1 EOG room for the filling of one train of air bottles from the.

opposite trains air compress~r. This operator action was

required at least daily since late October 1989.

The inspector

reviewed the maintenance activity which was causing this action and

determined that work on* a discharge check valve which had been

removed for corrective maintenance on one of the two EOG air bank'~

air compressors was waiting on material for repair.

The check valve

(Ol-EG-42) had been tagged out.for maintenance on October 22, 1989.

Aft~r removal and inspection of the valve, engineering redesigned the

valve application.

This redesign required that material be procured

to complete the modification -of the valve.

The material. 2 1/2"

round stock. was ordered through the procurement system on a material

requisition on December 1. 1989.

The requisition was processed in a

normal manner with an expected date of delivery of February 14. 1990.

The inspector could not determine if any effort was made to expedite

the material; however. after identification. of this item as an area

of interest in the latter part of the inspection period. the

inspector noted that this material request was receiving additional

followup action by the licensee.

After talking to the operations

coordinator in the maintenance/planning area on January 31, 1990, the

6

inspector was informed that the requested material would be received

later that same day.

The inspector considers that the operations

coordinator wa~ supplying operations priorities to o~tstanding work

orders. however. the planning process did not allow for proper

c6nsideration of all outstariding work.

After talking to additional

management later that same day. the inspector learned that the

~aterial -ordered was not certified for its intended application and

would have to be reordered.

The correct material was reordered that

same day and was received within two days.

The inspector noted that

the subject check valve was repaired and reinstalled in the #1 EOG

air start system befor~ this inspection period ended.

.

.

.

.

.

.

  • A second item. related to work associated with the correction of an

indicated ground condition on the Unit 1 B vital battery bus also

indicates a lack of prioritization and planning of maintenance

activities.

The _indicated ground was displayed in the control room

and identified by operations as a problem by work request 088416

dated November 29. 1989.

The inspector determined that the work to

troubleshoot this ground condition was authorized on December 12.

1989.

After identification of this item as an area of interest in

~he latter part of the inspection period, the inspector noted that

this item was receiving additional licensee attention. The inspector

was informed on January 22. 1990. that the ground had been traced to

one of the two vital battery chargers. Addi.tional procedures had to

be prepared to continue the troubleshooting of the ground.

When the

inspection period ended. the ground condition and its indication in

the control room still existed and maintenance was preparing to

continue troubleshooting after operations established required

conditions in accordance with the new procedure.

The inspector selected the two proceeding activities to follow up on

due to the concern that these activities either required operations

to take administrative actions in order to compensate for

out-of-service equipment or that operators did not have available

indicaticin in the control room.

The inspector considers that after

NRC involvement. the corrective action for each of these jobs

appeared to move towards resolution faster.

Several problems were

noted during review of each of the maintenance activities.

These

problems included lack of prioritization and good planning for the

maintenance activities and a lack of effective followup on procure-

ment of materials for safety-related work.

The inspectors

conclusions wer~ di~cussed with management and there was agreement

that the planning and procurement activities at the station needed

additional management attention. Planning and procurement activities

deficiencies

were

identified

as

weaknesses_ in

the

maintenance/surveillance area.

Within the areas inspected. no

vicilations were identified.

5.

Surveillance Inspecticins

(61726 & 42700)

During the reporting period. the inspectors reviewed various surveillance

. **

7

activities to assure compliance with the appropriate procedures as

follows:

Test prerequisites were met~

Tests were peiformed in accordance with approved procedures;

Test procedures appeared to perform their intended function.

Adequate coordination existed among personnel involved in the test.

Test data was properly collected and recorded.

Inspection areas included the following:

a.

b.

Auxiliary Feedwater (AFW) Test.

On January 4. the inspectors witnessed a routine monthly test and a

special full flow test of the Unit 1 AFW system in accordance with

procedures 1-PT-15.lC and 1-ST~273.

The first test involved a normal

demonstration of operability of the turbine driven AFW pump l-FW-P-2.

The inspector independently verified that the pump performance was

within the specified acc~ptance criteria .

The second test (1-ST-273) was performed to ~btain trendtng data for

AFW full flow to each steam generator from the AFW pump 1-FW-P-2 with

and without the use of the AFW booster pumps 1-FW-P-4A & B.

Although

the booster pumps are not required by TS. they could provide an * *

alternate source of feed water from the emergency condensate make-up

tank.

This test successfully demonstrated that full flow to the

steam generators could be achieved with the booster pumps aligned to

the suction of the AFW pumps. * The 1 i censee is considering

performance of this test on*a quartefly basis.

The inspector witnessed the test and noticed that the turbine casing

relief valve was lifting during the test and blowing steam into the

space.

This discrepancy was not annotated on the applicable* test

critique form nor was a station work request submitted until

questioned* by the inspector.

This appears. to be an additional

  • example of a weakness previously documented in Inspection Report 280.

281/89-34 regarding a lack of aggressive identification and evalua-

tion of anomalies that. occur during testing.

The licensee had

  • internally tasked the operations superintendent to evaluate this

weakness by January 30. 1990.

This latest example further indicates

that action is warranted to enhance the surveillance program.

Charging Pump - Unit 2

On January 10. 1990, inspector witnessed the running of charging pump

2-CH-P-lB in accordance with periodic test 2-PT-18.7. Chargirig Pump

Operability and Performance Test, dated October. 19, 1989. - This

8

surveillance was being accomplished to demonstrate the operability of

the charging pump following maintenance.

The rotating*assembly for

this pump had been replaced thereby altering the pump performance.

The inspec*tors also reviewed EWR No.90-033,. Evaluate CH Pump

Reference Valves. which evaluated the new discharge and vibrational

dat~.

The testing demonstrated satisfactory operation with regards

to flow~ head. and other required parameters.

No deficiencies were

.noted.

Within the areas inspected. no violations_ were identified.

6.

Licensee Event Report Review

(92700) *

The inspecto~s reviewed the LER's listed below to ascertain whether NRC

reporting requirements were being met and to determine -appropriateness -of

the corrective actionsr The inspector's review also iricluded followup on

implementation of corrective action and review of licensee documentation

  • that all required corrective actions were. complete.

LERs that identify violations of regulations and that meet the criteria of

10 CFR. Part 2. Appendix C.Section V are be identified as NCVs in the

following closeout para~raphs~

NCVs are considered first-time occurrence

violations which meet the NRC Enforcement Policy for exemption from

issuance of a Notice of Violation. These items are identified to allow

for proper evaluations of corrective actions in the event that similar

events occur in the future.

(Open) LER 280/89-37.

11A

11 S/G Header to Line SI Channel IV Declared

Inoperable Due to Malfunctioning Pressure Comparator. This issue involved

a failure of the subject comparator.

Corrective action for the failure

included replacement with a shop spare and testing after installation.

However. approximately 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> after the instrument wa-s returned to

  • service. the comparator failed again.

After the second replacement. the

instrument channel worked satisfactorily.

Part of the licensee's correc-

tive actions included a -commitment to review the repair and testing

methods associate_d with module refurbishment in the shop.

During* this

inspection period. a licensee QA audit of instrument maintenance

identified a finding with regards to traceability of electronic components

.. not being maintained.

Specific concerns in the finding related to

instructions not being provided for the repair of process modules.

traceability of the e 1 ectroni c components. and storage of the electronic

components.

The audit (S89-25) was is$ued on January 31. 1990.

The

inspector reviewed the audit finding and will review the licensee's

response and implementation of corrective actions prior to closeout of

this LER.

(Closed) LER 280/89-38. Unplanned Engineered Safety Features Component

Actuation. Auto Start of #3 EOG While Attempting to Shut Down Due to

Existing Hi Hi CLS Signal.

The issue involved an auto start of the #3 EDG

due to an existing CLS signal in the circuitry that had been initiated

9

earlier for special testing and never cleared.

The ilearing of the CLS

signal required tightening of a loose termin~l screw and resetting-of the

hi hi CLS signal.

The EOG was then returned to its automati~ mode of

operation.

This event and licensee corrective action was discussed in

Inspection Report 280. 281/89-28. This LER is closed.

(Close*d) LER 280/89-39.

11A

11 Steam Generator Header to Line Differential

Pressure Input to SI inoperable Due*to Malfunctioning Relay Contact.

The

issue involved a failure of the subject relay contact which was

contrary to the requirement of TS Tab1e 3.7-2. Corrective action included

connection of the leads affected to spare contacts on the relay and

satisfactorily testing of the modification.

In addition. the affected

drawings were revised to indicate the new lead contact locations.

The

inspector verified that corrective actions were ac~omplished.

(Closed) LER 280/89-40. Unplanned ESF Component Actuation~ TV-VG-109A

Failed Closed Due to Loose Connections in the Close Switch.

The issue

involved inadvertent closure of the subject valve due to a loss of

continuity in the electrical circuit to the trip valve

1s solenoid operated

air supply valve.

The valve had failed in its safety position.

Corrective action included tightening loose connections in the circuitry.

~nd satisfactorily testing of the valve.

The in~pector verified that the

corrective actions were accomplished. This LER is closed.

(Closed) LER 280/89~41. Auxiliary Vent Fan Taken.Out of Service Without

Implementing Technical Specification Action Statement Due to Personnel

Error.

The issue involved improper operator action with regards to

entering TS action statement 3.22 when taking a safety-related fan out of

service for maintenance.

The fan was determined to be out of service for*

approximately 30 minutes during the maintenance activity.

However. the

defi~iency was not discovered until after the fan had been ret~rned to

service.

Corrective actions to prevent recurrence which were implemented

by the operations superintendent included issuance of a memorandum to all

operations shift supervisors directing that safety-related equipment be

considered inoperable when their controls are pl~ced in the pull-to-lock

position.* The inspector revi~wed the corrective action arid discussed the

requirement with several SROs on shift.

The inspector considers -that

proper understanding of the requirement .is evident based on these discus-

sions.

This item is identified as an NCV (280/90-01-01) for failure to

meet the requirements of TS 3*.22 when taking a safety-related fan out of

service. This LER is closed.

(Closed) LER 280/89-42. Leakage Through Fault in Letdown System Drain Line

in Excess of Allowable Type

11C

11 Leakage.

The ;ssue involved identifica-

tion of RCS leakage through a crack in a fillet weld ori a socket tee

connecting a drain line to the letdown li.ne inside containment.

The

leakage point was between the inside containm-ent isolation valves and the

containment wall resulting in a containment integrity concern.

Immediate

corrective action included isolation of letdown to reestablish containment

integrity.

Additional corrective action included weld repair of the

10

1 eakage area and return to service of norma 1 1 etdown.

The inspector

verified that corrective actions were accomplished.

This LER is closed.

(Closed) LER 281/89-06, -Unplanned ESF Component Actuation, Closure of

Containment Isolation- Valve Due to Containment Particulate Radiation .

Monitor Alarm.

The issue involved the closure. of the containment

instrument air isolation valves due to the subject ala.rm.

This event was

discussed in inspection report 280. 28i/89-28.

The residents monitored

licensee evaluation and actions during that period *. This LER is closed.

(Closed) LER 281/89-08. Unplanned Engineered Safety Features Component

Actuation, Closure of TV-IA-201B Due to Loose Control Power Fuse.

The

issue involved identification of closure of th~ subject valve by operators

during control room board walkdowns.

Corrective action included identifi-. *

cation of a loose fuse in a fuse block which provided foi control power to

allow the valve to open.

The fuse block terminal clips had loosened

around the control power fuse~

A temporary modification was implemented

to correct the problem and a new fuse block was ordered.

Instrument air

was restored to the valve and the valve was returned to ~ervice after

te~ting.

The inspector reviewed the event and corrective actions.

This

  • LER is c 1 osed.

(Closed) LER 281/89-09, Turbine Trip/Reactor Trip Due to 86 BU Trip Caused

by Spurious Actuation of KD-41 Relay.

The issue involved a reactor trip

from approximately 14% power due to a faulted relay in the turbine

generator electrical circuitry protection system.

After the trip all

safety systems performed as *designed.

This event was discussed in

Inspection Report 280. 281/89-28. This LER is closed.

(Closed) LER 281/89-10, Reactor Trip Due to Low Ste~m Generator Level

Following a Higher Than Expected Load Increase During Unit Startup.

The

i.ssue involved an automatic reactor trip from approximately 25% power due

to low low steam generator level which was caused by a rapid load increase

on the unit.

After the trip all safety systems performed as designed.

This event was discussed iri Inspection Report 280, 281/89-28 and

identified a weakness in operator control of the EHC system.

This LER is

closed~

(Closed) LER 281/89-11. Containment Integrity Violated Due to Containment

Penetration Being in an Unanalyzed Condition.

  • The issue involved

identification of an improper ~ipe support for a Unit 2 containment piping

penetration.

This event. including corrective actions. was fully

discussed in Inspection Report 280. 281/89-28. This LER is closed.

(Closed) LER 281/89-12. Individual Rod Position Indicators Out of

Specification For Greater Than 60 Minutes in a 24 Hour Period.

The issue

involved two !RPI in control bank A differing from the bank

1s step demand

position by more than 12 steps for greater than 60 minutes which is in

violation of TS 3.12.E. Corrective action included adjustment of the !RPI

to within limits in the next 15 minutes.

The cause of the violation was

attributed to improper control of logging of times the rods differ from

11

the requirement.

Additional corrective actions to prevent recurrence

included computer modification to alarm prior to exceeding 60 minutes and

modification of the logging procedure. This event is identified as an NCV

(281/90-01-02) for failure to comply with the requirement£ of TS 3.12.E.

This LER.is closed.

Withiri the areas inspected. no violations were identified.

1~

Action on Previous Inspection Findings

(92701. 92702)

a.

(Closed) IF! 280. 281/88-28-03. Review of Testing of CCW Heat

Exchanger Service Water System.

This issue stemmed from the concern*

that the component cooling heat exchangers (CCWHX) may not be able to

remove the necessary heat during certain worst case scenarios.

Inspection Report 280. 281/88-14 identified the initial concern over

. the use of vacuum priming to maintain service water flow. with

additional. inspection documented in Inspection Report 280. 281/88-51.

The inspector reviewed test data and calculations contained in the

  • fol lowing documents:

Special Test 243. CC Heat Ex"changer Water Box Level Test.

Ca lcul a ti on ME-207. Opera bi 1 i ty Parameters of the Component

Cooling Heat. Exchangers.

Calculation ME-0222. Addendum 1. Component Cooli~g Water Heat

Transfer Operability Criteria.

Special Test 41A. 1-CC-E-lA Operability Check.

The inspector concluded* that adequate heat transfer capabi 1 i ty had

been demonstrated and is being maintained.

The original concern was

  • mitigated somewhat by the raising of the minimal intake canal leve.l * .*

set~oint.

In_addition. the licensee is turrently replacing the heat.

exchangers and improving the instrumentation available to monitor

their performance. Thii !FI is considered closed.

  • b.

(Closed) . !FI 280~ 281/89-06-04. Review of audits and weaknesses

concerning drawings and design change contra l .

The inspectors

identified a weakness regarding the licensee method for tracking and

completing *drawing. revisions that are identified- outside the formal

design change process.

For example. drawing discrepancies noted

during operator walkdown of the plant systems were annotated on a

drawing change request form with no unique number or formal tracking

method.

The licensee has since issued a revision to the applicable

  • station administrative procedure* that requires a drawing .change

request nu~ber be assigned to each request as it is submitted.

A further concern was identified regarding the absence of any

prescribed time frame for correcting drawing discrepancies* that are*

identified as noted above.

The licensee has instituted a policy to


----

12

. correct drawing discrep~ncies on a similar time frame as required for

design changes. * This policy was being fully implemented in

procedures as the inspection period ended.

The inspector reviewed

a 11 1 i censee actions taken as a result of the above concerns and

consider them adequate.

A review of the completed Quality Assurance audit S89-16. Station

Records and Procedures. was performed for items pertaining to control

room drawings.

The findings. corrective actions. and current status

bf the audit items were discussed with the lead auditor in this area.

The inspector concluded that an adequate audit was conducted in this

area. This !FI is closed.

8.

Installation and Testing of Modifications (37828)

This inspection effort included a review of onsite activities and hardware

associated with the installation of plant modificatioris and .a verification

that related modifications activities are * in confc;>rmance with the

applicable licensing requirements.

This review inclu~ed a plant walkdown

to identify recent or temporary modifications. a review of the current

temporary modifications in place. and a review of several minor and major

modifications.

a.

Minor Modifications

The station currently has* two methods that modify systems and

components.

The design change .. program has his tori cal ly been used for

major plant modifications performed by*construction with an extensive

engineering review and approval process prior to turning a

modification over to the station.

Minor modifications have been

  • handled using the EWR program that typically utilizes station

engineering and maintenance.

A programmatic review of the EWR

process was *dqcumented in Inspection Report 220.221/89_;39.

That

review cone 1 uded that previously fdentified weaknesses have been

aggressively pursued.

During this inspection period~ the inspector

questioned the philosophy of having two different programs for

modifications and was informed of a program under development that

encompasses both minor and major modifications.

Implementation of

this new program is currently scheduled to begin this Spring. with an

eventual elimination of the EWR process~

The inspector conducted numerous plant walkdowns during this

inspection period with an emphasis* on minor modifications and

concluded. in general. that adequate control was being maintained.

One example was identified. however. whe~e the licensee could not

  • produce any documentation regarding the modification.

This example

involved a pressure gauge installed on the seal assembly vent

connection of the Unit 1 outside recirculati-On spray pump 1-RS-P-2A.

The gauge had no needle or glass face. and was not shown on any

approved station drawing nor carried as a temporary modification.

The recirculation spray p~mp is used in post-accident conditions to

13

draw water from the containment sump and supply if- back to the

containment spray rings.

A failure at this gauge~ coupled with the

gauge isolation valve being open, could compromise the seal integrity

of the pump.* After identification of the issue, the licensee had the

gauge removed.

Although the safety significance of this condition

is limited by the gauge being installed at a vent connection down-

~tream of a normally closed valve, this is identified as a violation

for failure to provide and/or follow procedures with regard to the

modification process.

The vi6lation is being classified as an NCV,

50-280,281/90-01-03; in that the criteria specified in Section v; of

NRC Enforcement Policy were satisfied.

The inspector also questioned the temporary lighting and sump pumps

that are installed in the safeguards valve pit on both units.

The

various power supplies and control devices which are located in the

safeguards valve pit, have no labels and are in a general state.of

disrepair. This i~stallation has been in place for several years yet

the condition is not annotated on any drawing nor GOntrolled as a

temporary modification.

Permanently installed pumps, as depicted on

station drawings, have been inoperable for many years.

Although

flooding of the pit should not hinder the operability of the.

  • components, it does create a problem with maintenance and introduces

the possibility of exterior pipe corrosion.

The inspector questioned

the threshold for determining a need for temporary modifications and

discussed the specifics of this situation with station management.

The licensee position was that although they believe that the

installation of sump pumps should be .allowed withoµt any formal

modification controls, they stated that a more detailed evaluation

regarding the use of sump pumps would be performed to ensure that

adequate controls are maintained.

The inspector concluded that the

licensee actions were adequate.

b.

Major Modifications

During this inspection period, a major plant modification associated

with the resin transfer facility was reviewed.

The selection of this

modification was due, in part, to *a break in. the instrument* air

system that occurred on January 5.

This break, located within the

modification area boundary, resulted in a transient in the plant

instrument air System.

The initial area of concern, as documented in

deviation report Sl-90~23, was that the broken air pip~ was not shown

on the appropriate control room drawing.

Further investigation

revealed the break location to be in a portion of the instrument air

system being installed for the new resin blend facility.

This

construction effort is being conducted in accordance with Design

Change 85-16 and had not been certified and turned over to plant

operations.

The inspector reviewed the above design change, procedures, and

supporting documentation a~sociated with the demolition and*

construction of a new resin waste disposal system.

Construction of

the new system was essentially complete in November 1988.

However,

14

final functional testing determined that major design flaws existed

  • in the system.

Redesign and rework of the system was initiated in

early 1989 and functional testing has now been resumed.

The design

change that performed this work had.l39 field changes in effect at

the end of this inspection period.

The inspector also reviewed procedures and jumpers associated with

resin transfers pe~formed during 1989 and noted that portions of the

modified system had *been u~ed to transfer contaminated _resin prior to

completion of the design change.

The design ~hange program utilizes

a partial technical review process to place in service .smaller

segments of a larger modifications as :they are completed.

This

requirement *is specified in station administrative procedure

SUADM-ENG-03.

11Design Changes

11 * which also requires that SNSOC

approve the technical review prior to operability of equipment

affected by a design change.

This requirement was implemented during

the first half of 1989 in response to an NRC violation in this area.

The inspector reviewed the licensee*~ response to this violation ahd

concluded that corrective actio*ns had been* implemented in June 1989.

These corrective actions require t_hat a partial technical review

process should be initiated by t~e craft for turn ove~ of part of a

modified system prior to completion and testing of the entire modifi-

cation. * This partial closeout requires engineering concurrence for

~ork not completed. * Engineeiing is also responsible for completion

of the installation verificati6n that includes system walkdowns and

documentation that shows the portion of the system being turned over

for operation is complete.

In addition. this review identifies

drawing and procedure revisions that are required.

The completed

par ti a 1 techni ca 1 review package is then presented to SN SOC for

review and approval.

The inspector determined that there had not

been any partial technical reviews performed on Design Change 85-16

up to the time of this inspection.

Additional reviews determined that on at least two occasions after

June. 1989, equipment was used by operations that was installed or

modified by this design change yet the equipment had.not been through

the technical review process.

One of the events involved the - *

contamination of three employees that were attempting to operate a

portion of the system that was modified by the design change.

This

event was discussed in inspection report 89_-34 and resulted in a

violation .. The licensee initial evaluation of this eve~t concluded.

in part. that procedures and/or instructions were inadequate.

The inspector

1 s discussions with the design. engineers involved

indicate that although a formal engineering installation verification

was not performed, design did review the status of the system

~onstruction and testing and felt confident that the portion of the

system being considered for use would perform as required.

After

discussion between the inspector and the licen~ee. applicable control

room drawings were revised on January 30. 1990 *. to match the plant

,;

15

configuration. After these discussions~ the inspector concluded th~t

the licensee investigation into the contamination event up to this

.point had not identified problems which would have been ~ddressed by

the technical review process.

During the inspection. it was also concluded that the interface

between the post-modification test group (Advisory Operations) and*

normal plant operations department was weak.

This group uses generic

test procedures wit~ no formal instructions regarding isolation

and/or pl ant operations.

Their testing frequently energizes

  • equipment or aligns untested/modif.ied equipment to plant systems

after only a verbal discuss.ion with the shift supervisor.

The

inspectors held a meeting on January 30 with senior managers to

better understand thts interface and the circumstances surrounding

this modification.

The licensee concluded that adequate controls

were not in place regarding the Advisory Operations process and

initiated action on February 1. 1990. to require a technical review

prior to Advisory Operations aligning the modification to the plant

for testing.

This change should ensure that the control room

drawings and procedures are updated to reflect the modifications

prior to clearing the plant isolatio~. * The ins~ectors concluded that

this action was adequate; however~ they expressed concern .over the

absence of a detailed post-modification test program for control of

plant configuration.

This *concern was di!:;cussed with station

management and they consider that present post-modification testing

control is adequate.

However. after additional discussion. the

Station Manager committed to conduct a review of post-modification

testing control.

The operating procedures and installation of jumpers used for resin

. transfer were found to be vague with numerous mi nor errors.

The

specific resin flowpath used was not apparent from the available

documentation. nor was the flowpath annotated.on an approved station

drawing that was available in the control room. In addition. design

~hange 85-16 was inadequate in that it did not isolate ,the instfument

air system while modifications were being performed. This condition

contributed to the plant instrument air transient that occurred on

January 5. 1990.

The inspectors discusse~ the above findings with station management

throughout the inspection period.

The licensee had suspended resin

movement following the station management briefing of the contamina-

tion event in September. pending the development of more detailed

operating procedures.

Contaminated resin has not been discharged

since that event.

It should also be noted that the licensee had

previously implemented a policy that required SNSOC approval to

transfer resin.

This review and approval process failed to identify

that portions of systems were being used witho~t the proper technical

review.

The inspectors consider that the coordination between

station disciplines were certainly aggravated by the problems and

delays associated with this modification.

16

The inspecto.rs concluded that the lack of compliance with prescribed

management programs, such as technical reviews and procedures, ~oupled

with the lack of adequate procedures regarding system isolation and the.

control of plant configuration during post-modification testing, indicate.

a significant deficiency with regards to the modification and operation of

the resin facility project.

The above examples of a failure to provide

and/of follow procedures pertaining to this project is identified as an

NCV (280,281/90-01-03).

The violation is not being cited because the

criteria specified in Section V. of the Enforcement Policy were satisfied.

In addition, the contamination event was previously identified as a

violation in NRC Inspection Report 280,281/89-34.

9.

Evaluation of Licensee Self-Assessment Capability (40500).

On January 26, 1990, thi: inspector visited the licensee

1 s corporate

offices to attend the corporate nuclear safety meeting and to discuss

current organization and pl ans with the corporate nuclear safety staff.

This monthly meeting is required by TS 6.1.C._2.d.

Included in the

discussion were current issues of interest

to both the NRC and the

industry, recent reactor trips and other events which occurred at each of

the nuclear stations, and a discussion of the -~pcoming EOP assessment

which will be conducted in February at the Surry Power Sta.ti on.

The.

inspector a*lso was provided a copy -of the proposed corporate nuclear

safety assessment schedule for 1990.

The inspector noted that assessments

are scheduled in the areas of operations_, mainte*nance, procedures, and

other programs being implemented.

Also noted on the schedule was a

condition where the licensee would be exchanging personnel with other

utilities during performance of the other utility

1 s assessments in similar

areas.

The inspector considers that the licensee

1s proposed assessment

program and schedule appears to be aggressively focused at past problem

areas and is a strength.

The implementation and effectiveness of the

licensee

1s assessment program will be monitored and inspected in future

inspections.

Within the area inspected, no violations were identified.

10.

Exit Interview

The inspection scope and findings were summarized on February 6, 1990,

with those individuals identified by an asterisk in paragraph 1.

An

_additional exit was held with the Station Manager on February 9, 1990 to

clarify some of the issues and to obtain the commitments discussed below.

During this inspection period,* no violations or- deviations were

identified.

A strength was identified with regards to the licensee

I s

proP-osed program and schedule for conducting future safety assessments of

major areas at the Surry Power Station (paragraph 9).

However, several

weaknesses were identified in several functional* areas including

operations, maintenance/surveillance, and en~ineering/ tethnical support .

17

These weaknesses were:

.

.

The 11 censee' s -actions for ensuring that operations has good

capabilities to determine RCS leak rates have not occurred in a

tim~ly manner (paragraph 3.g).

In the maintenance area. a weakness was identified in the way some

balance of plant components were worked during the past refueling

outages (paragraph 4.a).

Deficiencies in planning and procurement activities were .. identified _

as weaknesses in the.maintenance/surveillance area {paragraph 4.c).

Another exampJe was 1dentified of a weakness previously documented_ in

Inspection Report 280.281/89-34 concerning a lack of aggressive

identification and evaluation of anomalies that occur during

.*surveillance testing (paragraph 5.a).

Also. significant weakneises were identified in an inspection of the

plant modification process.

One example was identified with regards

to an unauthorized modification to a recirculation spray pump.

In

addition. work associated with the fnstallation of a new resin blend

facility was found deficient in that adequate modification boundary

isolation was not established which contributed to a plant instrument

air transient.

The inspectors concluded that licens~e investigation

into the contamination event up to date had not identified problems

which would have been addressed by the technical review process.

_ This inspection effort also identified programmatic weaknesses

associated with the procedural guidance and plant configuration

control during post-modification testing. This concern was discussed

with station management

and

they consider that present

post-modification testing control is adequate.

However.* after

additional discussion. the Station Manager committed to conduct a

revi~w

of post-modification testing crintrol.

An

NCV

(280.281/90-01-03) was identified for failure to provide and/or

fo1low procedures for the above problems.

(paragraph 8).

During closeout of LER 280/89-41. (paragraph 6) an NCV was identified for

failure to meet the requirements of TS 3.22 when taking a safety-related

fan out of service (280/90-01-01).

During closeout of LER 281/89~12. (paragraph 6). an NCV was identified for

failure to comply with the requirements of TS 3.12~E (281/90-01-02).

.

.

'

The licensee* acknowledged the inspection findings and generally agreed

with the inspection conclusions.

The lice1_1see did not identify as

proprietary any of the materials provided to or r.eviewed by the inspectors

during this inspection.*

.

11.

I_NDEX OF ACRONYMS AND INITIALISMS

AFW

AUXILIARY FEEDWATER


~

.,

" '

ij:

18

ANSI

AMERICAN NATIONAL STANDARDS INSTITUTE

AP

ABNORMAL OPERATING PROCEDURE

CAD

COMP.UTER AIDED DESIGN

CAL

CONFIRMATION OF ACTION LETTER

cc

COMPONENT COOLING

ccw

COMPONENT COOLING WATER

. CFR

CODE OF FEDERAL REGULATIONS

CLS

CONSEQUENCE. LIMITING SAFEGUARD

CRO

-

CONTROL ROOM OPERATOR

cw

CIRCULATING WATER

DPI

DELTA PRESSURE INDICATORS

DR

DEVIATION REPORT

EOG

EMERGENCY DIESEL GENERATOR

EHC

ELECTRO-HYDRAULIC CONTROL

EMP

ELECTRICAL MAINTENANCE PROCEDURE

EOP

EMERGENCY OPERATING PROCEDURE

ESF

ENGINEERED SAFETY FEATURE

ESW

EMERGENCY SERVICE WATER

EWR

ENGINEERING WORK REQUEST

GDC

GENERAL DESIGN CRITERIA

GPM

GALLONS PER MINUTE

HP

HEALTH PHYSICS

HX

HEAT EXCHANGER

HPSI

HIGH PRESSURE SAFETY INJECTION

HSD

HOT SHUTDOWN

IA

INSTRUMENT AIR

IE

INSPECTION AND ENFORCEMENT

IFI

INSPECTOR FOLLOWUP ITEM

IRSP

INSIDE RECIRCULATION SPRAY PUMP

IOER

INDEPENDENT OFFSITE EVALUATION!REVIEW

!RPI

INDIVIDUAL ROD POSITION INDICATION

ISI

INSERVICE INSPECTION

LER

LICENSEE EVENT REPORT

LCO

LIMITING CONDITIONS OF OPERATION

LHSI

LOW HEAD SAFETY INJECTION

LOCA

LOSS OF COOLANT ACCIDENT

LOOP

.,.

LOSS OF OFFSITE POWER

MER3

MECHANICAL EQUIPMENT ROOM 3

MDV

MOTOR OPERATED VALVE

.

MCR -

MAIN CONTROL ROOM

NCV

NON-CITED VIOLATION

NOP

NORMAL OPERATING PRESSURE

NRC

NUCLEAR REGULATORY COMMISSION

NRR

NUCLEAR REACTOR REGULATION

OP

OPERATING PROCEDURE

ORS

. OUTSIDE RECIRCULATION SPRAY

PCV

PNEUMATIC CONTROL VALVE

PI

PRESSURE INDICATOR

PM .

PREVENTATIVE MAINTENANCE

PRT

PRESSURIZER RELIEF TANK

I

I

.; .... *~ .

~ .

,.'

...... "'

. ,.

PSI-

PSIG

PT

QA.

QC

RAI

RCS

RHR

RG

RO

RPS

RMT

RSHX

RSS -

RWP

RWST

SCFM.

SER

SI

SNSOC

sov

SPDS

SRO

SW

  • TAVG

TI

TS

TSC

UFSAR

URI

UV

vs

19

POUNDS PER SQUARE INCH

POUNDS PER SQUARE INCH GAUGE

PERIODIC TEST

QUALITY ASSURANCE

QUALITY CONTROL

RESIDENT ACTION ITEM

REACTOR COOLANT SYSTEM

RESIDUAL HEAT REMOVAL

REGULATORY GUIDES

REACTOR OPERATOR

REACTOR PROTECTION SYSTEM*

RECIRCULATION MODE TRANSFER

RECIRCULATION SPRAY. HEAT EXCHANGER

RECIRCULATION SPRAY SYSTEM

RADIATION WORK PERMIT

REFUELING WATER STORAGE TANK

STANDARD CUBIC FEET PER MINUTE

SAFETY EVALUATION REPORT

.

SAFETY INJECTION

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SOLENOID OPERATED VALVE

SAFETY PARAMETER.DISPLAY SYSTEM

. SENIOR REACTOR OPERATOR

SERVICE WATER

AVERAGE TEMPERATURE,OF RCS

TEMPORARY INSTRUCTION

TECHNICAL SPECIFICATIONS

TECHNICAL SUPPORT CENTER

. UPDATED FINAL SAFETY ANAL YSlS REPORT

UNRESOLVED ITEM

UNDER VOLTAGE

VENTILATION SYSTEM